JH tan
-
Upload
mohd-isa-harun -
Category
Documents
-
view
218 -
download
0
Transcript of JH tan
-
8/13/2019 JH tan
1/26
No Process Catergory Items Need Prepare Qty
1 MI Tool/jig IC leg bending Jig for U1 IC * check setting 2
2 MI Tool/jig Component storage bin 8
3 MI Tool/jig Solder Iron 3
4 MI Tool/jig Touch up block need lamp 3
5 MI Tool/jig After dipping cooling fan 6
6 MI Tool/jig Touch up Jig 3
7 MI Tool/jig Prevent PCB warpping jig 150
8 MI Tool/jig IC dispencer jig 29 MI Tool/jig AC contact insertion jig 3
10 MI Tool/jig Set-up ICT 2
11 MI Tool/jig Need brush to clean solder ball 2
12 MI Tool/jig air gun for ICT cleaning process 2
13 MI Tool/jig D20 prework jig need review ( process & Qty ) 150
14 Assy Tool/jig PCB breaking jig 3
15 Assy Tool/jig Dummy Battery 14
16 Assy Tool/jig Knock test jig 3
17 Assy Tool/jig Set dismental Jig 1
18 Assy Tool/jig set up Call lamp 4
19 Assy Tool/jig nejico with secondary tray 3
20 Assy Tool/jig Grease dispencer 3
21 Assy Tool/jig IC writer cycle time high = 19 ~ 22s need 3 units 2
22 Assy Tool/jig Case screwing process need top cover jig 3
23 Assy Tool/jig Need battery discharge jig 3
24 Assy Tool/jig Screwing process request sensor to prevent screw missing 3
25 Assy Tool/jig Battery A check cycle time high 35 ~ 39S need 4 units 12
26 MI Set-up MI conveyer & Dipping machine test run
27 MI Set-up Material top up list28 MI Set-up Line set up & relocate Tuner ICT * air supply 2
29 MI Set-up Line ESD confirmation
30 MI Set-up Need to know full MI conveyer PCB Qty ?
31 MI Set-up need to buy off WI D20 , C8 , C37 , C2 sub work process
32 MI Set-up ICT pass stamp date code
33 MI Set-up Need review component insertion sequence
34 MI Set-up ICT coverage vs visual check matrix
35 MI Set-up Check flux vs Dipping joint conveyer condition
36 MI Set-up Test MI conveyer speed Slow -OK ?
37 Assy Set-up Extend packing block
38 Assy Set-up Battery A PC hanging block
39 Assy Set-up ESD, power plug point
TCJ3400 Line Set-up Preparation
12/7 18/7 24/7 1/83 day 8 day 13 day
1st Line 2nd Line 3rd Line
-
8/13/2019 JH tan
2/26
52 Assy Quality Check screw torque
53 Assy Quality Counter to prevent battery A skip process
54 Assy Quality Appearance check template
55 Assy Quality Serial No control method ( lot by lot basic )
56 Assy Quality Material issueing lot by lot basic
57 Assy Quality AC blade carton label attention by colour
58 Assy Quality Equipment setting & spec indication
59 Assy Quality WI need Quality matrix table ( AC blade )
60 Assy Tool/jig Use micro sound scope to check foreign material + dummy set 3
61 Assy Quality Casing rubbing sound
62 Assy Quality Need to prepare difference table AC blade / manual .
