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UNIVERSITI PUTRA MALAYSIA
MOHAMAD MAAROFF BAHURDIN
FK 2012 135
OPTIMIZATION OF CUTTING CONDITIONS ON TOOL LIFE IN FACE MILLING SPHEROIDAL GRAPHITE CAST IRON
USING TAGUCHI METHOD
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OPTIMIZATION OF CUTTING CONDITIONS ON TOOL LIFE
IN FACE MILLING SPHEROIDAL GRAPHITE CAST IRON
USING TAGUCHI METHOD
MOHAMAD MAAROFF BAHURDIN
MASTER OF SCIENCE
UNIVERSITI PUTRA MALAYSIA
2012
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OPTIMIZATION OF CUTTING CONDITIONS ON TOOL LIFE IN FACE
MILLING SPHEROIDAL GRAPHITE CAST IRON USING TAGUCHI
METHOD
By
MOHAMAD MAAROFF BAHURDIN
Thesis Submitted to the School of Graduate Studies, Universiti Putra
Malaysia, in Fulfilment of the Requirements for the Degree of Master of Science
October 2012
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Abstract of thesis presented to the Senate of Universiti Putra Malaysia in fulfilment
of the requirement for the degree of Master of Science
OPTIMIZATION OF CUTTING CONDITIONS ON TOOL LIFE IN FACE
MILLING SPHEROIDAL GRAPHITE CAST IRON USING TAGUCHI
METHOD
By
MOHAMAD MAAROFF BAHURDIN
October 2012
Chairman: B.T. Hang Tuah Baharudin, PhD
Faculty: Engineering
ABSTRACT
The aim of this study was to determine the optimum cutting condition for face
milling when machining the nodular cast iron. The cutting conditions consist of the
cutting speed, the feed per tooth and the depth of cut. The original problem arose in
the crankshaft machining-line of the Proton engine shop where the face milling
cutting tool frequently changed due to premature of tool life. As a result, the
productivity of this production line was decreased. This problem occurred due to the
enhancement of the raw-cast hardness, and no detail study was made on the cutting
condition by the engine shop.
This study was carried in three experiments; the preliminary experiment,
optimization experiment and confirmation experiment. All experiments used the
same tool and the same material of the engine shop.The preliminary experiment
aimed to determine and benchmark the performance of the cutting tool and surface
roughness when machined in the laboratory environment. Taguchi optimization
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method was applied for optimization experiment. This experiment aims to regulate
the machining parameters of three parameters at three levels. A L9 orthogonal array,
signal-to-noise ratio and analysis of variance (ANOVA) were applied in order to
determine and analyzed the optimal cutting condition. The confirmation experiment
was conducted using the suggested cutting condition obtained from the optimization
experiment in order to validate the result.
The result of the preliminary experiment showed that the volume of material
removes using the current practice cutting condition was about two hundred and fifty
cubic centimetres. The average surface roughness measured was about point six
micrometers. The optimization result showed that the optimum cutting condition
capable to remove the material more than four hundred cubic centimetres with the
surface roughness measured about point six micrometers. Comparison between both
experiments shows that the result was different for about forty percent. This
indicated that the optimization experiment was successfully determined the optimal
cutting condition. Results obtained by Taguchi method match closely with ANOVA
and cutting speed is most influencing parameter. The confirmation experiment
conducted also agreed on the optimization experiment result where the result of
material removes volume and surface roughness was the same.
The results show that there is a proper way to determine the optimal cutting
conditions other than trial-and-error method, which indirectly saves operating costs.
It is recommended to the engine shop to adjust its current cutting conditions
according to the findings of this study. Research on the same topic by using another
grade inserts are recommended for further study.
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Abstrak tesis yang dikemukakan kepada Senat Universiti Putra Malaysia sebagai
memenuhi keperluan untuk ijazah Master Sains
PENGOPTIMUMAN KONDISI PEMESINAN PADA HAYAT MATA ALAT
DALAM PENGISARAN PERMUKAAN BESI TUANG BERGRAFIK BULAT
MENGGUNAKAN KAEDAH TAGUCHI
Oleh
MOHAMAD MAAROFF BAHURDIN
Oktober 2012
Pengerusi: B.T. Hang Tuah Baharudin, PhD
Fakulti: Kejuruteraan
ABSTRAK
Tujuan kajian ini adalah untuk menentukan parameter pemotongan yang optimum
untuk operasi mesin pengisar apabila memesin besi tuang bergrafik bulat. Parameter
pemotongan terdiri daripada kelajuan pemotongan, suapan per gigi dan kedalaman
pemotongan.Masalah ini asalnya berlaku di kilang pembuatan enjin Proton pada
baris pemesinan aci engkol di mana mata alat mesin pengisar ini kerap kali ditukar
disebabkan oleh hayat mata alat yang pramatang. Hasil dari kerapnya penukaran ini,
produktiviti barisan pengeluaran ini telah menurun. Masalah ini berlaku disebabkan
oleh peningkatan kekerasan bahan yang hendak di mesin, dan tiada kajian terperinci
telah dibuat pada parameter pemotongan oleh pihak kilang.
