Water Energy Nexus Retrofitting Urban Areas to achieve zero pollution
THE COST-EFFECTIVENESS OF RETROFITTING SANITARY … · overcome this water crisis and save water...
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THE COST-EFFECTIVENESS OF RETROFITTING SANITARY FIXTURES
IN RESTROOMS OF A UNIVERSITY BUILDING
A Thesis
by
BYOUNG HOON HWANG
Submitted to the Office of Graduate Studies of Texas A&M University
in partial fulfillment of the requirements for the degree of
MASTER OF SCIENCE
August 2003
Major Subject: Construction Management
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THE COST-EFFECTIVENESS OF RETROFITTING SANITARY FIXTURES
IN RESTROOMS OF A UNIVERSITY BUILDING
A Thesis
by
BYOUNG HOON HWANG
Submitted to Texas A&M University in partial fulfillment of the requirements
for the degree of
MASTER OF SCIENCE Approved as to style and content by: Paul K. Woods Ifte M. Choudhury (Chair of Committee) (Member) F. Michael Speed James C. Smith (Member) (Head of Department)
August 2003
Major Subject: Construction Management
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ABSTRACT
The Cost-effectiveness of Retrofitting Sanitary Fixtures
in Restrooms of a University Building. (August 2003)
Byoung Hoon Hwang, B.S., Hanyang University, Korea
Chair of Advisory Committee: Dr. Paul K. Woods
This study measured the actual water consumption of sanitary fixtures installed in
restrooms of a university building while most studies have been based on the
manufacturer’s reported flow rate. Furthermore, this study analyzed the appropriateness
of retrofitting with low-consumption water closets and urinals based on the actual water
consumption.
The purpose of this study is to analyze the cost-effectiveness of water savings from
retrofitting water closets and urinals in restrooms of the Langford Architecture building
A at Texas A&M University. The researcher directly measured the actual water-volume
per flush of as-is, tune-up, low-consumption manual, and low-consumption automatic
water closets and urinals. The data collected by these observations was analyzed, and the
researcher evaluated the water savings of retrofitting water closets and urinals.
Finally, this study provides the actual water-consumption data of sanitary fixtures and
proves that retrofitting with low-consumption fixtures can save on water costs. The
results will present practical standards to facility managers and other building
professionals and will also contribute to determining the feasibility of retrofitting water
closets and urinals.
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TABLE OF CONTENTS
Page
ABSTRACT ………………………………………………………………………. iii
TABLE OF CONTENTS ……………………………………………………….… iv
LIST OF FIGURES ……………………………………………………………..... v
LIST OF TABLES …………………………………………………………….….. vii
INTRODUCTION ………………….…………………………………………….. 1
Background ……………………………………………………….. 1 Purpose and scope …………………………………………….…... 3 Literature review …………………………….……………………. 4 Experiment method …….…………………………………………. 8
RESULTS OF WATER CLOSETS ……….……………………………………... 15
Pilot test: As-is phase of water closets …………………………….16 Tune-up phase of water closets …………………………………… 20 Low-manual phase of water closets …………………………….… 29 Low-automatic phase of water closets ………………………….… 36 Summary of water closets ………………………………………… 42
RESULTS OF URINALS ……….………………………………………………... 46
Pilot test: As-is phase of urinals …………………………………...47 Tune-up phase of urinals ………………………………………….. 52 Low-manual phase of urinals ……………………………………... 64 Low-automatic phase of urinals …………………………………... 71 Summary of urinals ……………………………………………….. 77
CONCLUSIONS …………………………………………………………………. 81
REFERENCES ….………………………………………………………………... 84
APPENDIX A ….……………………………………………………………….… 85
VITA …..………………………………………………………………………….. 86
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LIST OF FIGURES
FIGURE Page
1 Men’s restroom layout in the building ……………………………………. 9
2 Women’s restroom layout in the building ………………………………... 9
3 Water closet and urinal in the as-is phase …………………………….…... 10
4 Valve in the tune-up phase ………………………………………………... 11
5 Water closet and urinal in the low-manual phase ………………………… 12
6 Water closet and urinal in the low-automatic phase ……………………… 12
7 Measurement methods ………………………………………………….… 13
8 Water meter in the basement ……………………………………………... 14
9 Scatter plot - measured data (plug method) ………….……………….…... 18
10 Graph - balloon vs. plug methods ………………………………………… 22
11 Scatter plot - measured data ………………………………………………. 24
12 Graph - water meter vs. measured data …………………………………… 26
13 Scatter plot - water meter vs. measured data ……………………………... 27
14 Scatter plot - measured data ………………………………………………. 31
15 Graph - water meter vs. measured data …………………………………… 33
16 Scatter plot - water meter vs. measured data …….……………………….. 34
17 Scatter plot - water meter vs. measured data ……………………………... 37
18 Residual histogram - water meter vs. measured data ……………………... 39
19 Scatter plot - measured data ………………………………………………. 41
20 Graph - means in water closets …………………………………………… 42
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FIGURE Page
21 Graph - measured mean vs. standard in water closets ……………………. 44
22 Graph - coefficient of variance in water closets ………………………….. 45
23 Scatter plot - measured data (plug method) ………………………………. 48
24 Scatter plot - measured data (balloon method) ……………………….…... 51
25 Scatter plot - measured data (balloon method) …….……………………... 55
26 Graph - balloon vs. plug methods ………………………………….……... 56
27 Scatter plot - balloon vs. plug methods …………………………………… 57
28 Residual histogram - balloon vs. plug methods …………………………... 58
29 Graph - water meter vs. measured data (balloon method) ………………... 61
30 Scatter plot - water meter vs. measured data (balloon method) …………... 61
31 Scatter plot - measured data (balloon method) …….……………………... 66
32 Graph - water meter vs. measured data …………………………………… 68
33 Scatter plot - water meter vs. measured data ……………………………... 69
34 Scatter plot - water meter vs. measured data ……………………………... 72
35 Residual histogram - water meter vs. measured data ……………………... 74
36 Scatter plot - measured data ………………………….……………………. 76
37 Graph - measured means in urinals ……………………………………….. 77
38 Graph - measured mean vs. standard in urinals …………………………... 79
39 Graph - coefficient of variance in urinals ………………………………… 80
40 Graph - actual water-volumes ………………………………………….…. 82
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LIST OF TABLES
TABLE Page
1 National water efficiency standards ………………………………………. 5
2 Collected data in water closets ……………………………………………. 15
3 Descriptive statistics - as-is phase of water closets ………………………. 17
4 T-test - measured data vs. standard (3.5gpf) ……………………………… 17
5 Descriptive statistics - plug and balloon methods …………………………21
6 T-test - plug vs. balloon methods …………………………………………. 22
7 Descriptive statistics - tune-up phase of water closets …………………….23
8 T-test - measured data vs. standard (4.5gpf) ……………………………… 23
9 Descriptive statistics - water meter ……………………………………….. 25
10 T-test - water meter vs. measured data …………………………………… 25
11 Coefficients - water meter vs. measured data ……….……………………. 27
12 Model summary - water meter vs. measured data ………………………... 27
13 ANOVA table - water meter vs. measured data …….……………………. 28
14 Bonferroni test - with and without methods in water meter ………………. 28
15 Descriptive statistics - low-manual phase of water closets ………………..30
16 T-test - measured data vs. standard (1.6gpf) ……………………………… 30
17 Descriptive statistics - water meter ……………………………………….. 32
18 T-test - water meter vs. measured data …………………………………… 32
19 Coefficients - water meter vs. measured data …………………………….. 34
20 Model summary - water meter vs. measured data ………………………… 34
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TABLE Page
21 ANOVA table - water meter vs. measured data ………………………….. 35
22 T-test - with and without methods in water meter ………………………... 35
23 Coefficients - water meter vs. measured data …………………………….. 38
24 Model summary - water meter vs. measured data ………………………... 38
25 ANOVA table - water meter vs. measured data ………………………….. 38
26 Normality test - water meter vs. measured data …………………………... 39
27 Descriptive statistics - low-auto phase of water closets …………………...40
28 T-test - measured data vs. standard (1.6gpf) ……….………………….….. 40
29 As-is vs. comparative values of other phases in water closets …………… 42
30 Bonferroni test - water closets ……………………………………………. 43
31 The standard vs. measured means in water closets …………………….…. 44
32 Coefficient of variance in water closets …………………………………... 45
33 Collected data in urinals …………………………………………………...46
34 Descriptive statistics - as-is phase of urinals ……………………………... 47
35 Descriptive statistics - measured data (balloon method ) ………………… 49
36 T-Test - measured data (balloon method) vs. standard (1.5gpf) …….……. 50
37 Descriptive statistics - tune-up phase of urinals (plug method) ………….. 53
38 Descriptive statistics - tune-up phase of urinals (balloon method) ……….. 53
39 T-Test - measured data (balloon method) vs. standard (1.5gpf) ……….…. 54
40 Coefficients - balloon vs. plug methods ……………….…………………. 57
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TABLE Page
41 Model summary - balloon vs. plug methods ……………………………… 57
42 ANOVA table - balloon vs. plug methods …………….………………….. 58
43 Normality test - balloon vs. plug methods ………………………………... 58
44 Descriptive statistics - water meter with balloon method ………………… 59
45 Paired T-test - water meter vs. measured data (balloon method) ….……... 60
46 Coefficients - water meter vs. measured data (balloon method) …………. 62
47 Model summary - water meter vs. measured data (balloon method) …….. 62
48 ANOVA table - water meter vs. measured data (balloon method) ……….. 62
49 Bonferroni test - with and without methods in water meter ……………… 63
50 Descriptive statistics - low-manual phase of urinals ………………………65
51 T-test - measured data vs. standard (1.0gpf) ………………………….…... 65
52 Descriptive statistics - water meter ……………………………………….. 67
53 Paired T-test - water meter vs. measured data ….………………………… 67
54 Coefficients - water meter vs. measured data …………………………….. 69
55 Model summary - water meter vs. measured data ………………………... 69
56 ANOVA table - water meter vs. measured data ………………………….. 70
57 T-test - with and without methods in water meter ………………………... 70
58 Coefficients - water meter vs. measured data …………………………….. 73
59 Model summary - water meter vs. measured data ………………………... 73
60 ANOVA table - water meter vs. measured data ………………………….. 73
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TABLE Page
61 Normality test - water meter vs. measured data ………………………….. 74
62 Descriptive statistics - low-automatic phase of urinals ……………………75
63 T-test - measured data vs. standard (1.0gpf) ……….………………….….. 75
64 As-is vs. comparative values of other phases in urinals ………………….. 77
65 Bonferroni test - urinals …………………………………………………... 78
66 The standard vs. measured means in urinals ……………………… ……... 79
67 Coefficient of variance in urinals …………………………………………. 80
68 The standards vs. actual water-volumes ………………………………….. 81
69 The experiment result of the actual water-volumes (gpf) ………………… 82
70 As-is vs. comparative values of other phases …………………………….. 83
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INTRODUCTION
BACKGROUND
At the start of the new millennium, the world is faced with the certain realization that,
through unsustainable population growth, economic expansion and rising per capita
consumption, humanity is finally reaching the limits of renewable water resources
(International Union for Conservation of Nature and Natural Resources, 2000). To
overcome this water crisis and save water resources, some positive developments have
been achieved in the construction industry. Water-efficient plumbing fixtures, such as
low-flow toilets and showerheads, first became generally available to American
consumers in the late 1980s. Subsequently, under the Energy Policy Act of 1992, the
Congress established uniform national standards for the manufacture of these fixtures to
promote conservation by residential and commercial water users. Consequently, all
water-efficient plumbing fixtures must meet the standards for the maximum water
consumption (United States General Accounting Office [USGAO], 2000).
