Chapter 15: Energy and Chemical Change CHEMISTRY Matter and Change.
Girilambone Change Chemistry
Transcript of Girilambone Change Chemistry
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@
Pergamon
Minemls
llngineerng,
Vol
10,No.
5,
pp.
467-481,1997
O 1997Elsevier
cience td
P :
50892-{875(97)00026-5
Printed
n
Great Britain.
All r iglrts reserved
0892-687
5/97
$17.00+0.00
EXPERMNCE IN
OPERATING THE
GIRILAMBONE
COPPER
SX-EW
PLANT IN
CHANGING
CHEMICAL
ENVIRONMENTS
G.M.
MILLER,
D.J. READETT
and P.
HUTCHINSON
CMPS&F Pty Limited,
central Plaza
Two, 66 Eagle
street, Brisbane,
Qld.
4000,
Australia
(Received
3 JuIy 1996;
accepted l0 February
1997)
ABSTRACT
The
copper SX-EW
plant
operated
by the
Girilambone
Copper
Company
(GCC)
has
suffered
a number
of severe
process
upsets mmediately
ollowing
commissioning.
The
organic
reagent was
degraded by the
action of manganese
entrained
from
the leach
solution. The reagent
chemistry was restored
by the
large scale
use of treatment
by
an
activated clay. A
further
problem
was identified
as the reduction
in
SX
performance
by
the
generation
of
silica
gels
in the organic reagent.
A novel
mechanism
has been
proposedfor
the
generation
ofthese
gels.
Application
ofthe mechanism
has
allowed
the
identification of alternate
operating con"ditions
o
prevent
their
formation.
These
altered
conditions
have resulted
in
further
equipment
developments to
treat the
symptoms
generated.
A new
design of loaded
organic coalescer
has removed
the
increased
entrainment of aqueous resulting
from
operation of the
upstream
extraction
stage in
organic continuity. A new
medium has been
developed
or
installation
in the settlers,
to
minimise the total entrainments reporting to the subsequentstages of the SX plant.
Application
of these techniques
has been shown to
be
generally
appropriate
by use
in
other operations suffering
poor
SX
performance.
@
1997 Elsevier
Science Ltd
Keywords
Non-ferrous
metallic ores; electrowinning;
solvent
extraction; mineral
processing
INTRODUCTION
GirilamboneCopper Company
(GCC)
operates
a medium sized
open
pit
mine near Nyngan
in
central New
South Wales, Australia.
The
processplant
at GCC, usesheap eaching
(HL)
followed
by
solvent
extraction
(SX)
and electrowinning
(EW)
to recover copper as LME
grade
'A'
metal
(Figure
1). Leaching
is accomplished
with
dilute
sulphuric acid solutions, which dissolve the copper
and other chemically
amenable
ore constituents.
The
SX
plant
selectively
extracts
the
copper
from
the
pregnant
iquor
solution
(PLS),
and transfers
it into
the
EW electrolyte for
plating
by a DC current
onto stainless steel cathode
plates.
Presented
t MineralsEngineering
96,
Brisbane,Australia,August
26-28, 1996
46 7
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468
G. M. Milrer
rar
The commissioning
of the Heap
Leach-SX-EW plant
was
followed
by a
carastrophic
collapse
in
the
operation of the SX
section. The
phase
disengagement
imes increased
and
the
settlers
filled
with
stable
emulsion. The extraction
kinetics
decreased
and
the reagent
capacity
decreased;
resulting
in
a major
limitation
on the copper transfer
to the EW
plant.
On-site investigation
of the
cause
of the
situation
determined
that it was due to
the
presence
of manganese
n the
EW
electrolyte.
The
mechanisms
or
the
transfer to EW,
the method of it's
effects in the
SX and
the remediation
were
subject
to
intense
study
I
l].
The manganese
effects were eliminated
by the application
of a rehabilitarion
process
for
the
SX organic
[2]
and measures o prevent the oxidation of the manganese
o
permanganate
n
the EW.
Removal
of the manganese
effects and their
consequent
symptoms,
revealed
an underlying
problem
in
the
SX with continued
poor phase
disengagement.
This
was shown
[3]
to
be a silica
induced phenomena,
and
a
phenomenological
mechanismwas
postulated
o
explain he
observed
ield
behaviour
3].
Application
of
the mechanism allowed the
development
of a different
operating
technique n
the
process
plant,
to address
the silica effects, which was
contingentonthe
treatment
of the effects
of
the altered
process
egime
[4].
The results
of the
plant
changes were
unexpectedly
good,
with the
operation
attaining
alt
the
goals
of
production
rate
and
quality
[4,5].
,
CIRCI.IIT DESCRIPTION
The PLS from the heap each s pumped o a conventionallydesignedSX plant (Figure 1), consistingof
two stagesof extraction n series
E-1
and E-2), followed
by a
single stripping
stage
S-1).
The loaded
r)t5
]AMESON
t OLUIlN
srR0N6
ILTTTROIYTT
S
RONI
ELET IROLYI I
TANK
FARI4
TIRtUtI IN6
E E T
ROLYIE
SPENT
ELI(TROLTI
EW
PLANI
Fig.l
SX-EWPlant
Simplified
lowsheet
li l _4qu q _
I
l
I
I
| | r\*
I
r-\-i
5 l
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The
Girilambone
opper
X-EW
planr
organic
from
El is stored n two
tanksconnected
n
series
o assist n
the
de-entrainment
f
aqueous.
