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Transcript of The Palmdale Fuel Cell Project: Five-Year Review SCAP Energy Management Committee Meeting Mark...
The Palmdale Fuel Cell Project: Five-Year Review
SCAP Energy Management Committee Meeting
Mark McDannelLos Angeles County Sanitation Districts
July 28, 2009
Presentation Overview
Facility Descriptions and Design Parameters
ResultsLessons Learned & Conclusions
Antelope Valley Green Energy Program
Parallel renewable combined heat and power projects using digester gas
Similar size units at similar size plants250 kW Fuel Cell Energy molten
carbonate fuel cell at Palmdale 250 kW Ingersoll-Rand microturbine at
Lancaster
Palmdale Water Reclamation PlantPalmdale Water Reclamation PlantSTARTED: NOVEMBER 1952 CAPACITY: 15 MGD CURRENT FLOW: 9.2 MGD
Project Design Data
Manufacturer Fuel Cell Energy
Rated unit output, gross 250 kW
Net system power output 225 kW
Startup date 2005
Electrical efficiency (LHV) 47%
% of heat input recovered as waste heat
26%
Combined heat and power efficiency 73%
2005 Performance Test Data
Gross power output 251 kW
Electrical Efficiency 46%
Palmdale Fuel Cell Project
Fuel Cell Energy molten carbonate fuel cell
Capital cost $2.4 million
50% of cost recovered from SGIP
Fuel Cell Project Team
Quinn Power Systems Associates Prime contractor Operation and maintenance under contract to LACSD
Fuel Cell Energy- Fuel cell supplier Subcontracted to Quinn for fuel cell O&M
SCS Energy- Design and installation Gas treatment skid o&m
Facility ownership retained by LACSD
Fuel Cell Fuel Skid
Load Profiles at Palmdale Electricity Purchase Load Profile With and Without Fuel Cell In
Service (typical days)
0
50
100
150
200
250
300
350
400
0:00
0:45
1:30
2:15
3:00
3:45
4:30
5:15
6:00
6:45
7:30
8:15
9:00
9:45
10:3
011
:15
12:0
012
:45
13:3
014
:15
15:0
015
:45
16:3
017
:15
18:0
018
:45
19:3
020
:15
21:0
021
:45
22:3
023
:15
Time
Lo
ad (
KW
)
Fuel cell at full loadFuel cell out of service
Results
Plant PerformanceEconomicsSiloxane RemovalLessons Learned & Conclusions
Fuel Cell Availability and Capacity
58.2%
70.2% 69.8%
76.5%
42.6% 41.5%35.8%
31.8%
0%
10%
20%
30%
40%
50%
60%
70%
80%
90%
2005 2006 2007 2008
Availability Capacity Factor
Fuel Cell Availability and Capacity
Availability has increased during the program
Capacity has decreased despite improvements in availability
Capacity factor well below 90% target
Breakdown of Downtime
0%
10%
20%
30%
40%
50%
60%
70%
2005 2006 2007 2008
% T
ime
Un
avai
lab
le
Unknown/Other
Planned OutageDistricts' Equipment
SCE GridFuel Skid Outage
Power Equip. Outage
Palmdale Availability
Fuel cell balance of plant equipment Routine repairs on water treatment
systemMultiple significant fuel skid issuesFour electrode stack replacementsCarbon filter media replacement
Stack Replacements
Four stack replacements 3975 hrs - Replaced with new stack
design 2696 hrs – Stack degradation 5386 hrs - Sulfur poisoning & excessive
startups 9889 hrs - Sulfur poisoning
Causes of Capacity Reduction at Palmdale Fuel Cell
Frequent long time periods at reduced loads due to fuel cell issues
Variations in digester gas pressure due to issues with the fuel skid
Lower digester gas flows and higher methane content due to sewer cleaning
Defective stack installed in 2008
Causes of Capacity Reduction at Palmdale Fuel Cell, ctd
Long start up times after outagesParasitic Loads
Internal fuel cell loads of 18-20 kW not counted against net, but cost plant when fuel cell is in hot standby
Fuel skid, 25 kW (design value, not metered)
Three sulfur poisoning events have resulted in reduced power output for several months
Net Electrical Generation per Quarter
0
20
40
60
80
100
120
140
160
180
200
220
240
260
Q1
2005
Q2
2005
Q3
2005
Q4
2005
Q1
2006
Q2
2006
Q3
2006
Q4
2006
Q1
2007
Q2
2007
Q3
2007
