Meeting Multiple Challenges: Re-Rating W. A. Parish Unit 8

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Meeting Multiple Challenges: Re-Rating W. A. Parish Unit 8 NOx and Performance Improvements at a 650 MW coal-fired electric generating unit Derek Furstenwerth Manager, Air Resources Division, Environmental Department Reliant Energy

Transcript of Meeting Multiple Challenges: Re-Rating W. A. Parish Unit 8

Page 1: Meeting Multiple Challenges: Re-Rating W. A. Parish Unit 8

Meeting Multiple Challenges: Re-Rating W. A. Parish Unit 8

NOx and Performance Improvements at a 650 MW coal-fired electric generating unit

Derek FurstenwerthManager, Air Resources Division,

Environmental DepartmentReliant Energy

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Who Are Reliant Energy and Texas Genco?

• Reliant Energy – Top 10 Generator of Electricity in US– 21,000 megawatts– Operates in 13 states– Also provides support to Texas Genco

• Texas Genco– Former HL&P power plants– 14,400 megawatts total, 12,000 in Houston area– Created as result of Texas Electric Power Industry

Restructuring– Subsidiary of CenterPoint Energy, Reliant to

purchase in 2004

Page 3: Meeting Multiple Challenges: Re-Rating W. A. Parish Unit 8

W. A. Parish Station Description

• Located on a 4880 acre site near Thompsons, Tx

• Four gas-fired and four coal-fired steam generators, plus a 13 MW gas turbine generator. Total gross capacity of over 3800 MW (largest fossil plant in U.S.)

• Approximately 360 employees

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W. A. Parish Station

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W. A. Parish Unit Information

Gas196713GTCoal19826508Coal19805907Coal19786906Coal19776905Gas19685654Gas19612903Gas19581852Gas19581851

Primary FuelYearMWUnit

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W. A. Parish Unit 8

• Emission Control Equipment– Baghouse system for particulate control– Low sulfur coal plus flue gas

desulfurization system (FGD) – Low NOx burner/overfire air system– Selective catalytic reduction (SCR)

systems under construction

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What are the Challenges Facing W. A. Parish?

• Houston-Galveston SIP– Lowest Coal Unit NOx limits in nation– Cap-and-trade program

• Restructured Texas Electric Market

Page 8: Meeting Multiple Challenges: Re-Rating W. A. Parish Unit 8

Why Re-rate?

• Restructured Texas Electric Market– Economics based on production– Production dispatched based on lowest

cost– W. A. Parish is low-cost power plant

• New Opportunities– Improved materials– Better efficiencies

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Challenges to Re-rating or“Why doesn’t everyone?”

• New Source Review– BACT– More emission controls– Nonattainment NSR – LAER, offsets

• The Steady Downward March of NOx– NSPS, RACT, SIP Limits– Area-wide NOx reductions – 88% reduction by

2004– More emission controls

» Meeting Multiple Challenges - One stone, two birds

Page 10: Meeting Multiple Challenges: Re-Rating W. A. Parish Unit 8

The Steady Downward March of NOx

•WAP 5 – 8 Coal Fired Regulatory NOX

Limits

0.7

0.50.41

0.150.04

00.10.20.30.40.50.60.70.80.9

1

NO

x lb

/MM

Btu

WAP 5-7Permits(1977)

WAP 8Permit(1979)

NOx RACT(1999)

EPA NSPS(1998)

TNRCC SIP(2004)

Regulatory Limits

Current WAP Operating Levels (0.15-0.20)

W A Parish Coal Unit Regulatory NOX Limits

0.5

0.38

0.150.045 0.03

00.10.20.30.40.50.60.70.80.9

1

NO

x lb

/MM

Btu

WAP 8Permit(1979)

NOx RACT(1999)

EPA NSPS(1998)

TCEQ SIP(2004)

WAP SCRDesign

Regulatory Limits

2002 W A Parish NOx Emissions (0.155)

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Meeting Multiple Challenges –Re-rating Unit 8

• Increase Production Capacity– 10% Increase – from 590 to 650 MW– Improved efficiency

• New Source Review– No significant increase in NOx, SO2, or VOC due

to emission controls – No NSR or NSPS– PSD for CO, PM10, H2SO4 and Fluoride

• Existing equipment determined to represent BACT

• SIP Compliance– SCR under construction

• Operational by end of 2003• Lowest NOx coal plant in country

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W. A. ParishEmission Control Equipment

• Baghouse systems for fly ash removal– Utilize fiberglass bags to

trap fly ash– >99.9% removal efficiency

Unit 5 Baghouse contains ~15,000 bags

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W. A. ParishEmission Control Equipment

• Flue Gas desulfurizationsystem (FGD) for SO2 removal on Unit 8

– Spray tower design– Limestone slurry reagent– SO2 removal of ~80%

Unit 8 FGD System

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W. A. ParishEmission Control Equipment

• NOx Reduction– Advanced LNB/OFA

systems installed on all coal units

• 1st commercial installation of AlstomLNB/OFA system guaranteed to meet 0.15 lb/MMBtu

• 50%-60% NOx reductions achieved

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W. A. ParishEmission Control Equipment

Low NOx design of the Unit 7 & 8 TFS 2000 System

Air injected in theburnout zone

Fuel and air injected in thecombustionzone

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P2tm Coal LNB Nozzle Tip

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LNB Installation

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W. A. ParishEmission Control Equipment

Coal unit SCR'sunder construction– Vanadium-

titanium catalyst– Aqueous NH3

reagent– 80-85% reduction

to meet 0.03 lb/MMBtu

W. A. Parish Unit 8 SCR Retrofit

Fabric Filter

SCR Boiler

FGD

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Texas Coal-fired Unit NOx Rates (2001)

0

0.05

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0.15

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W. A. Parish Unit 6 SCR Construction (May , 2000)

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W. A. Parish Unit 6 SCR Construction (July, 2002)

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W. A. Parish Unit 5 SCR Construction (July, 2002)

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W.A.Parish Unit 8 SCR Construction (April, 2001)

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W. A. Parish Unit 6 Catalyst Loading (July, 2002)

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W. A. Parish Unit 6 Catalyst Loading

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W. A. Parish Ammonia Tank Farm

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W. A. Parish Unit 6 NH3 Injection Nozzles

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W. A. Parish Unit 6 NH3 Mixer

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Meeting Multiple Challenges –Review

• Increased Production Capacity– 10% Increase – from 590 to 650 MW– Improved efficiency

• Reduced Emissions– SCR under construction

• Cleanest coal plant in country• NOx to 0.03 lb/mmBtu design value

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Questions and Answers