From
here it is
pumped
to the strip
stage or removal
of the
copper nto
the EW
electrolyte.
Removal of the
entrainedorganic
in the strong
electrolyte
s achieved
with
a Jameson
lotation
column
followed by 30 minute retention
n
a surge ank;
and finally
in the
scavenger
EW
cells
where
the
final
traces
of organic are recovered
by the rising
oxygen
bubbles from
the
anode.
The
Jameson
lotation
cell
is the
second o be used n the recovery
of
organic from
electrolyte.
Copper
production
is
by electrowinning
on to
permanent
stainless
steel
blanks
at current
densities
up to
280
A/m2. The
growth
cycle is 7
days; with
final carhode
weight
of around
50 kg.
Typical PLS contains: 4
glL
of Cu,
3 to 6
glL
of Fe
(with
1
g/L
of ferric),
400
ppm
SiO2, 2
g/L
Al,
50
ppm
solids, 120
ppm
Mn and
a
pH
of 1.8.
MANGANESE
EFFECTS
ON SX
OPERATION
Development
of Manganese Problems
at
GCC
The developmentof the manganese roblem at GCC occurredquickiy. By the time the siruation was
recognised
a catastrophicoperationhad
developed
which entailed:
.
Loss of reagentkinetics
and capacity with
extreme raffinate
copper concentrations.
.
Stable emulsion filling
the extraction
stagesettlers.
.
Long
phase
break times in
both the field
and laboratory
ests.
r
10,000
to 15,000
ppm
entrainments
f both
phases
eaving
all settlers.
o
Minimal recovery
of organicby the flotation
column from
the
electrolyte,
with a layer
of
organic
forming on
the scavengerEW
cells.
.
High
organic loss to raffinate.
.
High loss
of electrolyteentrained
n the organic
lowing from
the strip
stage
o the E2
srage n
SX.
.
Extremely
poor product
quality
from the EW
scavenger
ells, and
deteriorating
quality
in the rest
of the EW
plant.
o MnO2 precipitatingon all EW surfaces.
.
Sticky cathodesand nodular growth
of the EW
product.
.
Purple colouration
of the electrolyte and formation
of CuCl2 on
the electrode
hanger
bars.
Thesesymptomswere interacting
and deteriorating
hourly.
Once he
situationhad
stabilised
he SX
plant
throughputwas constrained,
by the
high
entrainments,
o 60
percent
of design
capacity;
while
the
product
quality
from the EW
was acceptable rom
the commercial
cells but
of inferior
quality
from
the
scavenger
cells due to
'organic
burn'.
Mechanism of the Manganese
Problems
The
effects
of manganese
n
the
operation of the
copper SX
process
has only
been recently published.
Miller [ 1] hasdiscussedhe available iteratureand operational xperiences. o date ive copperSX plants
have reported adverse
effects rommanganese ntheirprocess
liquors. The
mechanism
of theproblem
is
reasonablystraight orward, but the consequent
ffects are
generally
multiple; with
complex
interactions
giving
further symptoms of
poor plant performance.
Manganous on
(Mn2+)
itself has no
effect on the operation
of the SX
plant.
It is
however ransferred
nto
the
EW electrolyteby the aqueous ntrainment
of the
pregnant
iquor
solution
PLS)
n the oaded
organic.
The highly
oxidising environment n the EW
cells can alter the
oxidation state
o Mn4+ or
Mn7+ Any
Mna+
produced
will
precipitate
as MnO2 in the
cells. If there is
sufficient iron
(Fe)
present
in
the
electrolyte his will
provide
a
pathway
or the higher
oxidation state
permanganate
Mn7+)
to be reduced
by
the
oxidationof Fe2+ to Fe3+.
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470
Mnl+
- .
5Fe2+
:
5Fe3+
* Mn2+
G. M. Mi l ler
et a/
( l )
The
stoichiometric atio
s 5:1 Fe:Mn
or
5.1:l mass
atio orthis
reaction.
oprovide
a sufficient
hemical
equilibrium driving
force to
maintain
most of
the manganese
n
the Mn2+
state,a
10:
mass atio
has
been
found
to be required
1].
However
during
the early
commissioning
of copper
SX-EW
plants
here
s a low
concentration
of Fe in the
electrolyte.This
allows
any manganese
n electrolyte
o
be oxidised
and o
cause
consequent
roblems.
The normal chemical potential
n
the EW
cells'electrolyte
(Eh)
is about
400
mV.
Under
conditions
of
manganeseoxidation
this can rise
to 900 mV
[].
Under
such conditions
the range
of, and rate
of
deleterious eactionscan
increase
o an extent
that causes roblems
with
the reaction products
Il]
eg:
o
The
SX reagent s oxidised
and the
reaction
products
accumulate
n
the organic phase.
r
Chloride in the
electrolyte
will be reduced
o
Cl
2
and released
t a
greater
ate
than
previously.
r
Increased
corrosion of
the
plant
stainlesssteel
components
can
occur leading
to mechanical
failures.
