WATER CONSERVATION & QUALITY IMPROVEMENT INITIATIVES 2013 Presentations/Day-2 at PMI... · WATER...

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WATER CONSERVATION & QUALITY IMPROVEMENT INITIATIVES H.S.BAGGA VINOD RATAN PRAG SOOD

Transcript of WATER CONSERVATION & QUALITY IMPROVEMENT INITIATIVES 2013 Presentations/Day-2 at PMI... · WATER...

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WATER CONSERVATION & QUALITY

IMPROVEMENT INITIATIVES

H.S.BAGGA

VINOD RATAN

PRAG SOOD

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From Industrial prospective, High cost, strict environmental regulations & poor availability of fresh water has emerged as one of the big challenges and driven the industries towards “Reduce, Reuse and Recycle” of the precious natural resource.

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Plant overview

Kawas Gas Power Project An ISO 9001:2008; 14001:2004;OHSAS 18001:2007;SA 8000 :2008

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Location Hazira-Surat-Gujarat

Installed Capacity Stage-I 656.2MW (2 CC Modules)

Type Combined Cycle Gas Power Plant

Gas Turbines 4 Nos. GE 9001 E 106 MW

Steam Turbines 2 Nos. Alsthom Rateau 116.1MW

Fuels Natural Gas: RLNG: Naphtha: HSD

Source of Water River Tapti. Pump House at Variav

Evacuation Thru’ 220 KV Transmission lines

Beneficiaries Gujarat, MP, Maharashtra ,DNH Chhattisgarh, Daman & Diu

NTPC Kawas (Stage - I) An ISO 9001:2008; 14001:2004; OHSAS 18001:2007; SA 8000 :2008

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SOURCE OF WATER

Since commissioning of the plant in 1993. Raw water for the project was sourced through irrigation canal of river tapi flowing very near of the plant

NTPC, Kawas along with other industries of Hazira belt and Surat Municipal Corporation constructed a weir at Siganpore Weir in 1996 (around 18 km away from the project)

Raw Water fed through Intake channel up to Two Reservoirs of Capacity approx. 18.5 Lac Cu.M, with Water distribution in the ratio of 1:4.

Since then Water is drawn from Siganpore Weir ( Upstream of River Tapi) at Variav through 16 KM pipeline having pumping capacity of 1500 Cu. M/Hr.

Reservoir Capacity ( Lacs CuM) at 3.9 meters depth

Capacity ( Lacs CuM) at normal operational [ 2.5 m]

Retention Time ( Days)

Live 4.69 2.9 14 days

Dead 13.93 8.78 44 days

In 1996 Gujarat Government intimated its inability to continue the supply of water from the irrigation canal to the project due to rapid industrialization in the Surat region

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Variav Pump House

NTPC KAWAS

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WATER USAGE AREA AT PLANT

• 680 M3/hr • 45 M3/hr

• 45 M3/hr

• 50 M3/hr

DM Water

(For cycle & non cycle makeup)

Drinking

Water (plant &

township)

Make up to

Cooling water

system

Service

Water

Average Daily water usage of 21000 M3/Day when plant runs at full load

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WATER CONSUMPTION PATTERN

Year

Total Water Consumption

(M3) Generation (MU)

Specific water consumption

[L/KWhr]

2010-11 6759893 3882.114 1.741

2011-12 6611950 3608.422 1.832

2012-13 3585786 2193.878 1.634

1.500

1.550

1.600

1.650

1.700

1.750

1.800

1.850

2010-11 2011-12 2012-13

Specific water consumption [L/KWhr]

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WATER CHARGES AT KAWAS

This incremental hike @ 10 % in water charges is likely to get double @ Rs 28 – 30 / CuM from next FY 2013-14 as per recent proposal put up in front of state government after exhaustive survey & deliberation

done during a study carried out by a reputed institute.

WATER CHARGES CALCULATION

Particular As on Jan 2013 Anticipated by FY 2013-14

charges for water drawn through VARIAV pump house, Ave.18000 M3/Day

@Rs. 14.34 per M3 @ Rs. 28.68 per M3

Chemical Cost @Rs. 1.23 per M3 @Rs. 1.23 per M3

Water Cess @Rs. 0.05 per M3 @Rs. 0.05 per M3

Pumping & Maint cost & Variav pump house Ave. Rs 20 Lac/Month

@Rs. 3.70 per M3 @Rs. 3.70 per M3

Industrial water cost to site @Rs. 18.09 per M3 @Rs. 18.09 per M3

Process water cost inclusive of chemical @Rs. 19.32 per M3 @Rs. 33.66 per M3

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NTPC KAWAS Financial figures of last 3 yrs (in Crores)

