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Thermal Load Effect on Vibration on a Reactor FWP - FSRUGfsrug.org/Presentations2016/13.pdf · 2016...
Transcript of Thermal Load Effect on Vibration on a Reactor FWP - FSRUGfsrug.org/Presentations2016/13.pdf · 2016...
Thermal Load Effect on Vibration on a Reactor FWP
By:
Maki M. Onari MSI Principal Engineer
Manager of Turbomachinery Testing11 Apollo Drive
Whippany, NJ 07981Tel: (973) 326-9920
George InchExelon Corp. Senior Staff Engineer
Nine Mile Point Nuclear Generating Station348 Lake Road
Oswego, NY 13126Tel: (315) 349-2441
Embassy SuitesSan Antonio, TX1.25 – 1.28.2016
2016 Feedwater SystemReliability Users Group (FSRUG)
PresentersMaki M. Onari:• Mechanical Solutions, Inc. – Manager of Turbomachinery Testing -
Principal Engineer: responsible for all MSI Turbomachinery Testing• B.S.M.E., Zulia University, Venezuela• Rotating Equipment Engineer, PDVSA: responsible for the predictive
maintenance of one of the largest petrochemical complex in Latin America• Co-Author Pump Vibration Chapter, McGraw-Hill Pump Handbook• Member of ASME and the ISO TC108/S2 Standards Committee for
Machinery Vibration• Presented tutorials, case studies, and lectured at the Texas A&M Symposia
since 2007 as lead instructor on vibration short courses.
George Inch:• Sr. Staff Engineer Mechanical Design Engineering at Nine Mile Point
Nuclear Station (Exelon Nuclear)• 26 years of experience at NMPNS
General Information
Constellation Energy – Exelon Corp.
Nine Mile Point Nuclear Station (NMPNS) Unit 2 – 1150 MW (Oswego, NY)
Application: Reactor Feed Water Pump (2FWS-P1A/B/C)
Manufacturer: Byron Jackson (Legacy Pump OEM)
Type: 20x20x22 HSB – 2 Stage (barrel type radial split)
Capacity: 8,000 gpm (min flow) to 22,870 gpm (max flow)
Normal operation steady slightly above BEP
Suction Press.: 550 psig
Discharge Press.: 1,200 psig
Speed: 3,339 rpm (55.7 Hz)
Temperature: 382 ºF
Normal Load: 10,500 to 11,500 BHP
General Information Cont.
Driver: Electric Machinery Induction Motor
(rated 16,500 HP @ 1785 rpm (29.8 Hz)
Gearbox: General Electric Speed Increaser (Gear ratio 1:1.87)
Modifications: Impeller vanes were changed from 5 to 7 vanes
New min-flow valve
Smoother suction passage
New bearing brackets and housings
New suction covers and bearings
General Information Cont.
Former 2FWS-P1A Cross Section
Byron Jackson 20x20x22 HSB – 2 Stage
Background• Mechanical seals have experienced repetitive failure since 1987 (MTBF of 6
months, mostly on the Alpha FWP). Possible axial shuttling of the pumprotor.
• Based on analysis performed by the OEM, it was concluded that the pumps
required a series of modifications in order to improve seal reliability and
also increase plant capacity by 15% (EPU).
– Redesigned mechanical seals
– New impellers
– Flow path to the first stage impeller
– Inboard (IB) suction cover
Background– Alpha FWP modified in spring 2010. High synchronous vibration was
detected only at the IB end of the pump shaft (over 4.2 mils pk-pk).
– FAT vibration on the order of 1.0 to 1.5 mils pk-pk.
– Vibration amplitude proportional to the load of the plant.
– It was recommended to modify the cold alignment between the pump
and the gearbox (on-line hot alignment monitoring).
General Information Cont.