Some studies have been conducted to measure water savings of water-efficient fixtures.
However, most of the results show only the average values and ratios without
considering the types of valve or the kinds of buildings. Furthermore, the results of some
_______________________ This thesis follows the style and format of the Journal of Construction Education.
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studies can be unreliable because the actual volume of water used by flushing sometimes
varies from the manufacturer’s reported flow rate (Vickers, 2001). Therefore, this study
will analyze the water savings from retrofitting water closets and urinals with precise
measurements, and evaluate the cost-effectiveness of applying low-consumption fixtures
depending on the types of valves in a university building.
Facility Water Management
Facility managers are being forced to find new ways and means of reducing their
operational costs due to increased pressure being exerted by top management for
organization-wide cost reductions (Lewis, 2000). New technologies and approaches to
design of building systems are making significant cost reduction possible. Such capital-
improvement projects can deliver a satisfying payback and return on investment (Clarke,
1996). In facility water management, the time comes when the manager decides it is
time to upgrade the system. The decision should be a logical one, driven by the life of
the system and the scheduled replacement time of the system’s component. Water
conservation can be accomplished when upgrading by installing low-flow or ultra-low-
flow toilets, low-flow urinals, and other water-saving equipment (Reid, 1996). Finally,
the result of this study will present practical standards of low-consumption fixtures to
facility managers and other building professionals and contribute to determining the
availability of retrofitting water closets and urinals.
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PURPOSE AND SCOPE
The purpose of this study is to analyze the cost-effectiveness of water savings from
retrofitting water closets and urinals in restrooms of the Langford Architecture building
A at Texas A&M University.
Objectives
• To measure the actual water consumptions of as-is, tune-up, low-consumption
manual, and low-consumption automatic water closets and urinals applied to the
restrooms of the Langford Architecture building A
• To analyze the cost-effectiveness of water savings from retrofitting water closets and
urinals with low-consumption fixtures.
Limitations
This study is limited to water closets and urinals in the restrooms of the Langford
Architecture building A at Texas A&M University. The building has four floors with
rooftop offices and a basement.
Assumptions
• Only the water-volume per flush is the determining factor in water consumption of
water closets and urinals—other conditions are equivalent.
• The water-volume per flush is subject to the types of valves in the water closets and
urinals.
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LITERATURE REVIEW
Increasing Environmental Awareness
Changing public attitudes regarding water issues notwithstanding, communities will
probably have to contend with an increasing demand from their citizens for
environmentally responsible action. A recent public opinion survey in Boulder,
Colorado—a community noted for its strong environmental ethic—indicated that 78% of
those responding were interested in water efficiency primarily because they believed
wise use of the resource was important. Understanding people’s increasing
environmental values and concerns can help managers and planners gain support for
implementing water efficiency program (Rocky Mountain Institute, 1991).
Improvement in Low-volume Fixtures
Improvements in water efficiency of toilets began in early 1980s as a result of
refinements in the design of conventional gravity toilets, the introduction of new
technologies and fixture designs, and local, state, and federal initiatives to promote water
conservation. Although some of the early “low-flow” fixtures in the United States in the
late 1980s received mixed reviews in terms of performance, manufactures have
improved the design and performance of low-volume toilets so that consumers can now
choose from a large number of reliable products (Vickers, 2001).
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Regulations; The Energy Policy Act of 1992
The Energy Policy Act of 1992 established water conservation standards for the
manufacture of four types of plumbing fixtures: toilets, kitchen and lavatory faucets,
showerheads, and urinals. With limited exceptions, the standards apply to all models of
the fixtures manufactured after January 1, 1994. (see Table 1).
Table 1
National water efficiency standards (Vickers, 2001) Fixture type Maximum allowable water use
Toilets, including gravity tank-type toilets, flushometer tank toilets, and electromechanical hydraulic toilets
1.6 gallons per flush (gpf)
Urinals 1.0 gallon per flush (gpf)
Under the Department of Energy’s regulations, water-efficient plumbing fixtures must
meet the standards for maximum water consumption. For each model of a regulated
plumbing fixture, manufacturers and private labelers must submit a compliance
statement to the Department to certify that the model complies with the applicable water
conservation standard and that all required testing has been conducted according to the
test requirements prescribed in the regulations (USGAO, 2000).
Low-consumption Water Closets
Low-volume toilets, also referred to by the terms low-flow, low-flush, low-consumption,
ultralow-flush, and ultralow-volume, typically use 1.6 gallons per flush (gpf) or less.
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Low-volume toilets are available in the same operating designs as high-volume fixtures.
Similarly, Low-volume toilets can be either floor- or wall-mounted and are available in a
range of styles, sizes, and colors. Low-volume toilets can be installed to replace high-
volume toilets in residential and nonresidential settings, with a few exceptions. Three
basic types of low-volume toilets are commonly available, along with several alternative
ultra-efficient designs.
In a office, replacing a 3.5 gpf toilets with a 1.6 gpf fixture will save an estimated 1.9
gallons per capita per day (gpcd) for males and 5.7 gpcd for females, the equivalent of
annual water savings of 494 gallons per capita per day (gpcy), respectively. A study of
more 200 gpf pressurized-tank toilets that replaced high-volume (2.5 gpf and higher)
fixtures in a variety of commercial properties in two California communities, the city of
Petaluma and Rohnert Park, Found that the average savings per toilet was 26 gallons per
day (gpd) (Vickers, 2001).
Low-consumption Urinals
Low-volume, flushometer-valve urinals that use 1.0 gpf or less can be installed to
replace high-volume, flush-valve fixtures, often with no modifications to the bowl or to
wall or floor connections. In some cases only the flush valve needs to be replaced to
lower the flow rate to 1.0 gpf. Low-volume, flush-valve urinals operate the same way as
high-volume, flush-valve urinals and toilets, except that the diaphragm orifice in the
valve has a smaller diameter. Installation of low-volumes, flush-valve urinals to replace
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other types of high-volume requires removal of the old fixture and flushing apparatus
and installation of an entirely new fixture and valve.
Water use by urinals in office restrooms for males is estimated to be about 2.0 gpcd
when a 1.0 gpf fixture is installed and 3.0 to 9.0 gpcd when high-volume fixture are in
use. Water use by toilets is also a factor in office restrooms for males. The frequency of
urinal flushing by males in office lavatories is estimated to be about two times per
workday (Vickers, 2001).
Water Flow Meter
All flow meters work on the basic principles of fluid mechanics. A type of common
meter utilized in facility water system is the disk meter. A disk meter more accurately
measures flows by using a flat disk that sits in the meter housing on an angle to the flow.
As the water passes through the meter, the disk turns, similar to the propeller. The
turning disk is geared to a clock face and the gears are designed to provide numbers that
correspond directly to the number of gallons used (Reid, 1996).