YEAR O&M Cost Station overheads Water charges

% of Overheads

2009-10 70.32 27.66 7.07 24.6 %

2010-11 84.28 30.88 7.43 24.5%

2011-12 85.78 31.18 7.79 25.1%

IMPACT OF WATER CHARGES ON PROFITIBILITY

Profit of Project = FIXED COST RECOVERY +MARGINAL GAIN-EXPENSES

O&M Cost Is the Major Component of EXPENSES

WATER CHARGES plays a significant role in the profitability of project

Decrease in WATER CHARGES can increase the profit of plant

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INITIATIVES TAKEN TO REDUCE WATER CONSUMPTION

• WATER CONSERVATION THROUGH INCREASE IN COC FROM 1.65 TO 5.0

• SWAS RECYCLE

• USAGE OF CW BLOWDOWN FOR HORTICULTURE PURPOSE

• CHECKING OF WHRB V/V PASSING DURING SHUTDOWN

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INCREASE IN COC FROM 1.65 TO 5.0

As per the design COC of 1.65 the water requirement was @ 2000 m3/hr

In the year 1996 the water source is shifted to Singpaur Weir at 18km

It forced to think on reduce the plant make up by operating the Circulating water system at a higher Cycles of Concentration (COC)

Site filtration skid to for continuous filtration of 1.25% of CW Water (1050 M3/hr) & Dedicated CW Chemical Treatment plant was commissioned to maintain the water quality

COC was increased to 5.0 from design of 1.65

WATER SAVING = 1000 M3/HR (50% of Original consumption)

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Recycling of SWAS Drains

Original Header of

SWAS Drains

New Header of

SWAS Drains

WATER SAVING 20 M3/DAY

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TAPPING TAKEN FROM CW BLOW DOWN LINE FOR HORTICULTURE USAGE

WATER SAVING 45 M3/DAY

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CW WATER USED FOR HORTICULTURE USING WATER

SPRINKLERS

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IDENTIFICATION OF V/V PASSING

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INITIATIVES TAKEN FOR IMPROVEMENT IN WATER QUALITY

• ISOLATION OF DEAD RESERVOIR

• SEPARTAION OF CLARRIFER

• ULTRA FILTRATION SYSTEM IN TOWNSHIP.

• REPLACEMENT OF DRINKING WATER/SERVICE WATER PIPELINES

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PROBLEM OF DEAD RESERVOIR WATER QUALITY

– Deterioration in Raw Water Quality • Increased industrialization

• Non release of water to Tapti river.

– Increased C0C to 5 from Design value of 1.65 • Increased stagnation time in reservoir due to low water

requirement

• Plant Water requirement reduced @ ~ 1000 M3/Hr from design

– Carry over of High Organics present in raw water and that originated from casurina trees to Dead reservoir.

– Due to High Retention Time ( > 30 days) in dead reservoir, Concentration of Organics are getting multiplicated.

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Earlier water quality at Dead Reservoir

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After water quality at Dead Reservoir

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Impact of Dead Reservoir Water on the Plant Process & Other Systems

• Severe Foaming in CW Forbay.

• Organic fouling / deposits in condenser tubes

• Disturbance in boiler chemistry due to carry over of organics to drums .

• Difficult to maintain ACC < 0.3 uS/cm

• Deterioration in MB o/l Quality.

• Difficult to achieve Cond < 0.3 uS/cm

• Reduction in OBR of DM Plant from 600 to 250 M3 .

• Specific Consumption of Chemicals increased.

• Red Worms Problems

Drinking Water

DM Plant

CW System

Boiler Cycle

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Various steps done to improve water quality

Improvement observed in the various processes.

Dead Reservoir has been isolated since Jan’2009.

It has been decided to Isolate Dead reservoir & fresh water to be taken through live reservoir only.

Joint Committee of M/s NETRA and Site representatives did a comprehensive study

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Benchmarks achieved in Quality of Water in 2012

• MB Outlet conductivity of 0.051 uS/cm

• DM Storage Tank Outlet conductivity of 0.22 uS/cm.

• After Cation Conductivity (ACC) of 0.09 uS/cm in SWAS system

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SEPARATION OF CLARIFIER

• Common outlet channel of two clarifiers has been separated.

• One clarifier is used for DM & Potable Water System @ 20 -30 % design flow to increase retention time thereby improving the clarification process

• Other clarifier is used for make up to CW system.

Better Organic

&

Turbidity Control

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Separation of clarifiers

New outlet line Laid for Clarifier -02

This modification of isolation of clarifiers has resulted in significant improvement in the DM water quality and maintaining ACC in the boilers.