Consequent Effects
of Manganese
Problems
Figure 2 shows,diagrammatically, hecascading ffectsof manganesence t reachesheelectrolyte.There
are a large number
of complex interactions
and
symbiotic
effects between
the
various
primary
and
secondary ymptoms.The
positive
eedback oops
hat also
exist ead o
catastrophic
ollapse
of the
process
integrity and
plant
operation. The
primary
effects, of
the high oxidation potential
of
the Mn7+
formed
in
the
electrolyte, are
related
to the oxidation
of the
SX organic reagent
].
This
gives
reaction products
which themselveshave the followins
effects:
r
Reduce
he chemical reaction
kinetics
of the extractant.
o
Reduce
he
reagent
capacity
o chelatewith
copper.
e
Create
polar
reactionproducts
which
reduce he
interfacial
ensioncharacteristics
f the
organic
phase
approximately 1000
ppm
ofdegradationproducts
s
all that s required
o alter
the surface
characteristics
ramatically, Miller[1]).
Production of MnO2
precipitates
which form
crud
Direct attack
on the EW lead anodes,
changing
voluminousPbO or Pb(OH)2
1].
Most
of these have further secondary
effects or interact
with
each other
to
give
accelerated process
collapse, as shown in Figure 2.
RESOLUTION
OF THE
MANGANESE
EFFECTS
The rehabilitation
programme
was aimed at reducing
and maintaining
the electrolyte
Eh at
around 400
mV,
maintaining
the
manganese
n the Mn2+ state, and removing
the
degradation
products
from the
SX organic
( to enable better phaseseparationand entrainmentcontrol). The initial reduction of Eh was attemptedwith
the addition of
ferrous
sulphate o the electrolyte. The
reduction was slow
and was supplemented
with
the
addition of SO2, by bubbling
into
one of the electrolyte anks
[1].
This was successful
n
obtaining an Eh
of 400 to
450
mV; and the
presence
of the iron at concentrations
above 1
g/l
was
sufficient
to maintain the
lowered Eh and the
mansanese n
the Mn2+ state.
The
rehabilitation
of
the
organic
was
achievedusing a treatmentwith
acid activatedclay.
This technique
was
developed
by Manison
[2],
in the mid 1980's. The
procedure
was implemented
on the
plant
organic
on a batch basis. Cycle times
for
the treatmentwere around 24 hours, for
a batch equivalent
o l07o
of
the circuit inventory. This
proved
to be inadequate
s he initial benefit rom
the treatedbatch
dissipated
within 12 hours. The extended reatment
imes were due to
the slow settlingof the clay from the
organic.
in the SX.
the
oxide
protection
layer
from PbO2
to a
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47 1
he Girilambone opper
X-EW
plant
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47 2
G. M. Mi l ler et al
The cycle times were reduced to 1 to 2 hours
by installing
a
plate
and frame
filter
to remove
the clay,
before
returning the
treated organic to the
circuit. The
benefit
of this treatment
was
obvious,
as the
plant
organic
retumed toward
the original extraction
capacity
and kinetics.
The
phase
break times
improved
but
did not
return
to the
previous
levels, as
expected. The
recovery
of organic
in the
flotation
columns
also
did not improve as expected; and the
problems
associated
with
organic
burn in the
EW
plant
were
not
mitigated. In all, the organic nventory was
treatedabout
5 times o recover
he chemical
characteristics.
SILICA EFFECTS
ON SX OPERATION
Plant Responses and Field Observations.
Further investigationof the SX circuit
characteristics
howed hat there
was a high
level
of silica in
the
organic
phase.
This led to the identification
of silica as a
potential
major
contributor
to the
problems
of
poor phase
disengagement, igh levels of entrainment
and
poor
organic recovery
n the
flotation
columns.
Silica has been recognised or some ime as having
adverse ffects
onthe operation
of
SX
plants
[3-5].
It
has an inverse
pH
solubility characteristic, which indicates
hat any
carry over from
the extraction
section
to the strip stage,can form silica
precipitates
n the
strip operation. This
was the
case n the field,
where
the
strip
settlerwas full of crud, the organicentrained n
the electrolyte
o the flotation
columns
contained
up to 50 percent crud, and the stripped organic was carrying a high load of light, fluffy crud. The
performance
of
the Jameson lotation column is
shown in Figure
3.
The
theoretical
performance
curve for
the column has been developedby
Readett
5].
It is based
on a constant 10
ppm
entrainment
of organic
in the column
tails.
100 . 0
90.0
80.0
70.0
i
60.0
o
8
so.o
o
E
;e
4o.o
10.0
20.0
30.0 40.0
50.0
60.0
70.0
80.0
9o.o
.too.o
FreeOrganicn Feed
Fig.3 JamesonCell Organic recovery
-
prior
to Modifications
Several
plant
observations
gave
the first indication of the true cause of the
problem.
It
was noted that:
l.
2 .
a
J .
^
5 -
When E-l
was
run aqueouscontinuous
(as
it had
been since
plant
start
up) significant
quantities
of
non compacting crud were being
generated
hroughout the organic
phase.
Significant build up of crud was occurring
in
the strip stage.
Organic
recovered from
the
Jamesoncell contained significant
quantities
of
'gelatinous'
crud.
There was a
gelatinous
film adhering o sectionsof the Jameson ell and scavengerelectrowinning
cells.
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The
Girilambone opper
X-EW
plant
A sample of the
gelatinous
material
was assayed
nd returned
a
SiO2 content
of
>
50% on
a dry
basis.