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EXPERIMENT METHOD
Fixtures in Restrooms
The experiment was conducted on water closets and urinals in restrooms of the Langford
Architecture building A at Texas A&M University. The building has a men’s and
women’s restroom on each of the four floors. There are two water closets in each men’s
room and four water closets in each women’s room for a total of twenty-four water
closets in the building. Each men’s restroom has three urinals for a total of twelve in the
building.
The fixtures were named m for those in the men’s restrooms and w for those in the
women’s restrooms. Water closets are w and urinals are u. The fixtures are numbered
clockwise in each restroom. A number prefix was used to indicate the floor. The fixture
2mw1 identifies the fixture as being on the second floor, men’s restroom, and water
closet number one. Figure 1 shows the men’s restroom layout in the building. Figure 2
shows the women’s restroom layout (Parker, 2002).
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2
13 2 1
Figure 1: Men’s restroom layout in the building (Parker, 2002)
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214
Figure 2: Women’s restroom layout in the building (Parker, 2002)
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Water Closets and Urinals
The researcher conducted a pilot test on as-is status, and measured the water-volume per
flush of tune-up, low-consumption manual, and low-consumption automatic water
closets and urinals with retrofitting. In the as-is phase, there were originally twenty-four
water closets (3.5 gpf) and twelve urinals (1.6 gpf). Figure 3 shows photos of a water
closet fixture and a urinal fixture in the as-is phase in the building. These fixtures were a
kind of flushometer-valve toilets—a tankless toilet with the flush valve attached to a
pressurized water supply pipe (see Appendix A).
Figure 3: Water closet and urinal in the as-is phase
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After the as-is phase experiment, in tune-up phase the original valves of water closets
and urinals were replaced partly with new diaphragms, handles, and vacuum breakers
(see Figure 4). However, chinas and other plumbing systems had the same status as the
as-is phase. Finally, the standard of the water closets was replaced to 4.5 gpf, but urinals’
were the same 1.6 gpf as in the as-is phase.
Figure 4: Valve in the tune-up phase
After the tune-up phase, low-consumption valves and chinas were installed, but other
plumbing systems had the same status as before. Figure 5 and 6 show water closet and
urinal fixtures in the low-manual and low automatic phases. They were also a kind of
flushometer-valve toilets, and the standards of the water closets and urinals were
replaced to 1.6 and 1.0 gpf.
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Figure 5: Water closet and urinal in the low-manual phase
Figure 6: Water closet and urinal in the low-automatic phase
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13
Measurement Methods
A plug or balloon was used to stop up the waterway of the fixtures. After flushing with
stopping up the waterway, the researcher measured directly the actual water-volume per
flush (gpf) and repeated this over five times on each for all fixtures on each phase (see
Figure 7).
Figure 7: Measurement methods
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14
Water Flow Meter
After a pilot test on as-is phase, a water-flow meter, Rosemont 8705, was installed to
obtain reliable data in the basement of the Langford Architecture building A (see Figure
8). The water meter was read before and after flushing the water closets and urinals
while keeping all other fixtures and water appliances turned off.
Figure 8: Water meter in the basement
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15
RESULTS OF WATER CLOSETS
The researcher conducted a pilot test on water closets in the as-is status, and then
measured the water-volume per flush of the tune-up, low-consumption manual, and low-
consumption automatic water closets with retrofitting. The researcher repeated the
observations with the plug or balloon measurement method for each water closet fixture
in restrooms of the Langford Architecture building A at Texas A&M University. The
collected data in the water closets is categorized in Table 2 by measurement methods
and phases.
Table 2
Collected data in water closets
Water Closet (24 EA)
Old water closet fixtures (china and valve)
New water closet fixtures (china and valve)
Pilot Test (As-is) Tune-up Low-Manual Low-Auto
Phase (Valve
type)
Measurement (3.5 gpf) (4.5 gpf) (1.6 gpf) (1.6 gpf)
Plug 10 times for each of all fixtures
5 times for each of all fixtures
Balloon No data 5 times for each of all fixtures
5 times for each of all fixtures with plug or balloon
10 times for each of selected 8 fixtures with plug or balloon
5 times for each of all fixtures with plug
5 times for each of all fixtures with balloon
5 times for each of all fixtures with plug or balloon
10 times for each of selected 8 fixtures with plug or balloon Water-flow
Meter No data
5 times for each of all fixtures without measurement
5 times for each of all fixtures without measurement
10 times for each of selected 16 fixtures without measurement
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16
PILOT TEST:AS-IS PHASE OF WATER CLOSETS
First, the researcher conducted a pilot test on the water closets (02/08/2002~02/28/2002,
04/18/2002~05/08/2002).
a. The experimental objects were made up of twenty-four water closets (3.5 gpf) in an
unmodified condition (as-is). The researcher directly measured the actual water-volume
per flush with plug method, and repeated this ten times for all the fixtures in the
restrooms of the Langford Architecture building A.
b. Three water closets were different shapes, and they were not able to be measured
correctly: 1ww3, 2ww1, and 4ww2. Therefore, those values were removed on the pilot
test.
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17
Findings in the Pilot Test: As-is Phase
a. The measured mean, 3.305 gpf, was less than the standard 3.5 gpf (see Table 3).
Moreover, statistically, there was a significant difference between the mean and the
standard. To compare them, a one sample T-test was conducted:
H : μ as-is = 3.5 gpf, o
H : μ as-is 3.5 gpf. a ≠
The null hypothesis was rejected because p-value (.005) < .05 (see Table 4).
Table 3
Descriptive statistics - as-is phase of water closets
3.30503.44831.051
1.024991.454.873.42
MeanMedianVarianceStd. DeviationMinimumMaximumRange
ASIS_WCStatistic
Table 4
T-test - measured data vs. standard (3.5 gpf)
-2.808 209 .005 -.1950 -.3320 -.0581As-is WC
t dfSig.
(2-tailed)Mean
Difference Lower Upper
95% ConfidenceInterval of the
Difference
Test Value = 3.5
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18
1mw11mw2
1ww1
1ww21ww4
2mw1
2mw22ww2
2ww3
2ww43mw1
3mw2
3ww13ww2
3ww3
3ww44mw1
4mw2
4ww14ww3
4ww4
fixtures
2.00
3.00
4.00
5.00
gpf
AAAAAAAAAA
AAA
AAAAAAA
AAAAAAAAAA
AAAAAAAA
AA
AAAAAAAAAA
AAAA
A
A
AAAA
AAAAAA
AAA
A
AAAAAAAAAA AA
AAAA
AA
AA
AAAAAAAAAA
AAAAAAAAAA
AAAAAAAAAA A
AAAAAAAAA
AAAAAAAAAA
AAAAAAAAAA
AAAA
AAAAA
A
AAAAAAAAAA
AAAAAAAA
A
A
AAAAAAAAAA
AAAA
AAAAAA
AAAAAAAAAA
Figure 9: Scatter plot - measured data (plug method)
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19
b. The values between fixtures had considerable differences—standard deviation and
range were significant (see Table 3 and Figure 9). To define another measure of
variability, coefficient of variation (CV) was applied. The coefficient of variation (CV)
measures the variability in the values in a population relative to the magnitude of the
population mean. Thus, the CV is the standard deviation of the population expressed in
units of μ.
Coefficient of variation (CV) of as-is phase was 31.013 %:
CV = 100 ( s / ⎟ y ⎢)% = 100 (1.0250 / 3.3050)%. The result was assumed because
original fixtures had not been on a timely management service.
c. After the as-is phase, a water-flow meter, Rosemont 8705, was installed to obtain
reliable data in the basement of the Langford Architecture building A.
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20
TUNE-UP PHASE OF WATER CLOSETS
Second, the researcher collected data on the tune-up phase of the water closets
(09/26/2002~10/09/2002).
a. New diaphragms, handles, and vacuum breakers were installed in the original valves
of all water closets. However, chinas and other plumbing systems had the same status as
the as-is phase. Finally, the standard of the water closets was replaced to 4.5 gpf.
b. The researcher measured directly the actual water-volume per flush with plug and
balloon methods and repeated it five times for all twenty-four fixtures. At the same time,
the water meter was read.
c. Additionally, the water meter was read five times for all twenty-four fixtures, when
the plug or balloon method was not applied to china, to analyze whether the methods
were effective in measuring meter values.
d. Three water closets had different shapes, and they were difficult to measure correctly:
1ww3, 2ww1, and 4ww2. Therefore, the values were also removed on tune-up phase.
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21
Findings in Tune-up Phase
a. Plug and balloon measurement methods had similar means, standard deviations, and
similar graphs (see Table 5 and Figure 10). Moreover, statistically, there was no
significant difference between the measurement methods of plug and balloon in the tune-
up phase of the water closets. A paired T-test was conducted:
H : μ plug = μ balloon, o
H : μ plug μ balloon. a ≠
The null hypothesis was accepted because p-value (.219) > .05 (see Table 6). Therefore,
both plug and balloon methods were reliable, and there was no need to distinguish
between them.