Kajian ini telah dijalankan dalam tiga bentuk eksperimen; eksperimen permulaan,
eksperimen pengoptimuman dan eksperimen pengesahan. Semua eksperimen telah
menggunakan mata alat dan bahan yang sama seperti yang digunakan oleh kilang
enjin. Eksperimen awal bertujuan untuk menentukan dan sebagai penanda aras
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prestasi mata alat memotong dan kekasaran permukaan apabila dimesin dalam
persekitaran makmal. Kaedah pengoptimuman Taguchi telah digunakan untuk
eksperimen pengoptimuman. Eksperimen ini bertujuan untuk mengawalselia
parameter pemesinan yang terdiri dari tiga parameter pada tiga peringkat. Tatasusn
ortogon L9, nisbah isyarat-kepada-hingar dan analisis variasi (ANOVA) telah
digunakan untuk menentukan dan menganalisis keadaan pemotongan yang optimum.
Eksperimen pengesahan telah dijalankan menggunakan keadaan pemotongan yang
diperolehi dari eksperimen pengoptimuman untuk mengesahkan hasilnya.
Hasil eksperimen permulaan menunjukkan bahawa jumlah bahan terbuang adalah
kira-kira dua ratus lima puluh sentimeter padu. Kekasaran permukaan purata yang
diukur ialah sebanyak perpuluhan enam mikrometer. Hasil eksperimen
pengoptimuman menunjukkan bahawa keadaan pemesinan optimum mampu
memotong bahan lebih daripada empat ratus sentimeter padu dengan kekasaran
permukaan diukur sebanyak perpuluhan enam mikrometer. Perbandingan antara
eksperimen permulaan dan pengoptimuman menunjukkan bahawa isipadu bahan
yang dibuang adalah berbeza sebanyak kira-kira empat puluh peratus. Ini
menunjukkan bahawa eksperimen pengoptimuman berjaya menentukan keadaan
pemotongan yang optimum. Keputusan yang diperolehi oleh kaedah Taguchi
sepadan rapat dengan ANOVA dan kelajuan pemotongan adalah parameter paling
mempengaruhi keputusan eksperimen. Eksperimen pengesahan dijalankan juga
bersetuju pada hasil eksperimen pengoptimuman di mana hasil jumlah bahan
terbuang dan kekasaran permukaan adalah sama.
Keputusan kajian ini menunjukkan bahawa terdapat satu cara yang betul untuk
menentukan keadaan optimum pemotongan selain dari percubaan secara rawak, yang
secara tidak langsung menjimatkan kos operasi. Adalah disyorkan kepada pihak
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kilang enjin untuk menyesuaikan keadaan paras semasa pemesinan menurut hasil
dari kajian ini. Penyelidikan mengenai topik yang sama dengan menggunakan satu
lagi gred sisipan adalah disyorkan untuk kajian seterusnya.
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ACKNOWLEDGMENTS
I would like to acknowledge the advice and guidance of Dr. BT. Hang Tuah
Baharudin and Professor Datin Napsiah Ismail, chairman and member of the
supervisory committee.
I also thank the UPM’s lab staff, especially Mr. Tajul Ariffin Md. Tajuddin and
Muhammad Wildan Ilyas Mohamed Ghazali. Special thanks go to Mr. Amir Abidin
Samsuddin and Mr. Azman Ismail, without whose knowledge and assistance this
study would not have been successful.
I acknowledge the Dr. BT Hang Tuah Baharudin and the UniKL’s STRG scheme for
their financial support for this project.
The case and data for this study were provided by Engine and Transmission
Manufacturing, a division of Proton Tanjung Malim Sdn. Bhd. I appreciate their
support.
I would like to thank my family members, especially my wife, Suzana Wati Zulkepli,
my son, M. Adam Fareez, my parents and my siblings for supporting and
encouraging me to pursue this degree.
Without my wife’s encouragement, I would not have finished the degree.
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I certify that a Thesis Examination Committee has met on 29 October 2012 to
conduct the final examination of Mohamad Maaroff Bahurdin on his thesis entitled
“Optimization of Cutting Conditions on Tool Life in Face Milling Spheroidal
Graphite Cast Iron Using Taguchi Method” in accordance with the Universities and
University Colleges Act 1971 and the Constitution of the Universiti Putra Malaysia
[P.U.(A) 106] 15 March 1998. The Committee recommends that the student be
awarded the Master of Science.