This was
believed to be indicative of the
presence
of
a colloidal
silica
(SiO2)
gel.
Further investigationhighlighted
that the silica level
in PLS had passed
he maximum
level
of 400
ppm
recommended n
the designcriteria, and
in
general,
silica levels n
all areas
of the
plant
were
excessive.
A summary of silica data is shown n
Table 1.
TABLE I
Silica Distribution Through
the
GCC SX Plant.
El aqueous
E2 aqueous
Stripped Organic
Jameson
colurnn orsanic
500
450-5 0
450
5,800
The solubility of silica, at the PLS
pH
of 2.0, is
around450
ppm;
while at the 180
g/l
in
the electrolyre,
is much ess.The extractionsystem
was
apparently
t silica saturation evels,
which implies
that
he oaded
organic
is
also
in
a similar state.
Site observationof the responses f various
plant
streams
o coalescing
f the entrainments,
howed
some
interesting
phenomena.
Coalescing
of aqueous rom organic, from
both aqueous
and organic
continuos
operation, was readily accomplished without
problems.
However
irrigation
of the organic from
an aqueous
continuousoperation,
prior
to coalescing locked he
coalescingmedia with
gels.
Irrigation
of the organic
from
an organic continuous operation caused no
problems
with
media blockage.
Development
of
an Empirical Mechanism
of Silica Effects
An
empirical
mechanism of the operation
at the GCC SX
plant
has
been developed
[3].
This
postulates
he
carry over of
silica from E-l to the strip
circuit by three routes:
o
Direct entrainment of PLS silica via
entrainment of aqueous n
the loaded organic.
.
Physio-chemicalattachment
of silica to the
polar
molecules
present
n the
organic
phase.
r
Indirect entrainment of silica via PLS
tied up as fluffu crud in
the loaded orsanic.
Once in the strip stage he silica
precipitates due
to
low
solubility at 180
g/l
acid) and forms
gels
and
solids.
These
gels
and solids subsequently absorb organic, form
crud and carry through
in the electrolyte
as
entrainment.
The solids tend to form compacting crud, while the
gels
form non-compacting,
non-settling
emulsions.
Both forms have been observed n the strip stage; with
significant
quantities
of compact crud
present
in the settler; and large
quantities
of
'fluffy'
solids evident in the electrolyte
entrainment.
The
postulated
mechanism allows an understanding of the
processes
nvolved in
the
poor
operating
characteristics
of the Jameson organic
removal
column.
These
were:
The high
proportion
f
non
settlable olids
n
the organic ntrainment
up
o +50%
of the otal
organic olume.)
Poor organic esponseo
flotation
due o the
presence
f
non-settlable
olids.
Reasonably
igh levels of organic
entrainment
n
electrolyte.
Poor hydrophobicityof
the
organicdue o the arge
proportion
of solids.
a
a
a
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47 4
G. M. Miller
er al
The
ultimate aim of
the
process
nvestigation
and
development
was
to minimise
and
control
the
amount
of
organic appearing in the
scavenger
cells. The
first
step
to achieve
this
was
to improve
the
performance
of
the Jameson
column by improving
the
characteristics
f the
organic
being
fed
to it.
Throughout
the industry
E-l is
generally
run aqueous
continuous
to minimise
entrainment
of
aqueous
n
the loaded
organic. Some
operations,
however,
have
reported
the
benefits
of operating
E-l
organic
continuous, o control silica crud affectseg Olympic Dam and Chuquicamata 3]. Both of theseoperations
however
have been retrofitted
with a scrub
stage
o remove
the subsequent
igh
levels
ofaqueous
entrained
in
the organic.
The use
of
coalescers
n SX
circuits is
quite
common
in the
chemical
industry;
and
has
been recommended
for
use n mineral
processing
ircuits.
Olympic Dam
was
originally
supplied
with
a
combined
coalescer-
settler on copper SX raffinate,
before it
was fed
to the uranium
SX
circuit.
Certain patent
applications
by
Codelco, Chuquicamata
division exist
for coalescer
designs
and
media for
copper
SX
circuits.
On site
pilot
testwork
demonstrated
he viability
of
a coalescing
step
on the loaded
organic.
This
was
extended to a full
scale test
programme
to determine potential
performance
of
a coalescer
made
by
conversion of one of the loaded
organic
tanks.
The
physical
form of
the aqueous entrained
in
the organic
is changed
between
operation
in aqueous
continuity and
organic continuity. In
aqueous
continuity the
aqueous
s in the
form
of fine,
'bubble'
films
surrounding a core of
organic, within the
organic continuum.
This
is not readily
observable
n the
field due
to the opaque
organic. However,
a similar
phenomenon
can be observed
with
organic
films
surrounding
an aqueouscore in an aqueous
continuum,
arising from
an organic
continuous
operation.
These
fish
eyes'
are often seen n the raffinate
from E-2.
When
normal aqueous
haze'
coalesces rom the
organic,
two droplets
come together
o form
a larger
drop.
The larger drop volume has
a correspondingly
lower
surface
area. As
such some
concentration
of
interfacely
adhered species will
occur at the new
surface
until such
time as they
have
an opportunity
to
diffuse into the bulk mass
and return to
the
previous
average evels.