63 Assy Quality carton information prefer label type
64 Assy Quality manual prefer change colour possible mix with TAS9700 , template65 Auto Quality Add glue to reduce Dipping solder short
66 Assy Quality carton packing slot too tight , difficult to take out from slot hange
Assy Quality Bar code scanning system
-
8/13/2019 JH tan
3/26
Status When Dept PIC Remark
Eng Design limitation
OK 11-Jul PRD Watie
16-Jul PRD JH Tan
Eng
PRD Razak
Eng
ok Eng
ok 12-Jul PRD JH TanOK Eng Vincent
Eng
ok 16-Jul PRD Watie
OK 16-Jul PRD Watie
study 10-Jul Eng Takanishi
ok Eng
Eng
ok 16-Jul PRD Azri
Eng
18-Jul PRD JH Tan
ok 16-Jul PRD Azri
ok 12-Jul PRD Azri
10-Jul Eng Takanishi
study 10-Jul Eng Vincent
OK 10-Jul Eng Zazli
in progress 10-Jul Eng Zazli
OK 10-Jul Eng Zazli
in progress 16-Jul PRD/Eng Razak
OK 12-Jul PRD/Eng WatieOK 16-Jul Eng/PRD Watie
ok 12-Jul PRD Ibrahim
ok 16-Jul PRD Watie
ok 16-Jul PRD Watie
ok 12-Jul PRD Watie
ok 16-Jul PRD Watie
ok 16-Jul PRD Watie
in progress 17-Jul PRD Razak
in progress 17-Jul PRD Razak
in progress 12-Jul PRD Azriin progress 16-Jul PRD / Eng Azri
OK 16-Jul PRD Azri
-
8/13/2019 JH tan
4/26
ok 18-Jul PRD Azri
ok 18-Jul PRD Azri
ok 16-Jul PRD Azri
ok 16-Jul PC PS Khoo
ok 16-Jul MATC HH Lee
in progress IQC CC Lim
ok 16-Jul PRD Azri
ok Eng
PRD
ok 2-Jul IQC Vincent adjust molding parameter
ok 10-Jul Eng Teo
ok 10-Jul Eng Zazli
Ng 10-Jul Eng Takanishitest run 10-Jul Auto Govin 30% PCB will test run add glue process
oreitation up 10-Jul Eng Vincent
PRD/QC
-
8/13/2019 JH tan
5/26
No Process Skill process PIC Status1 MI Touch up
Hand insert block check before dipping
Visual check inspector
2 Assy IC programming
Battery A
Attach label
Packing
Critical to Quality Skill Process
-
8/13/2019 JH tan
6/26
Remark
-
8/13/2019 JH tan
7/26
Model :TCJ3400 2Q Status
Panel Qty Cav/panel Total Qty
1 Auto TCJ3400 29 6 174
2 MI TCJ3400 29 6 174
3 Assy TCJ3400 150
No Location Defect Qty
1 No Solder 18
2 solder short 483 Pin hole 0
Total 66
No OCATIO DEFFECT QTY
1 LED High up 1
2 LED Reverse 2
3 C37 Solder Short 1
4 R25 Shifted 1
5 U4 Solder Short 66 C8 High up 1
7 C8 One leg No insert 1
8 JP1 Missing 1
14
8%
No OCATIO DEFFECT QTY
1 Case Rubbing Noise 145
2
RemarkProcess
Dipping PPM
Model / VersionTCJ3400
No
MI ICT Defect Data
Total
LDR
Assy Defect Data
-
8/13/2019 JH tan
8/26
3
4
5
6
7
8
145
85%
Total
LDR
-
8/13/2019 JH tan
9/26
No LOCATION DEFFECT QTY No LOCATION DEFFECT QTY
1 LED High up 1 1 C37 Slanting 12
2 LED Reverse 2 2 D3 High up 4
3 C37 Solder Short 1 3 D20 High up 5
4 R25 Shifted 1 4 LED High up 5
5 U4 Solder Short 6 5 D20 Slanting 4
6 C8 High up 1 6 SA1 High up 1
7 C8 One leg No insert 1 7 C8 Long lead 7