Members of the Thesis Examination Committee were as follows:
Dr. Mohd Khairol Anuar Mohd Ariffin, PhD Associate Professor
Faculty of Engineering
Universiti Putra Malaysia
(Chairman)
Dr. Shamsuddin Sulaiman, PhD
Professor
Faculty of Engineering
Universiti Putra Malaysia
(Internal Examiner)
Dr. Faieza Abdul Aziz, PhD Associate Professor
Faculty of Engineering
Universiti Putra Malaysia
(Internal Examiner)
Dr. Safian Sharif, PhD
Professor
Faculty of Engineering
Universiti Teknologi Malaysia
(External Examiner)
_____________________________
SEOW HENG FONG, PhD
Professor and Deputy Dean
School of Graduate Studies
Universiti Putra Malaysia
Date:
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This thesis was submitted to the Senate of Universiti Putra Malaysia and has been
accepted as fulfilment of the requirement for the degree of Master of Science. The
members of the Supervisory Committee were as follows:
B.T. Hang Tuah Baharudin, PhD
Senior Lecturer
Faculty of Engineering
Universiti Putra Malaysia
(Chairman)
Napsiah Ismail, PhD
Professor
Faculty of Engineering
Universiti Putra Malaysia
(Member)
_____________________________
BUJANG BIN KIM HUAT, PhD
Professor and Dean
School of Graduate Studies
Universiti Putra Malaysia
Date:
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DECLARATION
I declare that the thesis is my original work except for quotation and citations, which
have been duly acknowledged. I also declare that it has not been previously, and is
not currently submitted for any other degree at Universiti Putra Malaysia or other
institutions.
_________________________________
MOHAMAD MAAROFF BAHURDIN
Date: 29th October 2012
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TABLE OF CONTENTS
Page
ABSTRACT ii ABSTRAK iv
ACKNOWLEDGMENTS vii DECLARATION x
TABLE OF CONTENTS xi LIST OF TABLES xiii
LIST OF FIGURES xiv LIST OF ABBREVIATIONS xvii
CHAPTER
1. INTRODUCTION 1
1.1. Background of the Study 2
1.2. Crankshaft Machining Line 6
1.2.1. The roughing cells 7
1.2.2. The OP10 machining process 9
1.3. Problem Statement 12
1.4. Research Objectives 13
1.5. Scope of the Study 14
1.6. Significance of the Study 15
2. LITERATURE REVIEW 16
2.1. Introduction 16
2.2. The Cutting Condition Optimization 17
2.3. Milling of Cast Iron and Its Related Issues 20
2.4. Milling Process 23
2.4.1. Milling cutting parameters 23
2.4.2. Milling cutting tools 27
2.5. Cast Iron Alloys 39
2.5.1. Cast iron 40
2.5.2. Nodular cast iron and its machinability 42
2.5.3. The cast iron chip formation 45
2.6. Design of Experiment – Taguchi Method 46
2.6.1. Taguchi design method overview 47
2.6.2. Confirmation experiment 53
2.6.3. Signal-to-noise (S/N) ratio analysis 53
2.6.4. Analysis of variance (ANOVA) 55
2.7. Summary of Literature 58
3. MATERIALS AND METHODS 59
3.1. Introduction 59
3.2. Cutting Conditions’ Transformation 60
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3.3. Experiment Material 62
3.3.1. Work piece 62
3.3.2. Cutting tool 64
3.4. Equipment and Testing Facilities 66
3.5. Experiment Methodology 68
3.5.1. Material hardness measurement 69
3.5.2. Experimental run process flow 70
3.5.3. Preliminary experiment 76
3.5.4. Optimization experiment 76
3.5.5. The confirmation experiment 82
4. RESULTS AND DISCUSSION 83
4.1. Introduction 83
4.2. Preliminary Experiment 84
4.2.1. Preliminary experiment result and discussion 85
4.2.2. Tool wear analysis 87
4.2.3. Summary of the preliminary experiment 89
4.3. Optimization Experiment 89
4.3.1. Optimization experiment result 90
4.3.2. Signal-to-noise (S/N) ratio analysis 94
4.3.3. Analysis of variance (ANOVA) 97
4.3.4. Tool wear analysis 98
4.3.5. Discussion of the optimization experiment 100
4.4. Prediction and Confirmation Experiment 102
4.4.1. Removed volume (tool life) prediction 102
4.4.2. Confirmation experiment result and analysis 103
4.4.3. Discussion and conclusion of confirmation
experiment 107
4.5. Summary of Result and Discussion 108
5. CONCLUSIONS AND RECOMMENDATIONS 110
5.1. Conclusions 110
5.2. Recommendations for Further Studies 112
REFERENCES 113
APPENDICES 117 BIODATA OF STUDENT 121
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LIST OF TABLES
Table Page
Table 1.1: OP10 tool usage detail 9
Table 2.1: Mechanical properties of Nodular cast iron 43
Table 3.1: Current practice machining condition by the engine shop 60
Table 3.2: The initial machining condition for the study 61
Table 3.3: Chemical composition (wt %) for JIS G 5502 FCD 700 62
Table 3.4: Mechanical properties of JIS G 5502 FCD 700 62
Table 3.5: Cutting tool geometry and details (WGC4080R) 65
Table 3.6: Insert identification (SEMT13T3AGSN-G ACK300) 65