Typically the finest aqueoushaze is of the order of 10 micron radius. When two such drops coalescethe
actual surfacearea
of the two smaller
drops s l:l .26that
of
the larger
drop. Even
after
ten drops have
coalesced he surfacearea
eduction s
only l:2.15.
This coalescence rocess
s relatively
slow and multiple
contacts
can take many minutes
(with
7r to t hour required
for
significant
reduction
of entrainment
levels).
This
slow reduction in total
surface area allows
time for de-attachment
and diffusion
of
speciesaway
from
the interface into the
bulk of the drop.
Typical
aqueous
fish
eyes' are
of
the
order of I
to 2 mm diameter
with
a film
(skin)
thickness
of
approximately
0.01
microns.
When these ilms
collapse
eg
by contact
with air,
solids
or larger aqueous
drops) hey will form a single
solid'
droplet
of equivalentvolume
to the volume
of the
skin.
Calculations
contained
in Table
2 show that such a
typical fish eye would
collapse
to a droplet
of 31 micron
diameter;
with
a consequent urfacearea reduction
of 1:1030. This
collapse s
also extremely
rapid;
occurring in
fractions of a second. Thus the collapse of these skins produces extremely high surface concentration
gradients
or
adsorbed pecies;and allows ittle time
for these
gradients
o disperse
nto
the bulk solution.
As a result of these concentration
gradients,
silica
polymerisation
can
occur near
the drop surface
forming
nascent
gels
and
networks
within the aqueous
drop.
Any subsequentcoalescenceof these aqueous
drops can cause urther
gel
structure
growth
as the nascent
gels
are brought together and they become more
ordered.
This is the mechanism by which the
gel
formation
occurs from water
sprayed organic
(operating
aqueous
continuous and
producing
aqueous
fish
eyes'). The spray has
the effect of creating
small diameter
drops
of water
which
burst the
'skins'
on contact.
Only that
part
of the skin in
close
proximity
to the water
drop
combines with it. The rest of the skin
collapsesaway from
the
point
of
penetration,
into a single
drop
(like
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The
Girilambone
opper
X-EWplant
a
pricked
balloon), due
to contraction
from
surface
tension.
The
reason hat coalescence
of these
skins directly
onto a media
substrate
does not
cause
such
gel
formation
is
probably
due o the following
mechanism.
The
skin
contacts
n, collapses
nd wets
he
medium.
As such
there is no immediate
small droplet
formation
and no
significant
reduction
in
surface
area.
Subsequent
collapsesof further
skins allows
a slow buildup
of larger
volumes
on the
surface
of the
media.
The
extra
time allows the interfacial
concentrationgradients
o be lowered
by
diffusion
into
the
bulk
aqueous.
The
combinationof low surfacearea eductionand onger ime for droplet ormationallows he silica
to
diffuse
from
the interface nto
the bulk, and
thus not form gels
during
the coalescing
stage.
An observation hat the
water
sprayed
organic had
higher
aqueous
evels
s easily
explained
by the
extra
water added.The fact that
this extra water
did not
separaten
the oaded
organic
ank(s)
s again
a
function
of the effects of the collapse
of the aqueous
kins.
Someof these
will
have formed
silica
gels
ar
the drop
interface.
These
gels
will have
fully encapsulated
he interior
aqueous
and will
carry
it
through
the
subsequent eparation
stages.
TABLE
2 Calculated
Droplet
Size and Area
Comparisons
l. Aqueous
Haze'
Radius,m
Volume,
m3
Area, m2
Area/Volume,
m2lm3
Equivalent No. of l0 micron
units
Area reduction cf l0
micron
l0 x l0-o
4 . 1 9
1 0 - 1 5
12.56
10-10
3.0x 105
I
I
12.6
10-6
8.38 10-15
1.994
10-e
2.38
l }a
2
r . 2 6
2155
x l0-il
4 . 1 9
l 0 - r a
58.33 10-e
1 3 . 9
1 0 4
l0
2 . 1 5
2. Aoueous
tlsh
Eves'
Radius, m
Film
thickness,m
Volume, m3
Area, m2
Area/Volume
Area reduction
Original
'fish
eye'
10-3
10-8
12.56
x 10-14
12.56 x 10-6
108
I
Equ v al
ent co l ap ed- sohd-'U-rop
31x 10-6
N/ A
12.56
l}-ta
1 . 2 1 5
1 0 - 8
9.67x l}a
r030
RESOLUTION
OF TIM
SILICA EFFECTS
Plant Modifications
The
process
electedor improvement
f the Jamesonell
performance
nvolved:
Modification f theNo 1 oaded rganic
ank o actasa coalescer
o remove
ntrained
queous.
A
plant
shutdownwas arranged
o modify and ill
the tank with the
medium
and hen o restart
with E-l organic ontinuous.
Operation f E-1 n organic ontinuity.
This
aterwas
possible
nly because
n organic ecycle
had
been
ncorporatedn
the original
design).
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476
G. M. Miller
er
al
Operation
of El in Organic
Continuity
With the conversion of
E-l to
organic
continuous
operation,
extremely
significant
changes
occurred
to
the
operating regime
of the SX and
EW
plants.
These
nclude:
a
a
a
a
a
a
a
o
a
Virtual
elimination
of crud
production
n
E-1
(and
subsequently
-2).
Major reduction n crud production n the strip.