8 JP1 Missing 1
14 388% 22%
No LOCATION DEFFECT QTY
1 LED High up 1 High up 17
6 C8 High up 1 Slanting 16
2 D3 High up 4 Solder Shor 73 D20 High up 5 Long lead 7
4 LED High up 5 Reverse 2
6 SA1 High up 1 Shifted 1
7 C8 Long lead 7 7 Missing 1
8 JP1 Missing 1 1 One leg No 1
7 C8 One leg No insert 1 1
2 LED Reverse 2 2
4 R25 Shifted 1 1
1 C37 Slanting 12
5 D20 Slanting 4
3 C37 Solder Short 1
5 U4 Solder Short 6
MI Block Check Defect Data
TotalLDR
Total MI Defect Data
17
16
7
MI ICT Defect Data
TotalLDR
High up33%
Slanting31%
SolderShort13%
Long lead13%
Reverse4%
Shifted2% Missing
2%
One legNo insert
2%
-
8/13/2019 JH tan
10/26
LOCATION DEFFECT QTY
C37 Slanting 12
C8 Long lead 7
U4 Solder Short 6
D20 High up 5LED High up 5
D3 High up 4
D20 Slanting 4
LED Reverse 2
LED High up 1
C8 High up 1
SA1 High up 1
JP1 Missing 1
C8 One leg No insert 1
R25 Shifted 1
C37 Solder Short 1
-
8/13/2019 JH tan
11/26
No LOCATION DEFFECT QTY No LOCATION DEFFECT QTY Repair
1 Case Rubbing Noise 145 1 LED slanting 35 10
2 2 C8 long lead 9
3 3 C8 high up 1
4 4 C1 high up 4 3
5 5 C37 slanting 2
6 6 LED high up 1
7 7 N pin hole 1
8 8 C2 high up 2
145 5585% 32%
No LOCATION DEFFECT QTY
1 LED slanting 35 Slanting 37
6 C37 slanting 2 Long lead 9
2 N pin hole 1 1 High up 83 C8 long lead 9 9 pin hole 1
4 C8 high up 1
6 C1 high up 4
7 LED high up 1
8 C2 high up 2
7
2
4
1
5
3
5
Assy Visual Check Defect Data
TotalLDR
Total MI Defect Data
Assy Defect Data
TotalLDR
37
8
Slanting67%
Longlead16%
High up15%
pin hole2%
0%0%
0%
0%
-
8/13/2019 JH tan
12/26
LOCATION DEFFECT QTY
LED slanting 35
C8 long lead 9
C1 high up 4
C37 slanting 2C2 high up 2
N pin hole 1
C8 high up 1
LED high up 1
-
8/13/2019 JH tan
13/26
Model :TCJ3400 Dipping PPM
No Indicator Defect Qty
1 No Solder 182 solder short 48
3 Pin hole 0
propose to add gluepropose to add gas hole
-
8/13/2019 JH tan
14/26
-
8/13/2019 JH tan
15/26
-
8/13/2019 JH tan
16/26
-
8/13/2019 JH tan
17/26
x % = %
x
SEC
Daily Ouput (9.00hrs): pcs. *if 95% yield: pcs
Hourly Output: pcs Hourly Output: pcs
NO.
1 2 3 4 5 7 8 9 1011121314151617181920212223242526
REV : 0
13
6
11
Appearancecheck
VisualInspectionPCBA
Milan
Fatin
Vijaya
Mimi
Borj
Arsi
Atikah
ThinThin
Suriani
JOB
DESCRIPTION
Breaking
EMP.
NAME
Yahya PREPAREDAPPROVED
92.3
CHECKED
MAX TIME x NO. OF OPRS
CYCLE TIME AVERAGE
52.3
17
10
13
27.06.2013
100BALANCING EFFICIENCY = 204
39 10ASSY 10170 190.59
9 21
TCJ3400
TACT
TIME
CYCLE
TIME
(SEC)
ENGINEERING PROCESS VS TIME STUDYLINE BALANCING/PROCESS STANDARD TIME/DAILY OUTPUT
LINE O/P TARGET CYCLE TIME DATEMODEL TOTAL PROCESS TIMEHEADCOUNT
Labelatta
ch
ICProgram
&Powerware(Tester:13.12
Combinecases&Screwing.