Modified 2FWS-P1A Cross Section
Vibration Testing Approach
• Experimental Modal Analysis (EMA) test
• Continuous Monitoring (CM) testing
• Operating Deflection Shape (ODS) testing
Experimental Modal Analysis (EMA)
June 2010 Vibration DataAlpha FWP Initial Testing
2FWS-P1A Pump Typical FRF PlotsFrequency Respo nse(Signal 4,Signal 17) - M ark 1 (M agnitude)
Working : 01 h rec 6 : Input : Enhanced
0 40 80 120 160 200 240 280 320 360 400
1u
3u
10u
30u
100u
300u
1m
3m
10m
[Hz]
[g/lbf] Frequency Respo nse(Signal 4,Signal 17) - M ark 1 (M agnitude)
Working : 01 h rec 6 : Input : Enhanced
0 40 80 120 160 200 240 280 320 360 400
1u
3u
10u
30u
100u
300u
1m
3m
10m
[Hz]
[g/lbf]
44 Hz
89 Hz1x r
pm
(57 H
z) Horizontal
Direction
Axial
Direction
Frequency Respo nse(Signal 2,Signal 17) - M ark 1 (M agnitude)
Working : 01 a rec 7 : Input : Enhanced
0 40 80 120 160 200 240 280 320 360 400
1u
3u
10u
30u
100u
300u
1m
3m
10m
[Hz]
[g/lbf] Frequency Respo nse(Signal 2,Signal 17) - M ark 1 (M agnitude)
Working : 01 a rec 7 : Input : Enhanced
0 40 80 120 160 200 240 280 320 360 400
1u
3u
10u
30u
100u
300u
1m
3m
10m
[Hz]
[g/lbf]
1x r
pm
(57 H
z)
59.25 Hz
Frequency Respo nse(Signal 1,Signal 17) - M ark 1 (M agnitude)
Working : 01 v rec 8 : Input : Enhanced
0 40 80 120 160 200 240 280 320 360 400
1u
3u
10u
30u
100u
300u
1m
3m
10m
[Hz]
[g/lbf] Frequency Respo nse(Signal 1,Signal 17) - M ark 1 (M agnitude)
Working : 01 v rec 8 : Input : Enhanced
0 40 80 120 160 200 240 280 320 360 400
1u
3u
10u
30u
100u
300u
1m
3m
10m
[Hz]
[g/lbf]
395 Hz
1x r
pm
(57 H
z)
89 Hz
Vertical
Direction
2FWS-P1A Pump Main Mode Shapes
Lateral Rocking Mode @ 44 Hz Twist Mode @ 89 Hz
Axial Rocking Mode @ 59.3 Hz OBB Vertical Mode @ 395 Hz
Continuous Monitoring (CM) Testing
14
6600 gpm min-flow
9300 gpm min-flow
9300 gpm to Reactor
14000 gpm to Reactor
17000 gpm to Reactor
18000 gpm to Reactor
20000 gpm to Reactor
15400 gpm to Reactor
Pump Shaft Vibration
16
Pump Shaft Vibration
17
Pump IBB Housing VibrationAxial
Horizontal
Vertical
18
Pump OBB Housing VibrationAxial
Horizontal
Vertical
19
* View from pump end unless otherwise stated
Gearbox HS DE Orbit Plots
6600 GPM14:00, 6-12-2010
9300 GPM14:30, 6-12-2010
9300 GPM15:00, 6-12-2010
20000 GPM3:56, 6-13-2010
20
Pump IBB Orbit Plots
6600 GPM14:00, 6-12-2010
9300 GPM14:30, 6-12-2010
9300 GPM15:00, 6-12-2010
20000 GPM3:56, 6-13-2010
* View from pump end unless otherwise stated
21
Pump OBB Orbit Plots
6600 GPM14:00, 6-12-2010
9300 GPM14:30, 6-12-2010
9300 GPM15:00, 6-12-2010
20000 GPM3:56, 6-13-2010
* View from pump end unless otherwise stated
Shaft Center Line Position Relative to Original Cold Alignment Position
22
Operating Deflection Shape (ODS)
23
• Natural excitation signature of the rotating equipment
• Steady load operation
• Hundreds of vibration measurements with reference signal
• Data base of amplitude vs. frequency and phase angle
• 3-D CAD model assigning motion to each individual vibration data point
• Create animations of the equipment and related piping and foundation
Operating Deflection Shape (ODS)
24
ODS Animation at 1x rpm
25
• Misalignment: Severe offset misalignment between the HS
gearbox pinion shaft and the pump.
• Coupling Imbalance: Eccentricity of the coupling spacer from the
coupling mounting center line.
• Thermal growth between the pump shaft and the HS gearbox
pinion.
• Modify the cold alignment
• Verify the radial position of the coupling spacer for potential
eccentricity that could lead to imbalance forces.
Preliminary Conclusions & Recommendations (Possible Causes)
March 2011 Vibration DataAlpha FWP Testing – Root Cause Detection
• Radial bearings with tri-land bearings (7 mils diametral clearance) toforce the shaft operation closer to the center line of the pump.
• Reduced the torque on the OB pump foot bolts to facilitate thermalgrowth according to the OEM’s specifications.
• Adjusted the turn-buckles as per OEM’s specifications.
• Verified/ corrected the misalignment of the entire train.
• Installed temporary thermocouples at the IB and OB faces of the pumpcasing to measure transient temperature field.
• Installed temporary laser instrumentation to measure thermal growth ofthe pump casing in the axial and horizontal directions.
• Modified the warm-up procedure to alleviate rubbing during highthermal gradients within the pump (reduced seal cooling water flowrate from 10 to 5-7 GPM).
Modifications Performed in March 2011
GB HS DE - Shaft Vibration
Start-up Shut-down
Pump IBB - Shaft Vibration
Start-up Shut-down
Pump OBB - Shaft Vibration
Start-up Shut-down
GB HS DE - Shaft Movement
Warm-up Start-up Shut-down Cool-down
Pump IBB - Shaft Movement
Warm-up Start-up Shut-down Cool-down
Pump OBB - Shaft Movement
Warm-up Start-up Shut-down Cool-down
Shaft Orbits
N
View from East (pump OBB)
Shaft Orbits
N
View from East (pump OBB)
Shaft Centerline Plots
Through Cool-down
XY
XY
XY
N
View from East (pump OBB)
Preliminary Conclusions / Observations1. The root cause of the elevated vibration amplitude at the IBB of the
pump was due to thermally induced pump shaft bending.