Elimination
of fluffy
crud in loaded
organic.
Virtual
elimination
of solids n
organic
entrained
n electrolyte.
Stabilisationof
the
level
of
organic entrained
n
electrolyte.
Jamesoncolumn
operation at
or above ts
theoreticalperformance
curve.
Consistently ow levels
of
organic entrainment
n
the Jameson
ell tails,
less
han
10
ppm.
Increase
n copper
quality
to LME
'A'
from
scavenger
ells
(due
o
the essening
f organic
burn7.
Total elimination
of silica
contained n
loaded
orsanic.
Aqueous entrainment
in E-l
organic outflow
after restart,
was
high
and with
erratic
levels.
Highest
measured evels were
20-25,000 ppm.
When
high
levels were
measured
a distinct
dispersion
band was
evident at the
discharge end of the
settler. Field
observations
ended
o correlate
higher
entrainments
with
deeperdispersionbands. There
was no
buildup of
crud at the interface
n E-l
or evidence
of fluffu
crud
in the organic.
E-l break times rose
to
4Vz
minutes soon
after
the change
and remained
there for
4
days. They
subsequently
ecreasedo the
current evel
of 2 to 3 minutes.
There
hasbeen
some
evidence
of rag
(stable
emulsion
films) in the aqueous
uring the
break; but this
coalesces
nto the
interfaceprior
to completion
of
primary
break. No residual rag
is evident.
Aqueous
solutionsare
clear
with some
'fish
eyes'
present
especially at high
suspended olids oadings.
A significant reduction
in crud
production
has
been observed n
the
strip settler.
Daily
crud removal
has
been reduced o less
han once
oer
month.
The entrainment
of organic in
electrolyte has
not been
significantly
reduced
but the
proportion
of
crud/solids associatedwith the organic has decreased.The percentage f solids was almost zero in the
samplesanalysed.
Jameson Column Performance
The Jameson ell tails
have
becomeconsistently
ower
than 10
ppm.
This compares
o
erratic
and higher
levels
prior
to the changes.These esults
are
consistentwith
the Jameson
ell
operating
model
[5];
which
concludes that the
cell
produces
a 10
ppm
tail
(from
suitable feed)
independent
of
the
feed
concentration.
This has
been successfullydemonstrated,
ince
the changes,
with feed
levels
up to
37
ppm.
The
feed
concentration vs recovery
curve is
plotted
in Figure
4. As
is evident
the field
performance
is at
or better
than the theoretical
performance
line
since the circuit
changes.
The organic recovered from
the Jamesoncell still
shows
poor
disengagement
haracteristics
rom
the crud
formed during the recovery process.
As such it is
directed to
the crud tank
for treatment
prior
to its
reintroduction
o the circuit.
Scavenger Cell Operation
With the consistently low levels
of organic in
strong electrolyte,
the skimming
of
organic from
the
scavenger cells
became
viable.
Each cell was fitted
with feed and
discharge
skimmers.
Product
quality
improved dramatically in
both
physical
appearance
and chemical
quality.
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The Girilambone
opper
X-EW
plant
E
t00.0
90.0
80.0
70.0
60.0
50.o
40.0
30.0
20.0
10.0
tr
u o
EI
t o t
E E g
Eo
a
E
E
E
E
E
Eg
f
-
o
o
cr
t; A"t""t I
[=f "":"$11
o.o
].-
o-
0.0 10.0 30.0 40.0 50.0 60.0 70.0
80.0 90.0 100.0
FreeOrganic n Feed
Organic Recovery
-
post
Modifications
is.4 Jameson
Cell
Loaded Organic Silica
A seriesof
loaded
and stripped organic sampleswas
taken during to
the E-l flip to
organic continuity.
Figure
5
shows he silic, analysis
of theseorganic samples.As
can be seen he
silica level
dropped rom
487
ppm
in
loaded
organic
prior
to the flip; to zero
two weeks after the flip.
500.0
450.0
400.0
350.0
300.o
250.0
200.0
150.0
100.0
50.0
0. 0
511
1411
2111
SampleOate
--o-
Loaded
Org
--+-
Stripped Org
Fig.5
OrganicSilicaLevels
CL
CL
o
o
o
N
o
a
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478
Other
G. M.
Miller
ral
points
to note
from
this
Figure
are:
A reduction
n
silica
level
between
oaded
and
stripped
organic.
This
shows
he precipitation
of
silica from
loaded
organic
by
the
high
acid
strip
stage.
The
concentration
of
silica in
loaded
organic
is intermediate
betweenpls
and
raffinate
values.
This
indicates he evel of silica s probablyat equilibriumwith the aqueous hase oncentrationswhen
operating
aqueous
ontinuous.
However,
the zero
silica evel,
when
operating
organic
continuous
in E-1
supports
he
postulated
mechanism.
Loaded
Organic
Coalescer
Figure
6 shows the
result for
the
coalescer
for
the first
two
months
of operation.
The
feed
entrainments
were
high with
very
wide fluctuations.
The
unit has
provided
a consistent
output
with
an average
200
ppm
aqueous n
the loaded
organic,
with
a maximum
of 400 ppm.
Backwashing
has
been
required
on
a four
weekly
cycle and has
been ntegrated
with
the maintenance
schedule.
