api ENERGIA IGCC Plant StatusPbrkic71/1 DBK 00-10-05 ABB Oil, Gas and Petrochemicals John L. Spence...
Transcript of api ENERGIA IGCC Plant StatusPbrkic71/1 DBK 00-10-05 ABB Oil, Gas and Petrochemicals John L. Spence...
Pbrkic71/1 DBK 00-10-05
ABB Oil, Gas and Petrochemicals
John L. SpenceVice President Operations
ABB Lummus GlobalTechnology DivisionBloomfield, NJ, USA
api ENERGIA IGCC PlantStatus
by
2000 Gasification Technologies ConferenceSan Francisco, USAOctober 8-11, 2000
ABB Oil, Gas and PetrochemicalsPBrkic71/2 DBK 00-10-04
Outline
n Site location
n Project contractual scheme
n Process scheme
n Plant characteristics
n Overall project history
n Present project status
n Remaining activities to PAC
n Commissioning issues
n Lessons learned
ABB Oil, Gas and PetrochemicalsPBrkic71/3 DBK 00-10-04
Site Location
ABB Oil, Gas and PetrochemicalsPBrkic71/4 DBK 00-10-04
api ENERGIAapi ENERGIA
Shareholder and ancillary agreements
25 % Equity51 % Equity
Technologylicense agreements
24 % Equity
Fuel supply agreement
O & M agreement
Steam purchase agreement
Utilities and service supplyEnergy Sales agreement
Turnkey constructionagreement
Non-recourse debt
Completionundertakings
ABBABB
Texaco DevelopmentTexaco DevelopmentCorpCorp
ANONIMA PETROLI ANONIMA PETROLI ITALIANA, SPAITALIANA, SPA
API REFINERYAPI REFINERY
API GROUPAPI GROUP
LENDERSLENDERS69 BANKS69 BANKS
ABB Sadelmi *ABB Sadelmi *ABB Lummus GlobalABB Lummus GlobalABB Power Generation ABB Power Generation **
ENELENEL
Project Contractual Scheme
* Today: Alstom Power
ABB Oil, Gas and PetrochemicalsPBrkic71/5 DBK 00-10-04
TAR
FILTER
CAKE
STEAM TO
REFINERYSTEAM
POWERPOWERPOWER POWERPOWERPOWEROXYGEN
DEMI
WATER
DEMI
WATER
EXHAUST
SULPHUR
STEAM
WASTE
WATER
NITROGEN
STEAM
AIRAIRSEPARATORSEPARATOR
GASIFICA-GASIFICA-TIONTION
GASGASCOOLINGCOOLING
ACID GASACID GASREMOVALREMOVAL
SULPHURSULPHURRECOVERYRECOVERY
SOOTSOOTRECOVERYRECOVERY
GASGASTURBINETURBINE
STEAMSTEAMTURBINETURBINE
HEATHEATRECOVERYRECOVERY
STEAMSTEAMGENERATORGENERATOR
AUXILIARYAUXILIARYBOILERBOILER
HOT
EXHAUST
Process Scheme
ABB Oil, Gas and PetrochemicalsPBrkic71/6 DBK 00-10-04
Syngas Manufacturing Process Plant (SMPP)
n Technology: Texaco, UOP, Parsons, Südchemieand ABB Lummus Global
n Plant size:v 59 t/h of feed
v 130 t/h of syngas
v 127 t/h of Nitrogen
v 62 t/h of Oxygen
v 33 t/h pretreated waste water
v 4 t/h sulfur
ABB Oil, Gas and PetrochemicalsPBrkic71/7 DBK 00-10-04
Combined Cycle Power Plant (CCPP)
n Technology: Alstom PowerDry LowNOx , GT13E2 MBTU
n Plant size:vGas Turbine 190 MW
v Steam Turbine 100 MW
v HRSG 280 t/h
v Auxiliary Boiler 140 t/h
v Export steam to refinery 65 t/h
ABB Oil, Gas and PetrochemicalsPBrkic71/8 DBK 00-10-04
Api IGCC Project History
n 1990 Project idea/potential clients
n 1991 Technology selection, licensor, feasibility study
n 1992 License agreement, consortium agreement
n 1993 Basic engineering, nominated subcontractors, cost estimate,authority permitting
n 1994/95 LSTK proposal, feasibility analysis,development of contracts, financing
n November 1996 Signing of contracts, determination ofcontractual value in LIT
n December 2000 Provisional acceptance
ABB Oil, Gas and PetrochemicalsPBrkic71/9 DBK 00-10-04
Api Energia IGCCView of (right to left) the
cold box, the incinerator
stack, the grey water
treatment unit, the HRSG
and its stack, the sulfur
recovery units (foreground)
and the Selexol towers
ABB Oil, Gas and PetrochemicalsPBrkic71/10 DBK 00-10-04
Api Energia IGCCView of the HRSG
in the direction of
the air separation
compressor building
and the cold box
ABB Oil, Gas and PetrochemicalsPBrkic71/11 DBK 00-10-04
Api Energia IGCCGasifier structure
upper deck
ABB Oil, Gas and PetrochemicalsPBrkic71/12 DBK 00-10-04
Api Energia IGCCView of the naphtha
stripper and carbon
extraction unit
ABB Oil, Gas and PetrochemicalsPBrkic71/13 DBK 00-10-04
Api Energia IGCCView from the gasifier
deck of the acid gas
removal section
ABB Oil, Gas and PetrochemicalsPBrkic71/14 DBK 00-10-04
Api Energia IGCCView of the sulfur recovery
units (center), the sour
water stripping towers (right)
and the Selexol regenerator
and absorber
ABB Oil, Gas and PetrochemicalsPBrkic71/15 DBK 00-10-04
Api Energia IGCCView of the HRSG
showing the DeNOx
ABB Oil, Gas and PetrochemicalsPBrkic71/16 DBK 00-10-04
Api Energia IGCC
View of the GT
building and
air intake
ABB Oil, Gas and PetrochemicalsPBrkic71/17 DBK 00-10-04
Plant Performance Highlights
n Both gasifiers have operated at 100% rate
n All upstream and downstream process areashave run successfully
n Process chemistry working well
n SRU’s have operated on oxygen and acid gasat near design efficiency
n Gas turbine has operated at base load ondiluted syngas
n Emissions from gas turbine are lower thanexpected
ABB Oil, Gas and PetrochemicalsPBrkic71/18 DBK 00-10-04
Remaining Activities to PAC
n Complete gas turbine testing
n Validate the CEMS
n Operate auxiliary boiler on syngas
n Conduct the 96-hour guaranteeperformance test
n Complete the 30-day reliability run
ABB Oil, Gas and PetrochemicalsPBrkic71/19 DBK 00-10-04
Project and Commissioning Issues
n Excessive number of equipment componentfailures
n Gasket upgrading to spiral wound types witha center ring
n Replacement of valves
n Pump outages and pump seal failures
n Operational learning experiences
n Feed injector weld failures and modifications
ABB Oil, Gas and PetrochemicalsPBrkic71/20 DBK 00-10-04
Lessons Learned
n An IGCC plant is a highly integrated facility
n Each facility has its own operatingcharacteristics
n Continuous emissions monitoring systemsare time consuming to obtain certificationby the authorities