19
Knocktest&Hipot(Tester:5.41s)
BatteryA(
Tester:26.00s)
BatteryB(
Tester:7.38s)
C'binePCB
toL/case&Applygrease
Packing
17
35
39
87.7
767
productivity / pass yield
808
max tact time calculation
Remark
204 ACTION TAKEN
PROCESS:INSERTION ~ PACKING
20.4
0
5
10
15
20
25
30
35
40
1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26
target = 7 sec
output= 1200
-
8/13/2019 JH tan
18/26
KAGA COMPONENTS (M) SDN BHD Model :TCJ3400 Event :PP
Engineering / QA Comment Sheet Customer :Kaga Date :14.5.13
Problem Statement Root Cause Proposal Action PIC / Date
study
Prefer widen U1 location hole follow U1
dimension
propose to add glue in between C37 lead
D20 slanting
productivity loss prework IC ( bend IC lead )
U2 solder short
U1 need to do prework IC lead bending by jig
propose to add gas hole
propose to add glue in between U2 lead
U3 solder short
C37 solder short
1 A B C
2 A B C
3 A B C
A B C
A B C
4 A B C
A B C5 A B C
A B CA B C5 A B C
A B CA B C6 A B C
Widen the U1 PCBinsertion position hole
A B C4 A B CA B CA B C5 A B C
-
8/13/2019 JH tan
19/26
Model Sec PRD Event Qty 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29
TCJ3400 TAS MI N 69000 1.2 1.8 2.4 2.4 3.6 4.8 6 6 7.2 9 9 9
TCJ3400 TAS ASSY N 69000 1.2 1.8 1.8 3.6 4.2 4.8 5.4 6.6 7.8 7.8 9
Output W/H ( S ) Cycle time 10% loss
1200 32400 27 24.3
1800 32400 18 16.2
2400 32400 13.5 12.15
3000 32400 10.8 9.72
3600 32400 9 8.1
4000 32400 8.1 7.29
New & Critical Model event on Line
-
8/13/2019 JH tan
20/26
30 31
6.6
9 6
-
8/13/2019 JH tan
21/26
x % = %
x
SEC
Daily Ouput (9.00hrs): pcs. *if 95% yield: pcs
Hourly Output: pcs Hourly Output: pcs
NO.
1 2 3 4 5 6 7 8 9 101112131415161718192021222324252626
REV : 0
124
Visualinspection
26.41
CHECKED
6.65
CYCLE TIME AVERAGE
ACTION TAKEN
PROCESS:INSERTION ~ PACKING
Syikin
113.11
3
Maria
3
InsertT1
ICT(Tester=2.42s)
Rabiul
4 5.7
298
InsertSA
1
InsertU1
3
InsertC1
4
ENGINEERING PROCESS VS TIME STUDY
LINE BALANCING/PROCESS STANDARD TIME/DAILY OUTPUTLINE O/P TARGET CYCLE TIMEMODEL TOTAL PROCESS TIMEHEADCOUNT
InsertL1
InsertU2
4 4 3
InsertC2
433 3
TCJ3400
TACT
TIME
CYCLE
TIME
(SEC)
PCBA
DATE
17170
100BALANCING EFFICIENCY = 113.11
29 17190.59
PREPARED
productivity / pass yieldmax tact time calculation
1086 1032
TouchUp
MAX TIME x NO. OF OPRS
22.9
Remark
26.06.2013
InsertC8
APPROVED
Norlina
Surtina
InsertD2
0
Shima
Lina
Vijaya
118
JOB
DESCR
IPTION
InsertAC
Contact
EMP.
NAME
InsertF1
Firna
Suhaida
Tina
Zaida
Bhakta
NweHtay
Siti
Suri
3
InsertCN
1
Pre-inspe
ctionbeforedipping
InsertC3
7
Zaiton
0
5
10
15
20
25
30
35
40
1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26
target = 7 sec
-
8/13/2019 JH tan
22/26
MODEL: TCJ3400 JUMP LIST
STEP PARTS NAME LO ACT UN STD UN MEAS UN RO,CO UN MD -R H-LIM UN L-LIM UN HPIN LPIN JFHPA COMMENTS
6 U1 5-6 C2 10 o 10 o 14 0 10 % -10 % 50 0 10000 NO TEST POINT
7 U1 6-7 C2 10 o 10 o 14 0 10 % -10 % 0 51 10000 NO TEST POINT
8 U1 7-8 C2 10 o 10 o 14 0 10 % -10 % 51 51 10000 SAME POINT75 C5*/ C2 22 pF 22 pF 7 0 20 % -20 % 51 50 10000 //C2
88 C28*/ C1 100 nF 100 nF 7 0 20 % -20 % 42 43 10000 //C37