Table 3.7: Physical properties of insert coating 65
Table 3.8: The basic Taguchi L9 (34) orthogonal array 77
Table 3.9: Machining parameters and their levels 78
Table 3.10 Recommended cutting condition by the tool maker 78
Table 3.11: Experimental layout 79
Table 3.12: Complete randomization experimental run with replication 79
Table 3.13: Optimization experiment result summary 80
Table 4.1: Result of optimization experiment 90
Table 4.2: Detail study on experimental run #5 & #7 92
Table 4.3: Experimental result and S/N ratio 95
Table 4.4: S/N ratios response table - larger the better 96
Table 4.5: Analysis of Variance for S/N ratios 97
Table 4.6: Average removed volume of the optimization experiment. 100
Table 4.7: Parameter-level prediction for mean and S/N ratio. 102
Table 4.8: Result of confirmation experiment 104
Table 4.9: Comparison the prediction and conformation experiment result 104
Table 4.10: Summary of experiment result 108
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LIST OF FIGURES
Figure Page
Figure 1.1: Comparison of two-month production rate 3
Figure 1.2: Downtime analysis 4
Figure 1.3: Crankshaft S4PH 6
Figure 1.4: Crankshaft machining line layout 7
Figure 1.5: OP10 machining operation 8
Figure 1.6: OP20 operation, to turn the front shaft and counter weight 8
Figure 1.7: OP 10 tool usage 10
Figure 1.8: OP10 tool change frequency for two-month record 11
Figure 1.9: Tool deterioration frequency - not because of tool life 11
Figure 2.1: Illustration of axial depth of cut (ae) and radial depth of cut (ar) (Grote and
Antonsson, 2009) 26
Figure 2.2: Angles on an insert cutting tools (Stephenson and Agapiou, 2006) 27
Figure 2.3: Combination of principle angles: Double positive angles and its effect on
chips formation (Sumitomo Electric, 2010) 29
Figure 2.4: Combination of principle angles: Double negative angles and its effect on
chips formation (Sumitomo Electric, 2010) 30
Figure 2.5: Combination of principle angles: Negative-positive angles and its effect on
chips formation (Sumitomo Electric, 2010) 31
Figure 2.6: Approximate ranges of carbon and silicon for steel and various cast
irons.(“Ductile Iron Data - Section 12,” 2011) 41
Figure 2.7: Photomicrograph of Nodular Cast iron (Elgun, 2004) 42
Figure 2.8: Segmented chip formation 45
Figure 2.9: Discontinues chip formation 45
Figure 2.10: Built-up edge (BUE) 46
Figure 2.11: Taguchi DOE procedure 48
Figure 2.12: Fishbone diagram of parameters that may affect the machining desired
quality (Benardos and Vosniakos, 2003) 49
Figure 3.1: Work piece dimension 63
Figure 3.2: Cutting tool used 64
Figure 3.3: Indexable inserts 64
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Figure 3.4: Vertical CNC machining centre 66
Figure 3.5: Optical microscope for flank wears monitor and measurement 66
Figure 3.6: The surface roughness measurement device 67
Figure 3.7: Hardness testing machine 67
Figure 3.8: Hardness measurement points 69
Figure 3.9: Machining process flow 70
Figure 3.10: Cutting edges identification marks 71
Figure 3.11: Flank face and wear width measurement of an insert edge 71
Figure 3.12: Special jig for insert placement under microscope 71
Figure 3.13: Milling process with straddle cut method (Moltrecht, 1981) 73
Figure 3.14: Three spot for taking surface roughness measurement 74
Figure 3.15: The intersection graph to find the actual machining length 75
Figure 4.1: The preliminary experiment results; removed volume and its average 86
Figure 4.2: The preliminary experiment results; surface roughness and its average 86
Figure 4.3: Effect of tool life (removed volume) versus work piece hardness 86
Figure 4.4: Flank wears versus machining length 87
Figure 4.5: Flank wear 88
Figure 4.6: Abrasion wears on flank wear region 88
Figure 4.7: Discontinues chip formation 88
Figure 4.8: Optimization Experiment Result - Removed Volume 91
Figure 4.9: Feed per tooth effect on removed volume 93
Figure 4.10: Frequency of the different work piece hardness 94
Figure 4.11: S/N ratios response graph 96
Figure 4.12: Wear curves for Cutting Speed 99
Figure 4.13: Tool Life Curve 99
Figure 4.14: Tool wears of optimal condition 1 106
Figure 4.15: Tool wears of optimal condition 2 106
Figure 5.1: Tool wear - Experimental run 1 118
Figure 5.2: Tool wear – Experimental run 2 118
Figure 5.3: Tool wear – Experimental run 3 118
Figure 5.4: Tool wear – Experimental run 4 119
Figure 5.5: Tool wear – Experimental run 5 119
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Figure 5.6: Tool wear – Experimental run 6 119
Figure 5.7: Tool wear – Experimental run 7 120