Table 5
Descriptive statistics - plug and balloon methods
4.15214.4014
.407.63799
2.785.272.49
4.19494.2275
.389.62334
2.785.292.51
MeanMedianVarianceStd. DeviationMinimumMaximumRangeMeanMedianVarianceStd. DeviationMinimumMaximumRange
PLUG
BALLOON
Statistic
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22
2.50
3.00
3.50
4.00
4.50
5.00
5.50
1mw1
1mw2
1ww1
1ww2
1ww4
2mw1
2mw2
2ww2
2ww3
2ww4
3mw1
3mw2
3ww1
3ww2
3ww3
3ww4
4mw1
4mw2
4ww1
4ww3
4ww4
gpf
fixtures balloon plug
Figure 10: Graph - balloon vs. plug methods
Table 6
T-test - plug vs. balloon methods
-.0429 .15481 .03378 -.1133 .0276 -1.269 20 .219PLUG_TUN -BALL_TUN
MeanStd.
DeviationStd. Error
Mean Lower Upper
95% ConfidenceInterval of the
Difference
Paired Differences
t dfSig.
(2-tailed)
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23
b. The mean, 4.17 gpf, in the tune-up phase of the water closets was less than the
standard 4.5 gpf (see Table 7). Moreover, statistically, there was a significant difference
between the mean and the standard. To compare them, a one sample T-test was
conducted:
H : μ tune-up = 4.5 gpf, o
H : μ tune-up 4.5 gpf. a ≠
The null hypothesis was rejected because p-value (.000) < .05 (see Table 8).
Table 7
Descriptive statistics - tune-up phase of water closets
4.17354.2864
.392.62595
2.785.282.50
MeanMedianVarianceStd. DeviationMinimumMaximumRange
TuneupStatistic
Table 8
T-test - measured data vs. standard (4.5 gpf)
-7.592 209 .000 -.3265 -.4113 -.2417Tune-up WC
t df Sig. (2-tailed)Mean
Difference Lower Upper
95% ConfidenceInterval of the
Difference
Test Value = 4.5
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24
c. Figure 11 shows that the difference between fixtures is less than in the as-is phase. It
is assumed that this is due to the original fixtures receiving a tune-up. Coefficient of
variation (CV) of tune-up phase was 14.999 %:
CV = 100 ( s / ⎟ y ⎢)% = 100 (0.6260 / 4.1735)%. It was quite less than the as-is phase,
31.013 %.
1mw11mw2
1ww1
1ww21ww4
2mw1
2mw22ww2
2ww3
2ww43mw1
3mw2
3ww13ww2
3ww3
3ww44mw1
4mw2
4ww14ww3
4ww4
fixture
3.00
4.00
5.00
gpf
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA
A
AA
A
A
AAAAA
A
AAAA
A
AAAA
A
AAAA
AAAA
A
AAAAA
A
AAA
A
A
AAA
A
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA
AAAA
A
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA AAAA
A
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA
AAAAA
A
AAAA
AAAAA
AAAAA
AAAAA
AAAAA
Figure 11: Scatter plot - measured data
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25
d. The mean of the water meter (4.034 gpf) was less than the directly measured means
(4.17 gpf) with plug and balloon methods because the water meter was not sensitive to
small water volume (see Table 7 and 9). A paired T-test was conducted:
H : μ meter = μ measure, o
H : μ meter μ measure. a ≠
The null hypothesis was rejected because p-value (.000) < .05 (see Table 10). Therefore,
the water meter was not appropriate as a measurement method.
Table 9
Descriptive statistics - water meter
4.03434.2300
.423.65019
2.525.102.58
MeanMedianVarianceStd. DeviationMinimumMaximumRange
METERStatistic
Table 10
T-test - water meter vs. measured data
-.1399 .15613 .02409 -.1886 -.0913 -5.808 41 .000METER -MEASURE
MeanStd.
DeviationStd. Error
Mean Lower Upper
95% ConfidenceInterval of the
Difference
Paired Differences
t dfSig.
(2-tailed)
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26
e. However, the water meter was reliable in measuring the water-volume per flush.
Figure 12 shows that the water meter and directly measured values in the tune-up phase
have similar graphs. The meter values and the measured values are moving together in a
constant rate. Moreover, a regression model showed that they had a relationship (see
Figure 13 and Table 11). The regression model had a high R-square and the test results
were acceptable (see Table 12 and 13).
2.40
2.80
3.20
3.60
4.00
4.40
4.80
5.20
1mw1
1mw2
1ww1
1ww2
1ww4
2mw1
2mw2
2ww2
2ww3
2ww4
3mw1
3mw2
3ww1
3ww2
3ww3
3ww4
4mw1
4mw2
4ww1
4ww3
4ww4
fixture
gpf
meter measured
Figure 12: Graph - water meter vs. measured data
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27
Linear Regression
3.00 4.00 5.00
water meter
3.00
3.50
4.00
4.50
5.00
mea sure d va lue s in tune -up
A
A
A
A
A
A
A
A
A
A
A
A
A
A
A
A
A
A
A
A
A
measure = 0.38 + 0.94 * meterR-Square = 0.96
Figure 13:Scatter plot - water meter vs. measured data
Table 11
Coefficients - water meter vs. measured data
.376 .189 1.991 .061
.941 .046 .978 20.337 .000
(Constant)METER
Model1
B Std. Error
UnstandardizedCoefficients
Beta
StandardizedCoefficients
t Sig.
Table 12
Model summary - water meter vs. measured data
.978a .956 .954 .13459Model1
R R SquareAdjustedR Square
Std. Error ofthe Estimate
Predictors: (Constant), METERa.
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Table 13
ANOVA table - water meter vs. measured data
7.491 1 7.491 413.578 .000a
.344 19 .0187.835 20
RegressionResidualTotal
Model1
Sum ofSquares df Mean Square F Sig.
Predictors: (Constant), METERa.
f. There was no difference between results with and without measurement methods in
the water meter. Therefore, the test with plug or balloon method had no effect on the
value of the water meter. To prove it, a Bonferroni test was conducted:
H : μ meter only = μ meter with plug = μ meter with balloon, o
H : at least one of the means differs from rest. a
The null hypothesis was accepted (see Table 14).
Table 14
Bonferroni test - with and without methods in water meter Dependent Variable: MET_VALU
-.0021 .20247 1.000 -.5008 .4966-.0085 .20247 1.000 -.5071 .4902.0021 .20247 1.000 -.4966 .5008
-.0064 .20247 1.000 -.5051 .4923.0085 .20247 1.000 -.4902 .5071.0064 .20247 1.000 -.4923 .5051
(J)2.003.001.003.001.002.00
(I)1.00
2.00
3.00
Bonferroni
MeanDifference
(I-J)Std.Error Sig. Lower Bound Upper Bound
95% Confidence Interval
1: meter only, 2: meter with plug, 3: meter with balloon
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29
LOW-MANUAL PHASE OF WATER CLOSETS
Third, the researcher collected data on the low-manual phase of water closets
(10/14/2002~10/27/2002).
a. New low-consumption manual valves and chinas were installed in the restrooms of the
Langford Architecture building A. However, other plumbing systems had the same
status as before. They all had the same shape of china and the same type of valves, and
the standard of the water closets was 1.6 gpf.
b. The researcher measured the actual water-volume per flush with plug or balloon
methods and repeated it five times for all twenty-four fixtures. At the same time, the
water meter was read.
c. Additionally, the water meter was read five times for all twenty-four fixtures, when
the measurement method was not applied to china, in order to analyze whether the
method was effective in measuring meter values.
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Findings in Low-manual Phase
a. The mean, 1.599 gpf, in the low-manual phase of the water closets was same as the
standard 1.6 gpf (see Table 15). Statistically, there was no significant difference between
the mean and the standard. To compare them, a one sample T-test was conducted:
H : μ low-manual = 1.6 gpf, o
H : μ low-manual 1.6 gpf. a ≠
The null hypothesis was accepted because p-value (.962) > .05 (see Table 16).
Table 15
Descriptive statistics - low-manual phase of water closets
1.59901.5657
.053.22959
.941.961.02
MeanMedianVarianceStd. DeviationMinimumMaximumRange
LowManual_WC
Statistic
Table 16
T-test - measured data vs. standard (1.6 gpf)
-.047 119 .962 -.0010 -.0424 .0404Low-manualWC
t df Sig. (2-tailed)Mean
Difference Lower Upper
95% ConfidenceInterval of the
Difference
Test Value = 1.6
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b. 2ww1 had considerable difference from the others (see Figure 14). However,
coefficient of variation, 14.358 %, was less than the as-is and tune-up phases:
CV = 100 ( s / ⎟ y ⎢)% = 100 (0.2296 / 1.5990)%.
1m
w1
1m
w2
1w
w1
1w
w2
1w
w3
1w
w4
2m
w1
2m
w2
2w
w1
2w
w2
2w
w3
2w
w4
3m
w1
3m
w2
3w
w1
3w
w2
3w
w3
3w
w4
4m
w1
4m
w2
4w
w1
4w
w2
4w
w3
4w
w4
fixture
1.00
1.25
1.50
1.75
2.00
gpf AAA
AA
A
A
A
A
A
A
A
AAA
A
AAAA
A
A
AAAA
AAAA
A
AAAA A
AA
AA
AAAAA
AAAAA
AA
A
AA
AAAA
A
A
AA
A
A
AA
A
A
A
A
AA
AA
AAAAA
AAAAA
AAAAA
A
A
AAA
A
AAAA
AAAAA
A
AA
A
A
AAAAA A
AAAA
Figure 14: Scatter plot - measured data
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c. The mean of the water meter (1.404 gpf) was less than the directly measured mean
(1.599 gpf) with plug and balloon methods because the water meter was not sensitive to
small water volume —It is the same result as the tune-up phase (see Table 17). A paired
T-test was conducted:
H : μ meter = μ measure, o
H : μ meter μ measure. a ≠
The null hypothesis was rejected because p-value (.000) < .05 (see Table 18). Therefore,
the water meter was not appropriate as a measurement method.
