Dam Foundation Treatment
Transcript of Dam Foundation Treatment
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A CASE HISTORY
OF
EXPLORATION &
REMEDIATION
HIGH PRESSURE
SEEPAGE AT ARAPUNI DAM,
NEW ZEALAND
Presented by:
Saravanan. S
(2010CEU3304)
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THE DAM
Arapuni dam is 64 m high curved concrete gravity dam with a
crest length of 94 m.
Arapuni Dam forms Reservoir for 186 MW Power Station
located on Waikato River, 55 km upstream of Hamilton City inNorth Island of New Zealand.
The Dam Construction was started in 1924 and lake filling
was completed in 1928.
The Arapuni Power Station is owned and operated by Mighty
River Power Ltd., a State owned electricity generation
company.
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THE CUT OFF PROVISIONS
Original features of the dam include concrete cutoff walls and a
network of porous (no-fines) concrete drains at the
dam/foundation interface (the “under drain”).
The original cutoff walls extend beneath the dam to a depth of
65m below the dam crest and extend 20m and 33m into the left
and right abutments respectively, for the full height of the dam.
There was no grout curtain constructed during Dam
construction.
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GROUTING AND DRAINAGE PROVISIONS FOR
FOUNDATIONS
Consolidation Grouting - For filling up the joints, cracks,crevices etc. and there by making the foundation homogeneous.
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GROUTING AND DRAINAGE PROVISIONS FOR
FOUNDATIONS
Curtain Grouting - For making a curtain to cutoff/ minimize
seepage
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GROUTING AND DRAINAGE PROVISIONS FOR
FOUNDATIONS
Drainage arrangements - To drain off seepage water and thusreduce uplift. Some rules in this respect are
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THE DAM FOUNDATION
The dam site is in an area of multiple ignimbrite flows from
volcanic eruptions over the last 2 million years.
The main dam footprint is founded on a 40-50m thick sheet of
Ongatiti Ignimbrite a point-welded tuff.
The upper part of the unit is very weak, with unconfinedcompressive strength of between 2 and 6 MPa, while below the
original dam cutoff wall the Ongatiti is considerably stronger
(up to 28MPa) and identified as the “hard zone”.
Beneath the Ongatiti Ignimbrite, about 40m below the base of
the concrete dam, are older ignimbrite deposits, identified as
Pre-Ongatiti for this project.
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THE DAM FOUNDATION (CONTD.)
At interfaces between ignimbrite sheets there tends to be
unwelded material, either airfall tephras or unwelded
ignimbrite.
The most extensive interface deposit is between the
Ahuroa and Ongatiti ignimbrite units, known as the
Powerhouse Sediments with a thickness of 4 to 8m.
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THE DAM FOUNDATION (CONTD.)
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THE CUT OFF PROVISIONS (CONTD.)
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THE CUT OFF PROVISIONS (CONTD.)
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THE SEEPAGE PROBLEM
Following lake filling and in the first 2 years of operation,
there was considerable leakage from the reservoir both from
the dam drains and from springs in the downstream rock.
Flows typically varied between 2200 liters/min and 4200
liters/min.
In May 1929, a large crack opened in the headrace channel
due to that the Lake was lowered. The lake was not refilled
until April 1932 while the headrace was lined.
During this time a single row cement grout curtain was
constructed along the full length of the dam and both
abutment cutoff walls.
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THE GROUT CURTAIN
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THE SEEPAGE PROBLEM (CONTD.)
After refilling the reservoir in 1932, leakage flows had been
reduced to 420 liters/min.
In the period 1932 to 1943, the records indicate that there were
several instances of sudden flow increases and a number of
holes on the right abutment were injected with hot bitumen
grout.
From 1943 to 1950 leakage was typically about 750 liters/min
but this declined to about 75 liters/min by 1950.
Leakage flows of about 75 liters/min were typical through the
period 1950 to 1995.
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THE SEEPAGE PROBLEM (CONTD.)
In 1995 the dam toe area was cleaned up and seepage
monitoring arrangements rejuvenated.
at this time, eight holes were drilled into the dam foundation
to explore seepage conditions.