2. Excessive pump shaft vibration. Mostly at 1x rpm, representing 57% ofthe total bearing clearance of 7 mils. There was a reduction in theamplitude by approximately 2.0 mils pk-pk as compared to the start-upperformed in December 2010 (~6.0 mils pk-pk).
3. At the start-up, the shaft bow effect quickly moved from the OB towardsthe IB end, then progressively worsened before leveling off at about 3.9mils pk-pk.
4. During the cool-down process, the pump shaft shifted approximately 2.5mils at the IB end while it shifted less than 1.0 mil at the OB end. Thegearbox HS shaft shifted approximately 0.5 mils at the DE.
5. Overall vibration throughout the pump train was less than 0.14 in/s rms.
Preliminary Recommendations
1. MSI recommended performing a Total Indicator Run-Out (TIR) map ofthe pump rotor mounted on V-blocks at room temperature. This shouldbe repeated after heating the entire pump rotor between bearings toconfirm the presence, location, and severity of any kinks in the shaft.
2. Conduct Finite Element Analysis (FEA) to analyze the thermal behavior ofthe pump casing and rotor at different temperature gradients measuredwith the thermocouples.
June 2012 Vibration DataAlpha, Bravo & Charlie FWP
Final Follow-Up Testing
Modifications (EPU Project)• New rotating elements on all three pumps.
• Improved inlet geometry for the 1st stage impeller (smoother suction stream passage or flow path towards the first stage impeller) like 2FWS-P1A pump.
• Balance drum re-dimensioned to provide unidirectional thrust load at any flow rate (rotor at times had been under compression towards the outboard (OB) end).
• Higher thrust load capacity (22,000 lbf) Kingsbury bearing with leading edge grooves (LEG) and RTDs.
• Thicker inboard (IB) suction cover due to resonance at 5x rpm and due to suspected acoustic resonances at 5x and 10x in the suction pipe (concluded by others).
Modifications (EPU Project)• Min-flow valves FV2B and FV2C were also replaced (like FV2A in 2010)
• 360 drip-pockets like 2FWS-P1A pump in 2010.
• Tri-land bearings like 2FWS-P1A pump in 2011.
• New gear sets on all three pumps to increase the output speed from 3,339 rpm to 3,400 rpm along with a new mechanical lube-oil pump.
• 11 GPM seal injection replaced by an API Plan 23 (thermo-syphon closed loop with a pumping ring). This was causing deformation of the inboard end cover of the pump.
Modifications (EPU Project)• Previous seal injection design allowed accumulation of condensate seal
water at the bottom of the pump casing with lower temperature than the reactor feed water. This was causing distortion of the inboard cover plate and therefore internal misalignment at the IBB.
2FWS-P1A Gearbox Low-Speed Shaft - NDE
44
Low and acceptable vibration amplitude of the gearbox LS shaft
2FWS-P1A Pump Shaft Vibration - Inboard
45
Low and acceptable vibration amplitude of the pump shaft
2.3 mils pk-pk
2FWS-P1A Pump Shaft Vibration - Outboard
46
Low and acceptable vibration amplitude of the pump shaft
2FWS-P1A Pump Inboard Bearing Vibration
47
Acceptable overall vibration
Vibration amplitude change
0.29 in/s rms
0.20 in/s rms
2FWS-P1A Pump Outboard Bearing Vibration
48
Acceptable overall vibration
Vibration amplitude change
0.30 in/s rms
0.20 in/s rms
2FWS-P1A Shaft Orbits @1am 6-12-2013
49
Pump Inboard Bearing GB HS Driven Bearing GB LS Driven Bearing Motor Driven Bearing
Pump Outboard Bearing GB HS Blind Bearing GB LS Blind Bearing
Acceptable orbit sizes
Final Conclusions1. Modifications implemented on these pumps during the outage (i.e. seal
injection API plan 23) eliminated the thermal distortion effect that wascausing deformation of the inboard end cover of the pump.
2. Previous seal injection design allowed accumulation of condensate sealwater at the bottom of the pump casing with lower temperature thanthe reactor feed water. This was causing distortion of the inboard coverplate and therefore internal misalignment at the IBB.
3. The shaft vibration at the IBB used to be approximately 4.5 mils pk-pk,while the vibration at the OBB was approximately 1.0 mil pk-pk.Vibration data gathered after the outage indicated significantimprovement at the IBB (3x reduction).
4. Radial proximity probe GAP voltage readings were not changing overtime during the warm-up or cool-down processes, versus such changesthat had been identified in previous tests.
Final Recommendations1. Pre-installation FEA analysis (structural and thermal) would have been
able to reduce risk and can spot problems before they occur(PREVENTION).
2. ODS / EMA / Continuous Monitoring Tests coupled with appropriateanalysis is a powerful troubleshooting tool to identify and visuallyunderstand the most difficult vibration problems in turbomachinery andpumping systems.