The
high
feed
entrainment
evels
have
resulted
rom
the operation
of the E1
mixer
settler
n organic
continuitv.
at
1111 1311
January
1994
E
3 m E
E
U
20o
E
E
e
o
o
L
ul
i-:""1----:-::"41
Fig.6
Loaded
Organic
Coalescer
Aq
Entrainment
in Feed
and
Discharee
IMPROVED
SETTLER
OPERATION
System Development
The operation
of the
GCC SX
plant
was improved
with the
change
n E1
continuity
to organic
continuous.
However
the level of aqueous
entrainment
in
the loaded
organic
was
of concern
in
case t
'broke
through'
the
coalescer, into
the strip circuit.
Methods
of
reducing
this
entrainment
and
of
the large
fluctuations
in
the
entrainmentwere investigated.
Many
methods
of
entrainment
ontrol
have
been
ried
,
Millert4l.
Al l
have
been
partially
or
generally
successful
n clean
solutions.
However
ndustrial
solutions
equire
sysrems
that
can operate well
with large
quantities
of crud
present
n
the
settlers.
Those
systems
hat
are tolerant
of crud have
had the least
success
with
entrainment
control.
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The Girilambone
opper
X-EW
plant
Coalescing
Requirements
The
primary
effect of
poor
settler
performance
s the
appearance
f a dispersion
band
of
significant
thicknessat the settlerdischarge.This leads o high
andhighly
erratic evels
of entrainments
n
the streams
advancing
from the settlers, which in turn leads
to effects such
as high organic
in raffinate
and
advance
electrolyte, high PLS entrainment n loaded
organic, and high electrolyte
entrainment
n
stripped
organic.
Thesesituations an becomeunstable nd require educed olumetric hroughputso satisfactorilystabilise
the operation.
The requirements
for in-settler
coalescing are different from
stream specific
uses
(such
as the loaded
organic
coalescer). n-settlercoalescingaims
primarily
to stabilise he
entrainment evels
at around
500-
1000
ppm;
which is the normal designcriteria for copper
circuits. The elimination
of
shock oads due to
entrainmentof
the dispersionband s important.
Streamspecificcoalescing
aims to reduce
entrainment
levels to 50-200
ppm
in order to reducecosts
organic
oss)
or
improve
downstream
process
effectiveness
(reduce
organic burn and minimise PLS to electrolyte).
There
s
about
an order of magnitudebetween he
success riteria for the two different
styles
of operation,
which leads o two different
setsof design criteria,
and solutions or the
problems.
The selectionof a
permanent
n-settler
coalescingmedium required
he
following
criteria
to be met:
Cheap,
easy to make, materials
readily
available, have intermediate
sudace tension
(so
that
both
continuities
could be treated successfully), chemically compatible, require
simple
installqtion,
density
greater
than electrolyte to
prevent
floating,
suficient open area to
allow crud to
pass
through unhindered.
One
of the
problems
n medium selection s that testing s not readily
done, except n
the industrial
plant
or a
large
pilot
unit. Even on a large
pilot
unit full hydraulic
similarity is not achievable.
For this reason
a scale
up factor was usedbasedon the streamcoalescer pecific low rate,
1m3lhrlm2
f media surface),
and the target
level
of
entrainment.A 1:4 ratio was
used as the basis.
A
packing
ype
having he following featureswas selected: andom
ype
packing,
available n various
sizes,
made from a commercialplastic andreadily available. The size of the packingwas selected asedon the
size of the openings
available for crud
passage.
This
allowed a
large
size to
be used, which in total
occupied
less
thal
40% o f the settler volume. The
packing
was contained
in coarse mesh
bags,
manufactured rom a solution
esistantmaterial,
o
prevent
heir escape nd
blockageof
pumps
and valves.
Operating
Results
The results
of the in-settler coalescingmedium addition have
been better than expected.
The addition
resulted
n immediate reductions n the entrainments rom all
stages reated.The operation
of the settlers
was more stable. With the levels of entrainment educed, he down stream mixer
was also more
stable,
with far fewer uncontrolled
changesof operatingcontinuity.
The settlers
were able to
perform
successfully nder
quite
adverse onditions.This included
maintenance
of full hydraulic
capacity with both:
r
Lower than design
emperatures
10oC
rather than 20oC).
o
3% higher than design
reagentconcentration.
.
Higher than
design solids n PLS
(up
to 200
ppm
cf
<20
ppm).
Under these
conditions he
settlerselection riteria would have esulted n a unit with
35
%
more area. The
capacity
was confirmed during summer operation
(closer
to nominal design
conditions) when the total
average
entrainment
loss of organic to raffinate was 10
ppm
over a 5 month
period.
This
again
demonstrates
he effectiveness f
the medium.
479
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480
G. M.
Miller
era/
Recent
operation
of
the settlers
after
systempumping
upgrades)
has
shown,
that
under
close
to
design
conditions,
the
settlers
will treat
307o
morc
than
design
lows.
The
limitation
at
GCC
is
not in
the
settler
performance
but in
the
pumping
systems
ervicing
he
SX
plant.
It
is
estimated
hat
the
settler
capacity
s
at least
40% improved
over the
'conventional'
design
criteria.
This
allows
for
easy
upgrading
of
SX
plant
hydraulic
capacities,
without
the need
or more
or enlarged
settler
units.