89 C29*/ C1 100 nF 100 nF 7 0 20 % -20 % 9 42 10000 //C40/C41/U3/U4
100 C40*/ C1 100 nF 100 nF 7 0 20 % -20 % 42 10 10000 /C29/C41/U3/U4
101 C41*/ C1 100 nF 100 nF 7 0 20 % -20 % 42 10 10000 /C29/C40/U3/U4
138 U1 G-6 C2 1 V 0.75 V 10 -4 20 % -20 % 51 0 10000 NO TEST POINT
139 U1 G-7 C2 1 V 0.75 V 10 -4 20 % -20 % 51 51 10000 SAME POINT
140 U1 G-8 C2 1 V 0.75 V 10 -4 20 % -20 % 51 51 10000 SAME POINT
144 U3* G-2 C1 1 V 0.75 V 10 -4 20 % -20 % 42 42 10000 SAME POINT
154 U4* G-9 C1 1 V 0.75 V 10 -4 20 % -20 % 42 42 10000 SAME POINT
-
8/13/2019 JH tan
23/26
Model No : TCJ3400
QTY QTY QTY TEST
No. COMPONENT AT PCB TESTED JUMPED %
1 RESISTOR 33 33 0 100
2 CAPACITOR 29 24 5 83
3 INDUCTOR /TRANSFORMER 2 2 0 100
4 DIODE /ZD/LED 7 7 0 100
5 TRANSISTOR 3 3 0 100
6 IC 3 3 0 100
7 JUMPER 5 5 0 100
8 FUSE 1 1 0 100
9 PHOTO COUPLER 1 1 0 100
10 VARISTOR 1 1 0 100
11
OVERALL 85 80 5 94%
-
8/13/2019 JH tan
24/26
No Process Items Need Prepare When PIC
1 MI U1 Ic need bending process
2 MI ICT L1 need to check value 10-Jul Badri
3 MI Power transformer packing prefer over turn , easy pick up 10-Jul CC Lim
4 MI auto punch LED request extend lead length
5 MI C8 request purchase standard part Teo
6 MI D20 prework jig need review ( process & Qty ) 10-Jul Takanishi
7 Assy IC writer cycle time high = 19 ~ 22s need 3 units 10-Jul Takanishi
8 Assy Case screwing process need top cover jig 10-Jul Vincent
9 Assy carton packing slot too tight , difficult to take out from slot 10-Jul Vincent
10 Assy Need battery discharge jig 10-Jul Zazli
11 Assy Screwing process request sensor to prevent screw missing 10-Jul Zazli
12 Assy Hot melt jig & cycle time ?? 8s after 3 week Zazli
13 Assy Casing rubbing sound 2-Jul Vincent
14 Assy Need to prepare difference table AC blade / manual . 10-Jul Teo
15 Assy Battery A check cycle time high 35 ~ 39S need 4 units 10-Jul Zazli
16 Assy Battery B check cycle time high 13 ~ 17S 10-Jul Zazli
17 Assy Appearance check cycle time high 39s 10-Jul Azri
18 Assy carton information prefer label type 10-Jul Zazli
19 Assy manual prefer change colour possible mix with TAS9700 10-Jul Takanishi
TCJ3400 PP3 problem facing review
-
8/13/2019 JH tan
25/26
Status Remark
NC Design limitation
Ok
in progress
NC machine limitation
NC Need prework jig & update WI
study
2 unit
study
in progress
OK
in progress
OK support by nation gate
change adjust molding parameter
In progress
OK
study
In progress
study
study
-
8/13/2019 JH tan
26/26
No Location Wrong value Reverse High up Missing One leg Not insert Need prework Cut lead ICT Assy
1 CN1 x x o o o x x
2 C37 o o o o o o o3 C8 o x o o o o o
4 U2 x o o o o x x
5 U1 x x o o o o x
6 C7 o o o o o o o
7 C2 o o o o o o o
8 L1 x x o o o x x
9 C1 o o o o o o o
10 T1 x x o o o x x
11 D20 o o o o o x o
12 F1 o x o o o o o
13 C23 o o o o o o o14 SA1 o x o o o o o
15 L / N plate x x o o o x x
Remark
o
x
* Need clincing jig to prevent high up
* Need prevent PCB warping jig to reduce dipping PPM
possible happen
not possible happen
TCJ3400
C8D20
CN1U2
U1C2L1
C1F1
N
L
C37
T1
Old PCBNew PCB
Old PCB
F1SA1
C7
C23SA1