Two of these holes, referred to as OP05 and OP06,
encountered high water pressures at discrete depths and
each flowed at several hundred liters per minute after drilling.
It is now evident that the various grouting works only filled
voids where the vertical drill holes connected to open voids
in vertical joints, leaving other leakage paths open.
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DETECTION OF HIGH PRESSURE SEEPAGE
Hole OP05 was subsequently used to measure the
pressure in the feature and hole OP06 was used as a
relief well.
With OP06 flow shutoff, the pressure in the feature in
1995 was about RL 97 m, 14 m below reservoir level. With
OP06 flowing at about 380 liters/min, the feature pressure
dropped to RL 87 m.
OP05 and OP06 pressure and flow were included in themonthly dam surveillance monitoring program thereafter.
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INVESTIGATION TO LOCATE THE FEATURE
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GROUTING THE FEATURE
When sharply rising pressures were identified in OP05 in
September 2000, a possible mitigation measure was to attempt
to grout the feature using OP05 and OP06.
There were two main concerns with this concept. First, little
was known about the nature of the flow paths within thefoundation and so the grouting operation and its effectiveness
would be very uncertain.
The high grouting pressures necessary to inject grout through
OP05 and OP06 could blow out the infill and so significantly
increase flow rates.
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GROUTING THE FEATURE (CONTD.)
Grouting took 12.5 hours during which 11.5 cubic meters of
grout was placed.
At the start of grouting, relief well discharge was transferred to
the most upstream well so that grout being injected at the
downstream end was in still water.
After about 2.5 hours, grout was detected at the relief well. The
relief well was closed after 6 hours and a further 4.4 cubic
meters of grout was injected to refusal at 8 bar. Minor
modifications were made to the mix during injection in
response to the field observations.
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VERIFICATION OF GROUT EFFECTIVENESS
The immediate response to grouting was that drainage flows
from the dam drains dropped from a total of 600 to 50 liters/min.
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UPGRADING THE DAM FOUNDATION
The assessment process following fracture grouting in 2001
identified two key issues relating to the fissure systems:
The presence of highly erodible joint infill in the dam
foundation that is vulnerable to piping erosion.
The presence of near-lake pressure in areas under the dam
due to open fractures hydraulically connected to the reservoir.
Mighty River Power committed to upgrading the dam
foundation seepage control measures so that the risk of further piping incidents would become extremely low and high
pressures under the dam would be controlled.
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LONG TERM SOLUTION
A comprehensive investigation took place to determine the
extent of foundation features requiring treatment to prevent
further incidents from developing.
A targeted and cost effective fix involving drilling and
concreting overlapping vertical piles from the dam crest
through the dam and underlying rock formation to a total depth
of 90m was selected to form four separate permanent cutoff
walls at selected locations beneath the dam.
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LONG TERM SOLUTION (CONTD.)
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LONG TERM SOLUTION (CONTD.)
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LONG TERM SOLUTION (CONTD.)
An international Alliance between the dam owner
(assisted by their designer) and a contracting consortium
was formed to identify cut-off options, develop them and
implement the selected methodology.
Construction of the cutoff walls commenced in
September 2005 and was completed in mid 2007.
Operation of the reservoir has not been affected and
electricity generation has continued during the project
works.
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CONCLUSION Arapuni Dam has had a history of foundation seepage incidents
since first filling in 1927.
The most recent leak was sealed in an emergency groutingoperation in 2001.
The dam’s owner, Mighty River Power Ltd, has undertaken a
dam foundation enhancement project to prevent future leakage
incidents from occurring.
The cutoff walls consist of overlapping 400mm diameter holesdrilled through the dam and underlying ignimbrite sheet with a
full reservoir.
The construction technique required for 90m deep cutoff walls
significantly extends international overlapping / secant pile
technology.
Construction was undertaken with close monitoring of the dam
foundation to ensure that the construction activities did not
generate another leak requiring emergency action and to ensure
that the dam’s safety was not compromised.
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THANK YOU