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•1st in any NTPC Station •Specifically dedicated for drinking water purpose •Consist of Carbon filter, micro filter, UF Skid & storage tanks

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ULTRA FILTERATION PLANT OPERATIONAL & PERFORMANCE REPORT OF JAN-2013

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SCHEME OF EFFLUENT DISCHARGE AT JHANOR

Year Effluent discharged (M3) DM Water Consumption (M3) DM water

consumption as %

of Effluent disposed

2009-10 1350930 890668 66%

2010-11 1203365 745020 61.9%

2011-12 1054935 532369 50.4%

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PIL PILOT UNIT SCHEME

A pilot study was conducted at site by M/s Pall Filtrations with MF+RO combination skid to treat CW blow down water, which is the major constituent of the combined effluent.

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PIL OUTCOME OF PILOT STUDY AT JHANOR

The quality of output from MF+RO skid w.r.t chemical parameters is such that it can be directly used as inlet to DM Plant for polishing and further use. It can reduced water consumption by 60% Recycling the effluents, in this manner, will fetch benefits in terms of reduced chemical consumption in DM plant, lower power consumption in the effluent disposal system and a big leap towards zero discharge.

On similar lines, NTPC Kawas has also initiated proposal for

recycling the CW Blow Down water @ 150 – 200 M3/Hr and utilizing

the same in CW system as make up, which will reduce the fresh

water consumption of the plant by ~ 20 % and effluent generation

will be reduced by ~ 75 %.

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VARIOUS STUDIES DONE TO CONSERVE WATER

• RAIN WATER HARVESTING IN YEAR 2012-13

• WATER BALANCE STUDY WITH THE HELP OF THERMAX 2011-12

• STUDY OF BTF LEAKAGE PROBLEM THROUGH CMI, BELGIUM IN YEAR 2012-13

• CANAL TOP SOLAR PROJECT FOR RAW WATER CANAL YR 2012-13

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RAIN WATER HARVESTING STUDY

Study being carried through M/s Furaat Earth Pvt ltd, Ahedabad to assess the potential of rain water harvesting at NTPC – Kawas Report envisages that with average rainfall of 1300 mm @ coefficient of 60 %, there is potential to harvest approx 18 lacs M3 of rain water considering the entire plant area of 560 acres. Report has identified following three potential points from where the rain water can be harvested. •COOLING BAY •OPEN INTAKE CHANNEL •ROOF TOP RAIN WATER FROM BUILDING

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RAIN WATER HARVESTING STUDY

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MODULAR SYSTEM FOR ROOF TOP WATER HARVESTING

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WATER BALANCE STUDY BY THERMAX

A comprehensive Water Balance Study was carried out in 2011 - 12 by M/s Thermax – To assess the gaps in the various

process water consumption / usage pattern

– To identify the areas for recycling of the effluents

– To improve the overall efficiency of the plant through installation of energy efficient devices, wherever applicable.

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STUDY OF BTF LEAKAGE PROBLEM THROUGH CMI, BELGIUM

• OEM of WHRB, M/s CMI, Belgium was awarded

to study the boiler tube leakage problem at Kawas.

• CMI representative visited site for study & assessment of problem.

• Observation of Comprehensive Report:- – HP2 SHT Inlet Header to be relocated to be modified

for complete draining during shut downs. – Provision of extra drain valves before & after

Desuperheating temperature control valves.

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FEASIBILITY STUDY OF CANAL TOP SOLAR PROJECT AT NTPC KAWAS

Feasibility Report

Canal Top solar project is feasible.

Expected cost of project = Rs 4 Crores

Expected Solar Output of project = 0.3 MW

Installation Time = 6-8 months from LOA

Site Feasibility survey has been completed by M/s Sunedison (I) Ltd [ Party who has carried out India’s 1st Canal Top Solar

Project].

Canal Top Solar project has been identified as S.D. Project of Kawas.

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PAY BACK PERIOD OF VARIOUS INITIATIVES

Initiative Actual/anticipated water saving /yr

Approx. Initial Cost

Pay Back period

Running at higher COC of 5 compare to design of 1.65

87.6 Lacs M3 2.5 Crores 6 months

Recycling of cooling water blow down water for horticulture purposes

0.164 Lacs M3 0.5 Lacs 2 months

Recycling of SWAS drains 0.073 Lacs M3 0.5 Lacs 4 months Rain water Harvesting 6 Lacs M3 10.0 Lacs 2 months Recycling of CW Blow down to achieve ZERO EFFLUENT DISCHARGE

14 Lac M3 21 Crores 7 years

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TOGETHER WE CAN TOGETHER WE WILL

MAKE THE DIFFERENCE

Thank you!

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Comparison of Water Charges in Western Region

This incremental hike @ 10 % in water charges is likely to get double @ Rs 28 – 30 / CuM from next FY 2013-14 as per recent proposal put up in front of state government after exhaustive survey & deliberation

done during a study carried out by a reputed institute.

State Project name Water Charges ( Rs / CuM)

Madhya Pradesh Vindhyachal 4.00

Chhattisgarh Korba, Sipat 7.24

Gujarat Kawas, Jhanor 14.64