Figure 5.8: Tool wear – Experimental run 8 120
Figure 5.9: Tool wear – Experimental run 9 120
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LIST OF ABBREVIATIONS
Cases
: Cutting tool edge angle 28
0 : Cutting rake angle 28
f : Radial rake angle 28
p : Axial rake angle 28
ae : Axial depth of cut 24
Al2O3 : Aluminum Oxide 34
ar : Radial depth of cut 24
CF : Catastrophic failure 37
CH : Chipping 37
CNC : Computer Numerical Control 3, 7
Co : Cobalt 32
CPS : Cam Profile Switching 4
CR : Cracks 37
CVD : Chemical vapor deposition 33
D : Milling cutter diameter (mm) 24
fe : Degree of error 56
FL : Flaking 37
fp : Degree of freedom for parameter p 56
ft : Total degree of freedom 56
fz : Feed per tooth (mm) 24
HRC : Rockwell hardness scale C 70
KT : Face wear 36
MPR : Monthly Performance Report 3
PD : Plastic deformation 37
PVD : Physical vapor deposition 33
Ra : Arithmetic mean surface roughness 68
SS’P : Corrected sum of square 58
SSe : Sum of square error 57
SSP : Sum of square for parameter 57
SST : Sum of square 57
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TiC : Titanium Carbide 34
TiCN : Titanium Carbo-Nitride 34
TiN : Titanium Nitride 34
VB :Flank wear 36
Vc : Cutting speed (m/min) 24
Vf : Feed velocity vector (mm/min) 24
Vp : Variance of the parameter 57
WC : Tungsten Carbide 32
z : Number of teeth 24
ρ : Parameter contribution 58
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CHAPTER 1
INTRODUCTION
In metal machining industries, various methods and instruments are being used to
acquire desired shape and dimensions. Until today, either conventional or modern
machine tool, the exploration in machining technology is still in vast progress. These
include new discoveries in various machining technologies such as in cutting tool
technology, machine tool technology and tool management strategies.
The introduction of these new technologies is only been appreciated and utilized by
some manufacturer. The main hurdle is the involvement of significant capital
investment that reflects all economic perspective such as cost and time which most
manufacture would not be interested. Majority of them prefers to carry out research
that could improve or maximize manufacturing system performance using the
existing available resources. Therefore, the research in determining the values of the
process parameters that yield the high-quality product is the most desirable (Baskar
et al., 2006; Benardos and Vosniakos, 2003).
Face milling is frequently used process in industrial machining to machine large and
flat surfaces in a very rapid and precise way. Normally, the cutter is equipped by
multi-edge of indexable inserts that can easily be replaced whenever the inserts have
reached its useful life. Many machining constraints should be considered as well as
the selection of machining parameters. The selection of proper machining parameters
using one self’s experience or from the handbooks will not always give the best
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results. Conversely, this may lead to shorten the tool life and directly increased the
production cost and ravage the production time.
1.1. Background of the Study
This study is based on the actual case condition originated from Proton Engine and
Transmission Plant (Proton ETM) situated at Tanjung Malim, Perak. This engine
shop is responsible to produce four main engine parts, namely cylinder head,
cylinder block, crankshaft and camshaft. There are two varieties of part as the engine
size is different, 1.3 and 1.6 liter engine, and the parts are produced in batches as a
changeover in equipment programming is required between parts. The parts produce
by this shop then shipped to another plant for assembly.
This shop floor consists of six machining process lines where two lines dedicated for
cylinder head machining, another two lines for camshaft, and the rests are for
crankshaft and cylinder block. The layout design for each line can be classified as a
flexible manufacturing system (FMS) except for camshaft as the raw-casts were
handled manually. As explained by (Groover, 2008), the FMS means a production
system that has an ability to identify and distinguish between the different incoming
part or product styles processed, quick changeover of physical setup and quick
changeover of operating instruction. Each process line consists of a group of
Computer Numerical Controls (CNC) machine tools, interconnected by an automated
material handling system such as conveyor, gantry or robotic arm to move part
between machines in the cell. All these systems are controlled by a distributed
computer system.
