Experience with Stress Corrosion Cracking (SCC)

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KINDER MORGAN ENERGY PARTNERS, L.P. Experience with Experience with Stress Corrosion Cracking Stress Corrosion Cracking (SCC) (SCC) Scott Davis – Director of Pipeline Integrity and Facilities Engineering

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Experience with Stress Corrosion Cracking (SCC). Scott Davis – Director of Pipeline Integrity and Facilities Engineering. Outline. KMP Liquids Pipelines July 30, 2003 Failure Repair and Start-up Sequence SCC Investigation Strategy SCC Investigation Status and Results. - PowerPoint PPT Presentation

Transcript of Experience with Stress Corrosion Cracking (SCC)

Page 1: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

Experience with Experience with Stress Corrosion Cracking (SCC)Stress Corrosion Cracking (SCC)

Scott Davis – Director of Pipeline Integrityand Facilities Engineering

Page 2: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

OutlineOutline

KMP Liquids Pipelines

July 30, 2003 Failure

Repair and Start-up Sequence

SCC Investigation Strategy

SCC Investigation Status and Results

Page 3: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

KMEP Liquids PipelinesKMEP Liquids Pipelines

KMCO

2

PACIFIC

PACIFIC

PACIFIC

CALNEV

Mid Con

PLANTATION

CFPL

Products Pipelines

Products Pipeline Terminals

Transmix Facilities

CO2 Pipelines

Terminals

Page 4: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

8” Tucson to Phoenix 8” Tucson to Phoenix

Release

Location

Page 5: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

July 30, 2003 FailureJuly 30, 2003 Failure

Approximately 13:09 line failure

SCADA alarm and Controller shutdown within 3 minutes

Operators dispatched and line isolated

Line excavated and exposed

Page 6: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

Repair and Start-up Repair and Start-up SequenceSequence

Visual examination, suspected seam weld failure

Entire joint replaced by August 1, 2003

Line re-started at 50% of MOP (~34% SMYS)

Page 7: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

Pressure Test ProtocolPressure Test Protocol

Metallurgist identified SCC on August 8, 2003

Line shut down for further testing

Pressure test in 2 sections– “Spike” test of 1 hour at 139% of MOP– 8 hours at 125% of MOP

Testing commenced on August 20, 2003

One test successful

Page 8: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

Pressure Test FailurePressure Test Failure

2nd test unsuccessful– Failed in 1st minute at 139% MOP – 40’ from original failure– Intermittent SCC cluster length 6”

– SCC ranged from 50-86% wt

Page 9: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

Return to OperationReturn to Operation

Bypassed 8” pipe near failure on August 24

Replaced 5400 feet of pipe in the immediate vicinity

Successful pressure test of section 2

Line restarted on September 12, 2003

Currently operating at 50% MOP

Increasing pressure dependant on results of SCC investigation

Page 10: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

High pH SCCHigh pH SCC

Still requires – Environment that is conducive to SCC – Susceptible pipeline material– Tensile stress in the pipeline steel

Differences:– No surface corrosion products– CP is adequately protecting the steel– Higher published stress threshold

Page 11: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

SCC InvestigationSCC InvestigationStrategyStrategy

1. Gather and investigate pipeline data

2. Develop algorithm to predict SCC likelihood

3. Complete case study on removed 5400’

4. Predict terrain conditions conducive to SCC

5. Conduct field geotechnical, CIS, and PCM

6. Select locations for excavations

7. Conduct field excavations

8. Reintegrate excavation findings

Page 12: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

SCC InvestigationSCC InvestigationStatus and ResultsStatus and Results

MPI conducted on 5400’ of removed 8”

SCC found in pressure test failure joint

SCC found in 1 joint approx. 1800’ upstream

Field surveys have been completed

Finalizing excavation locations

Anticipated completion prior to year end

Page 13: Experience with  Stress Corrosion Cracking (SCC)

KINDER MORGANENERGY PARTNERS, L.P.

Contact InformationContact Information

Scott P. DavisDirector – Pipeline Integrity and Facility Engineering

Kinder Morgan Energy Partners1100 Town & Country DriveOrange, California 92868

E-mail: [email protected]