Installationof the medium in anotheroperation,Miller[ 4], hasalso shown he benefitof this technique.
The
plant
was
operating
under severely
adverse
onditions.
Medium
was
added
o various
parts
of the
SX
settler
systems n
stages.The plant
throughput
was
doubled
from
50%
to 100%
of design
ate
in
a
period
of 4 months.
Figure
7 shows
he
accumulated
ffect
of the
medium
addition
on the
plant
feed
flowrate.
Medium
addition to the
settlers
reduced
he
aqueous
entrainment
n
the loaded
organic
from
+20,000 ppm
to less than
500
ppm.
The results
rom these
operations
how he
benefit
hat
can
be achieved
rom
the installation
ofcoalescing
medium
in the settler.
This
has
been ecognised
or some
considerable
ime;
however
the
development
of
a medium
that is
tolerant
of crud
and other
adverse
operating
conditions,
has now
been
Droven on a
continuous ndustrial
scale over
a
period
of nearlv
3
vears.
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f r om
30, 9 o 21r10when
;
S iO2
sa t u ra l i on
aused
I
t low.at€
o be reduced
nd
]
i
cont inuity
f l ipped
to organic
I
-=\-
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M"d',-'.ddil-l
wash aunder
]
(8,12,s4)
I
---\-
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t
*
150
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\
/ . ' -
i
Med ium
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I
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laund€r
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__'1
__
I
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dded
I
to Et sett ter
j
fl6:11lsa)uo l
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" l_
190994
06.1G94
24-1G94
Fig.7 Plant
Throughput
11-11 . 94
3G11. 94
18. 12 . 94
05. 01 . 95
Oate
Increase
with Settler
Medium
Addition
CONCLUSIONS
The
development f
the understanding
f the
prime
and
consequent
ffects
of manganese
n
SX and EW
operations,has
assistedn
the
improvement
f
performance
f the
GCC
plant.
Now
that
there is
an
operationalmechanism,
hese
effectscan
be avoided
y simple
preventative
measures,
specially
uring
commissioning.
For
those operations
ikely to
have manganese
n
the PLS,
addition
of iron
into
the electrolyte
s
recommended
before
the SX
plant
is charged
with
extractant.
Monitoring
of the EW
Eh will
give
timely
warning
of any
potential
degradation
of the
organic.
8/11/2019 Girilambone Change Chemistry
http://slidepdf.com/reader/full/girilambone-change-chemistry 15/15
The
Girilambone
opper X-EW
lant
481
The understanding
of
the effects
of silica on
the SX
plant,
has
been
advanced by the development of a
phenomenological
mechanism.
Application
of
this hasallowed he
plant
operation
o be altered o minimise
the silica
effects.
Development
of stream
speciflc coalescing
techniques and hardware, to address
the
consequent
ffects
ofthe
changed
operating
conditions,
has advanced he applicability ofthese
methods.
The
selection
of a
medium
for use
in the settlers
has enabled the
hydraulic capacity of the settlers to
be
improvedby between30 and 50 percent.The medium s tolerantof crud, cheapand easy o install. It also
provides a means
of
increasing
plant
capacities
without the
need for more or larger settlers.
The resolution
of the
problems in the
GCC operation
has been
the springboard
for the development of
a
number
of techniques
hat
have advanced
he
knowledge and
operation of the
SX circuit. Implementation
of these
techniques
has
been
found to
be
generally applicable
to other operations, and
are being
incorporated
in a
number of
new
projects.
ACKNOWLEDGMENTS
The
authors
would
like
to thank
the staff
and management
of
the Girilambone Copper
Company
for their
permission o
publish this
paper. The effort to
overcome he
problemswas huge; and
t is a credit
to them
that the
plant
operation
was restored
in such
a short
time. The
views
of the authors do not necessarily
reflect
those
of the
ComPanY.
REFERENCES
Miller,
G.,
The
Problem
of
Manganese
nd ts
Effectson Copper
SX-EW
Operations,
eds W.C.
Cooper
et al.
Copperg|-Cobre9S
649-663,
CIM
Santiago,
1995).
Mattison,
P.L., and
Champion,
W.H.,
Enhancement
f Solvent
Extractionby Clay
Treatment
of
Contaminated
Circuit
Organics,
Hydrometallurgy
Research
Development
and Plant
Practice, Eds.
K.
Ossco-Asarc
and
S. D.
Miller, 617-628,
Proc. AIME,
112 Annual
Meeting,
Atlanta,
(1983).
Readett,
D.J. &
Miller, G.M.,
The Impact
of Silica
on Solvent
Extraction:
Girilambone
Copper
Company,A CaseStudy, edsW.C. Cooperet al. Copper95-Cobre95, CIM, Santiago,679-691
(1ee5).
Miller,
G.M.,
Readet,
D.J.
& Hutchinson,
P., Entrainment
Coalescing
n Copper
SX Circuits
eds
D.C. Shallcross
et
al.. Proc.
ISEC 96,
Univ.
Melbourne,
Melbourne,
795-800
(1996).
Readett,
D.J., Experience
with
Column
Flotation
n
Electrolyte Clean-up
During
Process
Upset
Conditions
eds
D.C. Shallcross
et al.
Proc.
ISEC 96, Univ.
Melbourne,
Melbourne,
819-824
(1996).
l .
3 .
4 .
5 .