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Production analysis is conducted in order to evaluate the performance of each
production line. The analysis is based on the engine shop’s Monthly Performance
Result (MPR) report as a variety of data was recorded on it, such as machining and
assembly production status, process and material defects, downtime and etc. The
two-month machining performance results were analyzed as shown in Figure 1.1 and
Figure 1.2.
Prod Line
Months
Cyl. Bloc
k
Cran
ksha
ft
Cms-CP
S
Cms-S4
P
Cyl. He
ad 2
Cyl. He
ad 1
Mon
2
Mon
1
Mon
2
Mon
1
Mon
2
Mon
1
Mon
2
Mon
1
Mon
2
Mon
1
Mon
2
Mon
1
40
30
20
10
0
Pro
d R
ate
19.34
16.25
19.3421.83
28.12
33.47
39.4738.38
22.9821.24
8.967.54
Comparison of two months production rateTwo months production line analysis
Cyl. Head 1: Cylinder head machining line 1 Cyl. Head 2: Cylinder head machining line 2 Cmc-S4P: Camshaft machining line for standard engine Cmc-CPS: Camshaft machining line for CPS engine Crankshaft: Crankshaft machining line Cyl. Block: Cylinder block machining line
Figure 1.1: Comparison of two-month production rate
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Down cause
Prod Line
Month
BA
Cyl. Bloc
k
Cranks
haft
Cms-CPS
Cms-S4P
Cyl. H
ead 2
Cy l.
Hea
d 1
Cyl. Bloc
k
Cranks
haft
Cms-CPS
Cms-S4P
Cyl. H
ead 2
Cy l.
Hea
d 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
Mon 2
Mon 1
20
15
10
5
0
% P
rod
ucti
on
Ra
te
2.943.
13
20.90
11.13
8.31
6.70
8.31
7.73
7.08
6.48
1.05
5.64
7.87
16.20
15.90
7.06
8.18
4.72
8.18
2.84
4.42
6.35
0.53
7.13
Downtime analysisTwo months production line analysis
A: Inspection and quality adjustment B: Tool broke / changes
Figure 1.2: Downtime analysis
Figure 1.1 shows that the camshaft and the crankshaft production line have a
decreased rate compared to previous month. This indicates the lack of productivity,
which gives an immense impact to the monthly production target. According to
(Wilson, 2011), the production rate analysis is a measurement of the typical amount
of time it takes for a manufacturing operation to produce its goods, and this gives an
understanding of the relative efficiency of each machining line’s operation.
Further investigation was made by analyzing the downtime for each machining line
for both months. The downtime or stoppage is classified into two highly related
causes; one is because of the inspection and quality adjustment, and the other one is
because of the tool deterioration. The analysis result was shown in Figure 1.2.
Clearly, the percentage value between the two-month records of the crankshaft’s
machining line has shown a rapid increment of the downtime in both causes. The
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inspection and quality adjustment was 7.06% for month-one and rapidly increased to
15.90%. It goes the same for the other cause of the downtime; the tool broke and
change stoppages, where in the first month was only 11.13% and suddenly increased
to 20.90% in the second month. Compared with the other machining line, the
crankshaft is regarded as the most problematic production line.
Based on these results and the discussion with crankshaft’s production personnel, the
main cause of the frequent tool broke is because the mechanical properties of the raw
material have been improved. The improvement commenced mid 2009 as to fulfill
the need of the new car model. According to (Ahmad Shahrir Halimi, Head of
Department, Engine & Transmission Department, Proton Tanjung Malim Sdn Bhd,
pers. comm. 16 December 2009), as the improvement in raw-cast is not too
enormous, the management decided the part should be processed according to
previous condition without any changes to the process parameters and further study.
Since then, the problem of the tool broke frequently appeared on almost the
machining time which subsequently affecting the production target. Consequently,
the crankshafts’ production team has to adjust the machine setting to meet the need
of newly improved raw-cast. The common method used is the trial-and-error, and
this does not only involve in adjusting the machining parameter but also various
other's adjustment such as changing the cutting tool dimension and the sequence of
the machining process. This obviously led to a worst scenario as the production line
has about 22 operations on 31 CNC machines.
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1.2. Crankshaft Machining Line
The crankshaft machining line is designed to fabricate the crankshaft named SP4H
(Figure 1.3), for 1.6 engine size and S4PE, for 1.3 engine size; both were produced in
different batch, and the projected production target is 27 units per hour.