Table 17
Descriptive statistics - water meter
1.40381.3990
.048.21874
.701.711.01
MeanMedianVarianceStd. DeviationMinimumMaximumRange
METERStatistic
Table 18
T-test - water meter vs. measured data
-.1952 .07449 .01520 -.2266 -.1637 -12.84 23 .000METER -MEASURED
MeanStd.
DeviationStd. Error
Mean Lower Upper
95% ConfidenceInterval of the
Difference
Paired Differences
t dfSig.
(2-tailed)
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d. However, the water meter was reliable in measuring the water-volume per flush.
Figure 15 shows that the water meter and directly measured values in the low-manual
phase have similar graphs—It is same result as the tune-up phase. The meter values and
the measured values are moving together in a constant rate. Moreover, a regression
model showed that they had a relationship (see Figure 16 and Table 19). The regression
model had a high R-square and the test results were acceptable (see Table 20 and 21)
0.60
0.80
1.00
1.20
1.40
1.60
1.80
2.00
1mw1
1mw2
1ww1
1ww2
1ww3
1ww4
2mw1
2mw2
2ww1
2ww2
2ww3
2ww4
3mw1
3mw2
3ww1
3ww2
3ww3
3ww4
4mw1
4mw2
4ww1
4ww2
4ww3
4ww4
fixture
gpf
meter measure
Figure 15: Graph - water meter vs. measured data
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34
Linear Regression
0.80 1.00 1.20 1.40 1.60
water meter
1.00
1.20
1.40
1.60
1.80
mea su red in low
-manua l
A
AA
A
AA
AA
A
A
A
A
A
A
A
A
AA
A
A
A
A
A
Ameasure = 0.21 + 0.99 * meterR-Square = 0.89
Figure 16: Scatter plot - water meter vs. measured data
Table 19
Coefficients - water meter vs. measured data
.205 .103 1.991 .059
.993 .073 .946 13.679 .000
(Constant)METER
Model1
B Std. Error
UnstandardizedCoefficients
Beta
StandardizedCoefficients
t Sig.
Table 20
Model summary - water meter vs. measured data
.946a .895 .890 .07614Model1
R R SquareAdjustedR Square
Std. Error ofthe Estimate
Predictors: (Constant), METERa.
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35
Table 21
ANOVA table - water meter vs. measured data
1.085 1 1.085 187.113 .000a
.128 22 .0061.212 23
RegressionResidualTotal
Model1
Sum ofSquares df Mean Square F Sig.
Predictors: (Constant), METERa.
e. There was no difference between results with and without measurement methods in
the water meter. Accordingly, the test with plug or balloon method has no effect on the
value of the water meter—same result as the tune-up phase.
A paired T-test was conducted:
H : μ meter only = μ meter with measurement, o
H : μmeter only μmeter with measurement. a ≠
The null hypothesis was accepted because p-value (.085) > .05 (see Table 22).
Table 22
T-test - with and without methods in water meter
-.0157 .04262 .00870 -.0337 .0023 -2 23 .085Meter only - with measurement
MeanStd.
Deviation
Std.ErrorMean Lower Upper
95% ConfidenceInterval of the
Difference
Paired Differences
t dfSig.
(2-tailed)
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36
LOW-AUTOMATIC PHASE OF WATER CLOSETS
Fourth, the researcher collected data on the low-automatic phase of water closets
(11/11/2002~11/26/2002).
a. New low-consumption automatic valves were installed on the chinas in the low-
manual phase instead of low-consumption manual valves. However, chinas and other
plumbing systems had the same status as the low-manual phase. They all had the same
shape of china and the same type of valves, and the standard of the water closets was 1.6
gpf.
b. The researcher measured the actual water-volume per flush with plug or balloon
methods and repeated it ten times for randomly selected eight fixtures. At the same time,
the water meter was read.
c. The water meter was read ten times for each of the sixteen fixtures that were not
directly measured, when plug or balloon method was not applied to china, in order to
predict directly measured values.
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37
Findings in Low-automatic Phase
a. It was proven that there was a relationship between the water meter and measured
values in the tune-up and low-manual phases. To predict the actual water-volume values
of the sixteen fixtures that were not measured directly, the researcher conducted a
regression between the directly measured eight fixtures and the water meter.
The regression model was
Measure low-auto = Bo + B1 Meter low-auto
= 0.415 + .921 * Meter low-auto (see Figure 17 and Table 23).
Linear Regression
1.20 1.40 1.60 1.80 2.00
meter
1.60
1.80
2.00
2.20Mea su red values in low
-au to o f WC
A A AAA
AA
A
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A
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AA AAAAA
A
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AA AA
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AA A
AA AA AAA
AA
A
AAAAA AA
AA
A
AAAA AAA
AAAAA AAAAA
measured = 0.42 + 0.92 * meterR-Square = 0.94
Figure 17: Scatter plot - water meter vs. measured data
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38
Table 23
Coefficients - water meter vs. measured data
.415 .045 9.237 .000
.921 .027 .969 34.495 .000
(Constant)METER
Model1
B Std. Error
UnstandardizedCoefficients
Beta
StandardizedCoefficients
t Sig.
Table 24
Model summary - water meter vs. measured data
.969a .938 .938 .05965Model1
R R SquareAdjustedR Square
Std. Error ofthe Estimate
Predictors: (Constant), METERa.
Table 25
ANOVA table - water meter vs. measured data
4.234 1 4.234 1189.918 .000a
.278 78 .0044.511 79
RegressionResidualTotal
Model1
Sum ofSquares df Mean Square F Sig.
Predictors: (Constant), METERa.
The regression model had a high R-square and the test results were acceptable (see Table
24 and 25). Residual was also normally distributed (Figure 18 and Table 26).
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39
Regression Standardized Residual
2.251.75
1.25.75.25-.25
-.75-1.25
-1.75-2.25
-2.75
Dependent Variable: MEASURE
Fre
quency
12
10
8
6
4
2
0
Std. Dev = .99 Mean = 0.00
N = 80.00
Figure 18: Residual histogram - water meter vs. measured data
Table 26
Normality test - water meter vs. measured data
.090 80 .162 .985 80 .487StandardizedResidual
Statistic df Sig. Statistic df Sig.Kolmogorov-Smirnova Shapiro-Wilk
Lilliefors Significance Correctiona.
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40
b. The measured mean, 1.98 gpf, in the low-automatic phase of water closets was more
than the standard 1.6 gpf (see Table 27). Moreover, there was a significant difference
between the mean and the standard. A one sample T-test was conducted:
H : μ low-auto = 1.6 gpf, o
H : μ low-auto 1.6 gpf. a ≠
The null hypothesis was rejected because p-value (.000) < .05 (see Table 28).
Table 27
Descriptive statistics - low-automatic phase of water closets
1.98022.0512
.066.25768
1.522.37.85
MeanMedianVarianceStd. DeviationMinimumMaximumRange
LOW_AUTOStatistic
Table 28
T-test - measured data vs. standard (1.6 gpf)
22.994 239 .000 .3802 .3476 .4128Low-autoWC
t df Sig. (2-tailed)Mean
Difference Lower Upper
95% ConfidenceInterval of the
Difference
Test Value = 1.6
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41
c. Figure 19 shows that the difference between the fixtures is less significant than in
other phases. Coefficient of variation, 13.014 %, was the lowest value in the water closet
phases: CV = 100 ( s / ⎟ y ⎢)% = 100 (0.2577 / 1.980)%.
1m
w1
1m
w2
1w
w1
1w
w2
1w
w3
1w
w4
2m
w1
2m
w2
2w
w1
2w
w2
2w
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w4
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3m
w2
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4m
w1
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w2
4w
w1
4w
w2
4w
w3
4w
w4
fixture
1.60
1.80
2.00
2.20
2.40
gpf
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A
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A
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AAAAA
A
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A
Figure 19: Scatter plot - measured data
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42
SUMMARY OF WATER CLOSETS
a. The researcher compared the water-volume per flush of all phases in the water closets.
Figure 20 shows the means in the water closets. The result of the mean values is
Tune-up (4.174 gpf) > As-is (3.305 gpf) > Low-auto (1.980 gpf) > Low-manual (1.599 gpf).
Table 29 shows the comparative water-volume of other phases when it is assumed that
the mean of as-is phase is 100%.
3.305
4.174
1.5991.980
0.00
0.50
1.00
1.50
2.00
2.50
3.00
3.50
4.00
4.50
gpf
as-is(3.5gpf) tune-up(4.5gpf) low-manual(1.6gpf) low-auto(1.6gpf)
Figure 20: Graph - means in water closets
Table 29
As-is vs. comparative values of other phases in water closets Phase As-is Tune-up Low-manual Low-auto
Mean 3.305 gpf 4.174 gpf 1.599 gpf 1.980 gpf
Each / As-is (%) 100 % 126.29 % 48.381 % 59.91 %
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43
b. However, statistical analysis has a different result.
