Unit 4 2010 Summary Turbine

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  • 7/28/2019 Unit 4 2010 Summary Turbine

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    CONFIDENTIAL

    APS FOUR CORNERS

    UNIT 4 WINTER 2010 OVERHUAL SUMMARY TURBINE

    1475E.SAMHOUSTONPKWYS.SUITE#100,PASADENA,TX.77503PH(281)8845160FX(281)4769454

    PAGE1OF2

    BOILER FEED PUMPS

    The 14X16 expander and the 16 discharge piping coming off the north and south

    boiler feed pumps have been inspected utilizing the 37 DLplus Panametrics thickness gauge.

    These two components were check for thickness by establishing a 2 grid on the pipe surface.

    UT thickness was collected at the grid points and recorded in a data table included in the report

    following. The north 14X16 expander had an average UT thickness of 2.299 and the 16 pipe

    had an average reading of 2.369 which is well above the minimum wall thickness 2.040. The

    south boiler feed pump 14X 16 expander have an average UT thickness reading of 2.315 and

    the 16 pipe of an average UT thickness reading of 2.385, both components wall thicknesses are

    well above the minimum wall thickness of 2.040.

    HIGH ENERGY PIPING

    HOT REHEAT PIPING- A total of 4 girth welds have been inspected. The inspection

    method used included Wet Fluorescent Magnetic Testing, (WFMT) inspection, UT Shear Wave

    inspections, UT thickness inspection, and circumferential measurements on 4 welds. Prior to UT

    shear wave inspection on the HEP, all welds were prepared buffed cleaned, WFMT inspected,

    UT thickness inspected in four quadrants and circ. measured both up and downstream from the

    weld. The welds included the following: FW-61, FW-81,(tee to pipe butt weld) FW-66, and

    FW-87(elbow to pipe) located on the mezzanine deck inside the turbine building. No relevant

    indications have been found.

    MAIN STEAM PIPING- 13 girth welds have been inspected on the Main Steam piping

    system. Several type of inspection method was utilized to inspect these welds: WFMT

    inspection, UT thickness measurement in four quadrants, circumferential measurement upstream

    and downstream from the weld where possible, and 100% UT Shear Wave. All girth welds were

    power buffed cleaned free of scale material about 12 on each side of the weld. The following

    girth welds have been inspected: matching speed valve connections weld located on the

    mezzanine deck inside the turbine building, no relevant indication found; 4 each Main Steam

    Stop Valve (MSSV) inlet piping welds, weld #s FW 1-13, FW 1-14, FW 2-13, FW 2-14, no

    relevant indication found on all four welds; 4 each MSSV to Main Steam Control Valve

    (MSCV), MSSV #1 to MSCV #1, MSSV#2 to MSCV #2, MSSV#3 to MSCV #4, MSSV #4 toMSCV #3; and 4 each MSCV outlet piping weld #s FW 1-15, FW 1-16, FW 2-15, and FW 2-16.

    Several surface linear indications has been found on all 4 of the MSSV to MSCV girth welds,

    they range from 3/16 to 3/8 in lengths, all indications have been grind out and re-inspected, no

    relevant indications has been noted on the excavated areas. The excavation depth did not exceed

  • 7/28/2019 Unit 4 2010 Summary Turbine

    2/2

    CONFIDENTIAL

    APS FOUR CORNERS

    UNIT 4 WINTER 2010 OVERHUAL SUMMARY TURBINE

    1475E.SAMHOUSTONPKWYS.SUITE#100,PASADENA,TX.77503PH(281)8845160FX(281)4769454

    PAGE2OF2

    1/8 and no repairs were needed. No relevant indications were found on the MSCV outlet pipingweld #s FW 1-15 and FW 2-16. MSCV outlet piping weld # FW 1-16 had several linear

    indications, 3/16 to 1\4 in length, all indications has been ground out and re-inspected. No

    relevant indications were found and the excavation depth did not exceed 1/8, no repairs were

    needed.

    MSCV outlet piping weld # FW 2-15 have several linear indication at the toe of the weld,

    during the initial inspection two 3/16 LI have been found on the bottom toe of weld and the

    west side of the pipe and a 1 LI was found on the southwest of the pipe. These three linear

    indications crack open and they connected during the freezing of the MSCV to replace the seats

    inside the valve body. The 1 linear indication develop to a 6 crack and connected to the 3

    1/16 indication, this linear indication have been ground out and re-inspected and no relevantindications has been found, excavation depth did not exceed 1/8. The two 3/16 linear

    indication cracked open to a 7/8 depth and 4 in length. Samples have been cut out, sent to

    the libratory to be analyzed. Another WFMT and UT shear wave inspection was performed

    where the boat samples have been cut out prior to welding the excavation area and no relevant

    indications have been found. Also 4 valve seat pin have been welded back on the control valve

    during excavation repairs, these 4 welds and the repair weld have been dry MT inspected before

    the post weld heat treatment. A final inspection on the excavation area and the 4 seat pins was

    conducted by means WFMT and UT shear wave, no relevant indications has been found.