Figure 1.3: Crankshaft S4PH
The line have six manufacturing cells in which three cells for roughing process and
the rest for finishing process. The layout is as illustrated in Figure 1.4. Every cell has
more than four workstations and an operator. The operator is the person responsible
to monitor and verify the quality of a processed work piece after every 20 pieces. If
quality problems arise, the machine and cutting tool had to be inspected for error,
correction being made and recorded. After the correction is made, the adjustment
process then takes place where a single raw-cast will go through the entire machining
process and inspected again afterwards. If the processed part meets the desired
quality requirement, the subsequent process will continue in full capacity. This
adjustment process also implemented after a replacement of cutting tool.
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Figure 1.4: Crankshaft machining line layout
This machining line consists of 22 operations, and the entire systems are fully
automated except for part loading at the beginning of the conveyor, unloading at the
end of the production line and part inspection at every cell, which is done manually
by an operator. The gantry system is used to transport the part between the conveyor
and CNC machines.
The roughing line is intended to machine the part until it near net dimension. It
consists of seven operations within three cells. Based on discussion and interview
with the production personnel, this roughing line contributed higher downtime due to
the tool change and the adjustment process.
1.2.1. The roughing cells
First cell consists of four CNC machine tools, named OP10A, OP10B, OP20A and
OP20B. There are two operations involve in this cell; the primary OP10 operation is
to face mill both end facing (Figure 1.5), centering and reference face milling. The
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OP20 operation is to turn the front shaft and counter weight as illustrated in Figure
1.6.
According to observation and response from the operator, machine OP10 often has a
downtime, mainly because of frequent cutting tool's changes due to premature end of
tool life. It occupied nine different cutting tools, and the total cycle time projected is
97 seconds per part; the same cycle time for both part family.
Figure 1.5: OP10 machining operation
Figure 1.6: OP20 operation, to turn the front shaft and counter weight
Face mill and centering
Counter weight turning Front shaft turning
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1.2.2. The OP10 machining process
There are three major machining processes for OP10 with help of nine different
cutting tools. The major machining processes are the face milling of both ends of the
crankshaft, the centering for front and rear shaft and the reference face milling. Table
1.1 and Figure 1.7 show the details of the cutting tool used for each process and its
time. The most employed tools were the tool-four (T4) with 22.9%, tool-one (T1)
with 20.7% and tool-three (T3) with 14.8% of machining time.
Table 1.1: OP10 tool usage detail
Tool number Process detail Process time
(sec/process) Tool life set
Tool 1 Both end facing – milling 18.5 150
Tool 2 Rear centering – drill 7.5 250
Tool 3 Rear centering – drill 13.2 150
Tool 4 Rear turning – turning 20.5 150
Tool 5 Rear chamfering – turning 5.5 300
Tool 6 Reference face milling – milling 7.5 200
Tool 7 Front turning – turning 7.5 200
Tool 8 Front drilling – drill 5.5 500
Tool 9 Front centering – drill 3.5 500
Extracted from Proton ETM Crankshaft Process Sheet.
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Tool 1
Tool 2
Tool 3
Tool 4
Tool 5
Tool 6
Tool 7
Tool 8
Tool 9
Category
Tool 93.9%Tool 8
6.2%
Tool 78.4%
Tool 68.4%
Tool 56.2%
Tool 423.0%
Tool 314.8%
Tool 28.4%
Tool 120.7%
OP 10 tool usage (sec/raw-cast)OP 10 tool analysis
Figure 1.7: OP 10 tool usage
Therefore, an analysis of the frequent tool change was made. The three tools: T4, T1
and T3 are predicted to have frequent changes. The two-month tool change record of
OP10 is analyzed and the result shows in Figure 1.8. As predicted, it clearly showed
that the most frequent tool change is T1 with 77 times, T4 with 70 times and T3 with
58 times. However, these change frequencies are not only counted for tools that
reach its service life but also for the tool that deteriorated before its end of life such
as fracture and deform.
Figure 1.9 shows the frequency of tool change because of premature tool life. The
highest frequent change because of this early tool life is T1 with 39 times, which is
about 50% of the total tool change recorded. The T4 is the second highest recorded
with 34 times of overall 70 times of tool change made. It is nearly 48% of the tool
change due to the premature tool life.
The T1 tool lifespan set as in Table 1.1 is infrequently achieved. On average, the T1
lifespan is only capable to machine up to 94 raw-casts. It is about 60.27% from the
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total lifespan set. Obviously, any improvement on T1 will provide positive outcomes
for the productivity.