A Bonferroni test was conducted:
H : μ as-is = μ tune-up = μ low-manual = μ low-auto, o
H : at least one of the means differs from rest. a
The null hypothesis was rejected (see Table 30).
The result of statistics analysis is
Tune-up > As-is > Low-manual = Low-automatic.
Table 30
Bonferroni test - water closets Dependent Variable: VAR00002Bonferroni
-.8685* .18730 .000 -1.3744 -.36271.7059* .18135 .000 1.2162 2.19571.3244* .18135 .000 .8346 1.8142.8685* .18730 .000 .3627 1.3744
2.5745* .18135 .000 2.0847 3.06422.1929* .18135 .000 1.7032 2.6827
-1.7059* .18135 .000 -2.1957 -1.2162-2.5745* .18135 .000 -3.0642 -2.0847-.3815 .17520 .193 -.8547 .0916
-1.3244* .18135 .000 -1.8142 -.8346-2.1929* .18135 .000 -2.6827 -1.7032
.3815 .17520 .193 -.0916 .8547
(J)2.003.004.001.003.004.001.002.004.001.002.003.00
(I)1.00
2.00
3.00
4.00
MeanDifference
(I-J)Std.Error Sig. Lower Bound Upper Bound
95% Confidence Interval
The mean difference is significant at the .05 level.*.
1: As-is, 2: Tune-up, 3: Low-manual, 4:Low-automatic
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c. Most phases of the water closets have different actual water-volumes than the
standards (see Figure 21). The as-is, tune-up and low-automatic phases show significant
differences statistically between the standards and the actual water-volumes of flushing
(Table 31).
3.5
4.5
1.6 1.6
3.305
4.174
1.599
1.98
0.0
0.5
1.0
1.5
2.0
2.5
3.0
3.5
4.0
4.5
5.0
As-is Tune-up Low-manual Low-auto
gpf
Standard Mean
Figure 21: Graph - measured mean vs. standard in water closets
Table 31
The standard vs. measured means in water closets Phase As-is Tune-up Low-manual Low-auto
Mean 3.305 gpf 4.174 gpf 1.599 gpf 1.980 gpf
Standard 3.5 gpf 4.5 gpf 1.6 gpf 1.6 gpf
Mean / Std. (%) 94.43 % 92.76 % 99.94 % 123.75 %
Sig. (2-tailed) .005 .000 .962 .000
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45
d. There is a tendency in low-consumption fixtures to have a lower coefficient of
variance (CV). New fixtures in the low-manual and low-automatic phases have a low
CV, but old fixtures in the as-is phase have a high rate. The tune-up phase also has a low
rate (see Figure 22 and Table 32). It is assumed that the results are related to the
management status of the fixtures.
31.013
14.999 14.35813.014
0
5
10
15
20
25
30
35
as-is(3.5gpf) tune-up(4.5gpf) low-manual(1.6gpf) low-auto(1.6gpf)
(%)
Figure 22: Graph - coefficient of variance in water closets
Table 32
Coefficient of variance in water closets Phase As-is Tune-up Low-manual Low-auto
Std. Deviation 1.0245 0.6260 0.2296 0.2577
Mean 3.305 gpf 4.174 gpf 1.599 gpf 1.980 gpf
CV 31.013 % 14.999 % 14.358 % 13.014 %
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46
RESULTS OF URINALS
The researcher conducted a pilot test on urinals in the as-is status, and measured the
water-volume per flush of the tune-up, low-consumption manual, and low-consumption
automatic urinals with retrofitting. The researcher repeated the observations with the
plug or balloon measurement method for each urinal fixture in restrooms of the Langford
Architecture building A at Texas A&M University. The data collected in the urinals is
categorized in Table 33 by measurement methods and phases. Basically, the experiment
method and procedure for the urinals was similar to those of water closets.
Table 33
Collected data in urinals
Urinal (12 EA)
Old urinal fixtures (china and valve)
New urinal fixtures (china and valve)
Pilot Test (As-is) Tune-up Low-Manual Low-Auto
Phase (Valve
type)
Measurement (1.5 gpf) (1.5 gpf) (1.0 gpf) (1.0 gpf)
Plug 10 times for each of all fixtures
5 times for each of all fixtures
Balloon No data 5 times for each of all fixtures
5 times for each of all fixtures with plug or balloon
10 times for each of selected 4 fixtures with plug or balloon
5 times for each of all fixtures with plug
5 times for each of all fixtures with balloon
5 times for each of all fixtures with plug or balloon
10 times for each of selected 4 fixtures with plug or balloon Water-flow
Meter No data
5 times for each of all fixtures without measurement
5 times for each of all fixtures without measurement
10 times for each of selected 8 fixtures without measurement
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PILOT TEST: AS-IS PHASE OF URINALS
First, the researcher conducted a pilot test on urinals (02/08/2002~02/28/2002,
04/18/2002~05/08/2002).
a. The experimental objects were made up of twelve urinals (1.5 gpf) in an unmodified
condition (as-is). The researcher directly measured the water-volume per flush with the
plug method and repeated it ten times for each of all the fixtures in the restrooms of the
Langford Architecture building A.
Findings in the Pilot Test: As-is Phase
a. There was a significant difference between directly measured values and the standard.
The measured mean, 0.276 gpf, was much less than the standard 1.5 gpf (see Table 34).
It was because the plug measurement method did not stop up one of the waterways in a
urinal—one waterway was located in back. Finally, the balloon measurement method
was suggested to solve the problem.
Table 34
Descriptive statistics - as-is phase of urinals
.2758
.2213.019
.13756.12.63.51
MeanMedianVarianceStd. DeviationMinimumMaximumRange
As-is_UrStatistic
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b. Some values had considerable differences with the others (see Figure 23). The result
was assumed because original fixtures had not been on a timely management service.
Finally, the researcher decided to tune up the original fixtures to secure managed status.
1mu11mu2
1mu32mu1
2mu22mu3
3mu13mu2
3mu34mu1
4mu24mu3
fixtures
0.10
0.20
0.30
0.40
0.50
0.60
gpf
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Figure 23: Scatter plot - measured data (plug method)
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c. In the as-is phase, the plug measurement method was not correct, and the balloon
method that could measure the actual water-volume was not applied. Therefore, to
predict the values with the balloon method in the as-is phase, an equation, Predicted
Balloon as-is = 0.88 + 2.13 * Plug as-is, was applied—the regression procedure was
explained in the tune-up phase of urinals. Table 35 shows the predicted result of as-is
phase.
Table 35
Descriptive statistics - measured data (balloon method)
1.46301.3468
.086.29327
1.132.231.09
MeanMedianVarianceStd. DeviationMinimumMaximumRange
As-is_ Balloon_ Urinal
Statistic
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d. The predicted mean, 1.4630 gpf, in the as-is phase of urinals was less than the
standard 1.5 gpf (see Table 35). However, statistically, there was no significant
difference between the predicted mean and the standard. To compare them, a one sample
T-test was conducted:
H : μ as-is = 1.5 gpf, o
H : μ as-is 1.5 gpf. a ≠
The null hypothesis was accepted because p-value (.157) > .05 (see Table 36).
Table 36
T-Test - measured data (balloon method) vs. standard (1.5 gpf)
-1.426 119 .157 -.0370 -.0885 .0144as-is Ur
t df Sig. (2-tailed)Mean
Difference Lower Upper
95% ConfidenceInterval of the
Difference
Test Value = 1.5
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e. To define another measure of variability, coefficient of variation (CV) was applied.
The coefficient of variation (CV) measures the variability in the values in a population
relative to the magnitude of the population mean. Thus, the CV is the standard deviation
of the population expressed in units of μ.
Coefficient of variation (CV) of the predicted values was 20.048 %:
CV = 100 ( s / ⎟ y ⎢)% = 100 (0.2933 / 1.4630)%.
Moreover, there were some problem values (Figure 23).
1mu11mu2
1mu32mu1
2mu22mu3
3mu13mu2
3mu34mu1
4mu24mu3
fixture
1.25
1.50
1.75
2.00
2.25
g pf
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AMean = 1.46
Figure 24: Scatter plot - measured data (balloon method)
f. After the as-is phase, a water-flow meter, Rosemont 8705, was installed to obtain
reliable data in basement of the Langford Architecture building A.
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TUNE-UP PHASE OF URINALS
Second, the researcher collected data on the tune-up phase of the urinals (9/26/2002~
10/09/2002).
a. New diaphragms, handles, and vacuum breakers were installed in the original valves
of all urinals. However, chinas and other plumbing systems had same status as the as-is
phase, and the standard of the urinals, 1.5 gpf, was also the same.
b. The researcher measured the actual water-volume per flush with plug and balloon
methods and repeated it five times for all twelve fixtures. At the same time, the water
meter was read.
c. Additionally, the water meter was read five times per each for all twelve fixtures,
when the plug or balloon method was not applied to china, to analyze whether the
measurement methods were effective in measuring meter values.
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Findings in Tune-up Phase
a. There was a significant difference between the two means of directly measured values
with plug and balloon methods in the tune-up phase (see Table 37 and Table 38). The
mean (0.2521 gpf) measured with the plug method was around 17.85% of the mean
(1.4125 gpf) measured with the balloon method. It meant that the plug method missed a
lot of water. However, the balloon method was reliable because it could stop up the all
waterways of the urinals perfectly.