Q4
2007
Q1
2008
Q2
2008
Q3
2008
Q4
2008
Q1
2009
Net
Po
wer
, kW
Rated Net Output
Other Issues at Palmdale
Integration into plant digester gas system including flare and boilers was complex
Remote monitoring and operation help minimize down time
Installation of natural gas line was necessary for backup and controlled shutdown
Capital Cost
Fuel Cell $1,178,000
Fuel Treatment Skid $201,600
Installation $526,301
Control Room Signal $2,895
Gas Piping Installation $2,511
Satellite Internet $5,328
Warranty $330,000
Sales Tax $113,817
SCE Interconnection $3,038
Natural Gas Piping $19,084
Total Capital Cost $2,382,574
SGIP Rebate -$1,125,000
Net Cost to Districts $1,257,574
Facility Economics (design, assuming 90% capacity factor)
Capital Cost $2,382,574
Subsidies $1,125,000
Net cost $1,257,574
Annual power purchase savings (at 90% capacity factor)
$227,000
Total subsidized production cost /kW-hr
$0.093
Operation and maintenance /kW-hr $0.035
Capital recovery /kW-hr $0.058
Retail electricity cost /kW-hr $0.128
Cost of Power Production
$0.190
$0.058
$0.049
$0.035
$0.041
$0.00
$0.05
$0.10
$0.15
$0.20
$0.25
$0.30
$0.35
Design 90% C.F. Actual
$/kW
h
Natural Gas
O&M
Capital Recovery
Average Retail Electrical Price
$0.093
$0.28
Net Savings per Year
2005 $66,5512006 $69,4522007 $46,5432008 $2,119
Cumulative Net Savings
$-
$200,000
$400,000
$600,000
$800,000
$1,000,000
$1,200,000
$1,400,000
Dec-04
Mar-05
Jul-05
Oct-05
Jan-06
May-06
Aug-06
Nov-06
Feb-07
Jun-07
Sep-07
Dec-07
Apr-08
Jul-08
Oct-08
Jan-09
$1,257,574Capital Cost to Districts with
SGIP Grant
$184,665Net Savings Earned through Dec 2008
Siloxane Removal
Carbon absorptionAlso removes Cl, S to protect fuel
cellRequires periodic testing for
breakthroughShort term high siloxane levels
could cause undetected breakthrough
Criteria Pollutant Emissions
NOX 0.05 ppm @ 15% O2
0.0017 lb/MWh
CO 1.2 ppm @ 15% O2
0.025 lb/MWh
TGNMO 2.07 ppm0.016 lb/MWh
Sulfur Compounds
Raw Digester
Gas
Treated Digester Gas
H2S, ppm 20 ND<0.5*
Total Reduced Sulfur, ppm 20 ND<3.5
*Note-detection limit not sensitive enough to fully protect fuel cell
Trace Organic Compounds
Raw Digester
Gas
Treated Digester
Gas
Exhaust
Chlorobenzene, ppb 38 2.1 ND<0.05
Vinyl Chloride, ppb 2.0 0.38 ND<0.05
Benzene, ppb 26 2.4 0.95
Toluene, ppb 830 36 ND<0.27
Recent Operating Status
Stack replaced in Sep 2008.A leak in the new stack forced
reduction in output to 40 kW in Dec 2008
Operated at nearly 100% availability at reduced load
Fuel cell was shutdown June 11 upon discovery of sulfur breakthrough
Unit will not be restarted
Lessons Learned by LACSD
Ambient temperature considerations Chiller was undersized for high summer
temperatures Lower digester gas production during winter
months
Carbon media must be monitored and/or replaced periodically
Site involvementDigester gas system balancing
Lessons Learned by Fuel Cell Energy
Natural gas must be used as a backup fuel
A load bank should be installed to mitigate grid disturbances
Ensure proper maintenance of the fuel skid
Contracting Issues Impacting the Facility
These were demonstration projects; as such, providers would not provide availability guarantees
The current O&M contracts have no performance incentive or penalty: down time costs the owner but does not cost the contractor
Fast response not always justified by plant economics Other contracting options
Incentives and penalties for response time and availability Power purchase agreement, unit owned by provider or third
party These options are generally currently available
Conclusions
The Palmdale fuel cell did not meet performance goals
The Palmdale fuel cell met its goal to demonstrate a high efficiency, low emission technology on digester gas
As an early adopter, Districts allowed manufacturers to address and resolve design and operating issues