Tool 9Tool 8Tool 7Tool 6Tool 5Tool 4Tool 3Tool 2Tool 1
80
70
60
50
40
30
20
10
0
Tool number
Ch
an
ge
fre
qu
en
cy
6
25
4341
27
70
58
33
77
OP 10 tool change frequency for two-month recordOP 10 tool analysis
Figure 1.8: OP10 tool change frequency for two-month record
Tool 9Tool 8Tool 7Tool 6Tool 5Tool 4Tool 3Tool 2Tool 1
40
30
20
10
0
Tool number
To
ol d
ete
rio
rati
on
fre
qu
en
cy
2
8
10
8
6
34
8
4
39
OP10 tool deteriorate frequencyTool change record analysis
Figure 1.9: Tool deterioration frequency - not because of tool life
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1.3. Problem Statement
The performance of the crankshaft machining line previously was very satisfying and
often achieves the desired production target without many hassles. The production
output target is 97 units per hour. However, the production performance declined
drastically since mid-2009 due to increase of the production downtime such as the
tool change, the adjustment and the inspection of quality. The frequent production
downtime is because of the mechanical properties of the raw-cast has been improved
where the hardness of the material was increased from averagely 230HB to 255HB.
This material improvement is mandatory as to meet the requirement of the new
engine specification.
An investigation was made to machine OP10 as it was the first machine of the
production chain and reported as a liability to the entire machining line. The result
found that some of the cutting tool had frequently failed prematurely. There are nine
different cutting tools equipped within this OP10, but the most failed cutting tool was
T1 which is responsible to face mill both-ends of the crankshaft. The tool life limit is
design to cut about 150 raw-casts, but currently, the tool only able to cut on average
94 raw-cast. For a record, there is no preliminary study made to the lifespan of the
cutting tool after the improvement of the raw-cast. Hence, this study will determine
the T1 performance when face milling the newly improved raw-cast.
The need for T1 cutting tool replacement to the other grade or other specification is
impractical as the current tool is still capable to withstand the material hardness up to
300HB (Sumitomo Electric, 2010). Moreover, if the conversion to other grades or
brand of the cutting tool, it will consume huge cost and time. Therefore, this study
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also seeks the possibility to improve the T1 machining length. The proposed
improvement was to determine the optimal cutting parameters in order to obtain the
maximum T1 lifespan. However, the material removal rate should remain the same
or higher than the current practices as any reduction in this rate will result in low
productivity and definitely will not be accepted by the engine shop management.
Therefore, the need for evaluating the T1 performance with the new raw cast is
essential as to be compared with previous performance. This performance evaluation
will show the new T1 lifespan with the current machining parameters. It is expected
that the T1 lifespan will be reduced. Since the T1 ability toward the new work piece
is the still broad, hence, further study in seeking the maximum T1 utilization is a
must. The optimal T1 cutting parameters should be determined for maximizing the
tool life in terms of removed volume.
1.4. Research Objectives
The aim of this study is to evaluate and improve the T1 performance. The desired
outcome of this study is to maximize the service life of T1 while maintaining the
surface finish quality. Therefore, the specific objectives of this study are as follows:
i. To evaluate the performance of T1 insert in terms of removed volume
and the average surface roughness when face mill the spheroidal
graphite cast iron using the current engine shop cutting condition (the
initial cutting condition) in the laboratory environment.
ii. To determine the optimal cutting condition for the tool lifespan (T1)
in terms of materials removed volume when face milling the
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spheroidal cast iron by controlling three parameters at three levels
using Taguchi optimization technique with the averaged machined
surface response not exceeds 50 µm.
1.5. Scope of the Study
This study focuses on finding the optimal machining conditions namely cutting
speed, feed rate and depth of cut for face milling operation to obtain the optimum
material removed volume. At the same time, the quality of machined surface should
be monitored as there is a tolerance limit where its Ra value should not exceed or
equal to 50 µm.
The optimization method used in this study is the Taguchi method as it was proven to
be the simplest yet efficient method by many researchers such as (Gopalsamy et al.,
2009; Kacal and Gulesin, 2011; Khorasani et al., 2011; Lin, 2002a, 2002b; Tosun et
al., 2004; Yang and Tarng, 1998; Zhang et al., 2007).
Only one type of milling insert and one type of material is employed during this
whole study. For every experimental run, only one insert is used at a time. According
to (Richetti et al., 2004), results from the milling test using lesser number of inserts
than the cutter capacity can be used as comparison index of the machinability
between two or more machining conditions. (Lin, 2002a, 2002b), mentioned that the
uses only one insert during milling is acceptable in order to simplify the tool life
analysis. Furthermore, it also reduces the experiment cost and time.
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1.6. Significance of the Study
This study provided better understanding of various manufacturing aspects, and also
method for process improvement. These include the machining tools' operation and
its dynamism, cutting tool performance measurement, and method for quality
improvement.
Furthermore, utilization of Taguchi technique in seeking the optimal value of
machining parameters is presented in proper step according to (Khorasani et al.,
2011; Lin, 2002a; Ross, 1995). The optimization technique proposed hopefully will
benefits and help future researchers as guidance.
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