Table 37
Descriptive statistics - tune-up phase of urinals (plug method)
.2521
.2071.013
.11311.13.50.37
MeanMedianVarianceStd. DeviationMinimumMaximumRange
Tuneup _Plug_Ur
Statistic
Table 38
Descriptive statistics - tune-up phase of urinals (balloon method)
1.41251.3871
.114.33824
.732.021.29
MeanMedianVarianceStd. DeviationMinimumMaximumRange
Tuneup _Ball_Ur
Statistic
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b. The mean, 1.41 gpf, measured with the balloon method was less than the standard 1.5
gpf (see Table 38). Moreover, statistically, there was a significant difference between the
mean and the standard. To compare them, a one sample T-test was conducted:
H : μ tune-up_balloon = 1.5 gpf, o
H : μ tune-up_balloon ≠ 1.5 gpf. a
The null hypothesis was rejected because p-value (.048) < .05 (see Table 39).
Table 39
T-Test - measured data (balloon method) vs. standard (1.5 gpf)
-2.016 59 .048 -.0876 -.1745 -.0006tune-upUr
t df Sig. (2-tailed)Mean
Difference Lower Upper
95% ConfidenceInterval of the
Difference
Test Value = 1.5
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c. The values measured with the balloon method had considerable differences between
the fixtures (Figure 24). Coefficient of variation (CV), 23.946 %, was more than as-is
phase:
CV = 100 ( s / ⎟ y ⎢)% = 100 (0.3382 / 1.4125)%.
1mu11mu2
1mu32mu1
2mu22mu3
3mu13mu2
3mu34mu1
4mu24mu3
fixture
1.00
1.50
2.00
gpf
A
AAAA
AAAAA
AAAAA
AAAA
A
AA
AAA
AAAAA
AAA
A
A
A
AA
A
A
A
AAAA
A
A
A
A
A
A
AAAA A
AAAA
Mean = 1.41
Figure 25: Scatter plot - measured data (balloon method)
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d. Even though the plug method was not correct, it was reliable in measuring the water-
volume per flush. Figure 26 shows that the values measured with the plug method have
similar graphs to the values measured with the balloon method in the tune up phase.
Therefore, it was assumed that there was a relationship between the values measured
with both plug and balloon methods.
The regression model between balloon and plug methods in the tune-up phase of urinals
was Balloon tune-up = Bo + B1 Plug tune-up = 0.88 + 2.13 * Plug tune-up (see Figure
27 and Table 40). The test results of the model were acceptable (see Table 41 and 42).
Residual was also normally distributed (Figure 28 and Table 43).
0.00
0.20
0.40
0.60
0.80
1.00
1.20
1.40
1.60
1.80
2.00
2.20
1 2 3 4 5 6 7 8 9 10 11 12
fixtures
gpf plug
balloon
Figure 26: Graph - balloon vs. plug methods
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57
Linear Regression
0.20 0.30 0.40 0.50
plug
1.00
1.50
2.00
ballo
on
A
A
A
A
AA
A
A
A
AA
A
ball = 0.88 + 2.13 * plugR-Square = 0.51
Figure 27: Scatter plot - balloon vs. plug methods Table 40
Coefficients - balloon vs. plug methods
.875 .182 4.810 .0012.132 .663 .713 3.215 .009
(Constant)PLUG
Model1
B Std. Error
UnstandardizedCoefficients
Beta
StandardizedCoefficients
t Sig.
Table 41
Model summary - balloon vs. plug methods
.713a .508 .459 .24877Model1
R R SquareAdjustedR Square
Std. Error ofthe Estimate
Predictors: (Constant), PLUGa.
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Table 42
ANOVA table - balloon vs. plug methods
.640 1 .640 10.335 .009a
.619 10 .0621.258 11
RegressionResidualTotal
Model1
Sum ofSquares df Mean Square F Sig.
Predictors: (Constant), PLUGa.
Regression Standardized Residual
1.501.00.500.00-.50-1.00-1.50-2.00
Dependent Variable: BALLOON
Freq
uenc
y
5
4
3
2
1
0
Std. Dev = .95 Mean = 0.00
N = 12.00
Figure 28: Residual histogram - balloon vs. plug methods
Table 43
Normality test - balloon vs. plug methods
.293 12 .005 .862 12 .052StandardizedResidual
Statistic df Sig. Statistic df Sig.Kolmogorov-Smirnova Shapiro-Wilk
Lilliefors Significance Correctiona.
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59
e. Basically, both the as-is and tune-up phases had the same chinas, valves (1.5 gpf), and
plumbing systems. Therefore, it was assumed that the relationship between values
measured with the plug and balloon methods in the as-is phase was the same as the
relationship in the tune-up phase. Finally, to predict the data measured with the balloon
method in as-is urinals, the regression model in the tune-up phase was applied. The
equation, Predicted Balloon as-is = 0.88 + 2.13 * Plug as-is, was applied.
f. The mean of the water meter, 1.204 gpf, was less than the directly measured mean,
1.413 gpf, with balloon methods because the water meter was not sensitive to small
water volume (see Table 44). To prove it, A paired T-test was conducted,
H : μ meter with balloon = μ balloon, o
H : μ meter with balloon μ balloon. a ≠
The null hypothesis was rejected because p-value (.000) < .05 (see Table 45).
Therefore, the water meter was not appropriate as a measurement method.
Table 44
Descriptive statistics - water meter with balloon method
1.20351.2210
.109.33074
.511.761.25
MeanMedianVarianceStd. DeviationMinimumMaximumRange
MET_BALLStatistic
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Table 45
Paired T-test - water meter vs. measured data (balloon method)
-.2089 .05849 .01688 -.2461 -.1718 -12.4 11 .000Meter -Balloon
MeanStd.
Deviation
Std.ErrorMean Lower Upper
95% ConfidenceInterval of the
Difference
Paired Differences
t dfSig.
(2-tailed)
g. However, the water meter was reliable in measuring the water-volume per flush.
Figure 29 shows that meter and values measured with the balloon method in the tune-up
phase have similar graphs—they are moving together in a constant rate. Moreover, a
regression model showed that they had a relationship (see Figure 30 and Table 46). The
regression model had a high R-square and the test results were acceptable (see Table 47
and 48)
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0.20
0.40
0.60
0.80
1.00
1.20
1.40
1.60
1.80
2.00
2.20
1 2 3 4 5 6 7 8 9 10 11 12
fixtures
gpf
meter with balloon balloon
Figure 29: Graph - water meter vs. measured data (balloon method)
Linear Regression
0.50 1.00 1.50
Water Meter
1.00
1.50
2.00
Mea
sure
d w
ith B
allo
on in
Tun
e-up
A
A
A
A
AA
A
A
A
AA
A
measured = 0.20 + 1.01 * meterR-Square = 0.97
Figure 30: Scatter plot - water meter vs. measured data (balloon method)
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Table 46
Coefficients - water meter vs. measured data (balloon method)
.200 .070 2.879 .0161.007 .056 .985 18.027 .000
(Constant)MET_BALL
Model1
B Std. Error
UnstandardizedCoefficients
Beta
StandardizedCoefficients
t Sig.
Table 47
Model summary - water meter vs. measured data (balloon method)
.985a .970 .967 .06129Model1
R R SquareAdjustedR Square
Std. Error ofthe Estimate
Predictors: (Constant), MET_BALLa.
Table 48
ANOVA table - water meter vs. measured data (balloon method)
1.221 1 1.221 324.978 .000a
.038 10 .0041.258 11
RegressionResidualTotal
Model1
Sum ofSquares df Mean Square F Sig.
Predictors: (Constant), MET_BALLa.
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63
h. There was no difference between results with and without measurement methods in
the water meter. Therefore, the test with plug or balloon method had no effect on the
value of the water meter. To prove it, a Bonferroni test was conducted:
H : μ meter only = μ meter with plug = μ meter with balloon, o
H : at least one of the means differs from rest. a
The null hypothesis was accepted (see Table 49).
Table 49
Bonferroni test - with and without methods in water meter Dependent Variable: METERBonferroni
.0082 .14161 1.000 -.3490 .3653
.0000 .14161 1.000 -.3572 .3572-.0082 .14161 1.000 -.3653 .3490-.0082 .14161 1.000 -.3653 .3490.0000 .14161 1.000 -.3572 .3572.0082 .14161 1.000 -.3490 .3653
(J)2.003.001.003.001.002.00
(I)1.00
2.00
3.00
MeanDifference
(I-J)Std.Error Sig. Lower Bound Upper Bound
95% Confidence Interval
1: meter only, 2: meter with plug, 3: meter with balloon
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64
LOW-MANUAL PHASE IN URINALS
Third, the researcher collected data on the low-manual phase of urinals (10/14/2002~
10/27/2002).
a. New low-consumption manual valves and chinas were installed in the restrooms of the
Langford Architecture building A. However, other plumbing systems had the same
status as before. They all had the same shape of china and the same type of valves, and
the standard of urinals was 1.0 gpf. Furthermore, all waterways of new china could be
stopped up with both plug and balloon measurement methods.
b. The researcher measured the actual water-volume per flush with the plug or balloon
methods and repeated it five times for all twelve fixtures. At the same time, the water
meter was read.
c. Additionally, the water meter was read five times for all twelve fixtures, when the
measurement method was not applied to china, in order to analyze whether the method
was effective in measuring meter values.
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65
Findings in Low-manual Phase
a. The mean, 0.670 gpf, in the low-manual phase of the urinals was less than the
standard 1.0 gpf (see Table 50). Moreover, statistically, there was a significant
difference between the mean and the standard. To compare them, one sample T-test was
conducted:
H : μ low-manual = 1.0 gpf, o
H : μ low-manual 1.0 gpf. a ≠
The null hypothesis was rejected because p-value (.000) < .05 (see Table 51).
Table 50
Descriptive statistics - low-manual phase of urinals
.6703
.6451.004
.06685.60.82.21
MeanMedianVarianceStd. DeviationMinimumMaximumRange
Lowmanual_Urinal
Statistic
Table 51
T-test - measured data vs. standard (1.0 gpf)
-35.944 59 .000 -.3297 -.3480 -.3113Low-manual Ur
t df Sig. (2-tailed)Mean
Difference Lower Upper
95% ConfidenceInterval of the
Difference
Test Value = 1.0
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66
b. Coefficient of variation (CV) of the low-manual phase was 9.973 %:
CV = 100 ( s / ⎟ y ⎢)% = 100 (0.0669 / 0.6703)%.
It was quite less than the as-is and tune-up phases, and Figure 31 shows that the
difference between the fixtures is not significant.
1mu11mu2
1mu32mu1
2mu22mu3
3mu13mu2
3mu34mu1
4mu24mu3
fixture
0.60
0.70
0.80
gpf
AAAA
A
A
A
A
A
A
AA
A
A
A
A
A
A
A
A
AAA
A
A
A
AAAA
A
A
A
A
A AA
AAA
A
A
AA
A
A
A
AA
A
A
A
A
A
A
A
A
A
A
A
Mean = 0.67
Figure 31: Scatter plot – measured data (balloon method)
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67
c. The mean of the water meter (0.487 gpf) was less than the directly measured mean
(0.670 gpf) with plug and balloon methods—it is the same result as in the tune-up phase
(see Table 52). A paired T-test was conducted:
H : μ meter = μ measure, o
H : μ meter μ measure. a ≠
The null hypothesis was rejected because p-value (.000) < .05 (see Table 53). Therefore,
the water meter was not appropriate as a measurement method.
Table 52
Descriptive statistics - water meter
.4867
.4750.004
.06184.40.59.19
MeanMedianVarianceStd. DeviationMinimumMaximumRange
METERStatistic
Table 53
Paired T-test - water meter vs. measured data
-.1833 .03420 .00987 -.2051 -.1616 -18.569 11 .000METER -MEASURED
MeanStd.
Deviation
Std.ErrorMean Lower Upper
95% ConfidenceInterval of the
Difference
Paired Differences
t dfSig.
(2-tailed)
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68
d. However, the water meter was reliable in measuring the water-volume per flush.
Figure 32 shows that the water meter and measured values in the low-manual phase have
similar graphs—it is the same result as in the tune-up phase. The meter values and the
measured values are moving together in a constant rate. Moreover, a regression model
showed that they had a relationship (see Figure 33 and Table 54). The results of the
model were acceptable (see Table 55 and 56)
0.30
0.40
0.50
0.60
0.70
0.80
0.90
1 2 3 4 5 6 7 8 9 10 11 12
fixtures
gpf
meter measured
Figure 32: Graph - water meter vs. measured data
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69
Linear Regression
0.40 0.45 0.50
0.55
Water Meter
0.60
0.65
0.70
0.75
0.80
Mea
sure
d in
Low
-man
ual
A
A
A
A
A
A
AA
A
A
A
A
var00007 = 0.21 + 0.95 * var00006R-Square = 0.75
Figure 33: Scatter plot - water meter vs. measured data
Table 54
Coefficients - water meter vs. measured data
.207 .085 2.427 .036
.951 .174 .865 5.459 .000
(Constant)METER
Model1
B Std. Error
UnstandardizedCoefficients
Beta
StandardizedCoefficients
t Sig.
Table 55
Model summary - water meter vs. measured data
.865a .749 .724 .03573Model1
R R SquareAdjustedR Square
Std. Error ofthe Estimate
Predictors: (Constant), METERa.
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70
Table 56
ANOVA table - water meter vs. measured data
.038 1 .038 29.796 .000a
.013 10 .001
.051 11
RegressionResidualTotal
Model1
Sum ofSquares df Mean Square F Sig.
Predictors: (Constant), METERa.
e. There was no difference between results with and without measurement methods in
the water meter. Therefore, the test with plug or balloon method had no effect on the
value of the water meter—it is the same result as in the tune-up phase. A paired T-test
was conducted:
H : μ meter only = μ meter with measurement, o
H : μ meter only μ meter with measurement. a ≠
The null hypothesis was accepted because p-value (.534) > .05 (see Table 57).
Table 57
T-test - with and without methods in water meter
-.0048 .05979 .00772 -.0203 .0106 -.626 59 .534Meter Only -With Measure
MeanStd.
Deviation
Std.ErrorMean Lower Upper
95% ConfidenceInterval of the
Difference
Paired Differences
t dfSig.
(2-tailed)
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71
LOW-AUTOMATIC PHASE OF URINALS
Fourth, the researcher collected data on the low-automatic phase of urinals (11/11/2002~
11/26/2002).
a. New low-consumption automatic valves were installed on the chinas in the low-
manual phase instead of low-consumption manual valves. However, chinas and other
plumbing systems had the same status as the low-manual phase. They all had the same
shape of china and the same type of valves, and the standard of the urinals was 1.0gpf.
b. The researcher measured the actual water-volume per flush with plug or balloon
methods and repeated it ten times for randomly selected four fixtures. At the same time,
the water meter was read.
c. The water meter was read ten times for eight fixtures that were not directly measured,
when the plug or balloon method was not applied to china, in order to expect directly
measured values.
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72
Findings in Low-automatic Phase
a. It was proven that there was a relationship between the water meter and measured
values in the tune-up and low-manual phases. To predict the measured values of the
eight fixtures that were not measured directly, the researcher conducted a regression
between the directly measured four fixtures and the water meter.
The regression model was
Measure low-auto = Bo + B1 * Meter low-auto
= 1.064 – 0.137 * Meter low-auto (see Figure 34 and Table 58).
0.78 0.80 0.82 0.84 0.86
meter
0.93
0.94
0.95
0.96
0.97
measure
A
A
A
A
measure = 1.06 + -0.14 * meterR-Square = 0.15
Figure 34: Scatter plot - water meter vs. measured data
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Table 58
Coefficients - water meter vs. measured data
1.064 .186 5.720 .029-.137 .226 -.393 -.604 .607
(Constant)METER
B Std. Error
UnstandardizedCoefficients
Beta
StandardizedCoefficients
t Sig.
Table 59
Model summary - water meter vs. measured data
.393a .154 -.269 .02002Model1
R R SquareAdjustedR Square
Std. Error ofthe Estimate
Predictors: (Constant), METERa.
Table 60
ANOVA table - water meter vs. measured data
.000 1 .000 .365 .607a
.001 2 .000
.001 3
RegressionResidualTotal
Sum ofSquares df Mean Square F Sig.
Predictors: (Constant), METERa.
The regression model had a low R-square (see Table 59) and the regression results were
not good (see Table 58 and Table 60). Figure 35 and Table 61 shows the normality test
of residual. It was inferred that small sample size caused the problem. However, the
equation was acceptable because, obviously, it was proven that there was a relationship
between the water meter and measured values in the other phases
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74
Regression Standardized Residual
.500.00-.50-1.00
Dependent Variable: MEASURE
Freq
uenc
y
2.5
2.0
1.5
1.0
.5
0.0
Std. Dev = .82 Mean = 0.00N = 4.00
Figure 35: Residual histogram - water meter vs. measured data
Table 61
Normality test - water meter vs. measured data
.300 4 . .833 4 .176StandardizedResidual
Statistic df Sig. Statistic df Sig.Kolmogorov-Smirnova Shapiro-Wilk
Lilliefors Significance Correctiona.
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75
b. The mean, 0.9783 gpf, in the low-automatic phase was less than the standard 1.0 gpf
(see Table 62). Statistically, there was a significant difference between the mean and the
standard. To compare them, a one sample T-test was conducted:
H : μ low-auto = 1.0 gpf, o
H : μ low-auto 1.0 gpf. a ≠
The null hypothesis was rejected because p-value (.037) < .05 (see Table 63).
Table 62
Descriptive statistics - low-automatic phase of urinals
.9783
.9710.001
.03161.93
1.03.10
MeanMedianVarianceStd. DeviationMinimumMaximumRange
LOWAUTOStatistic
Table 63
T-test - measured data vs. standard (1.0 gpf)
-2.374 11 .037 -.0217 -.0418 -.0016Low-Auto Ur
t df Sig. (2-tailed)Mean
Difference Lower Upper
95% ConfidenceInterval of the
Difference
Test Value = 1.0
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76
c. Figure 36 shows the difference between the fixtures, and coefficient of variation (CV),
3.230 %, is the lowest value in the urinal phases:
CV = 100 ( s / ⎟ y ⎢)% = 100 (0.0316 / 0.9783)%.
1mu11mu2
1mu32mu1
2mu22mu3
3mu13mu2
3mu34mu1
4mu24mu3
fixture
0.90
0.95
1.00
gpf
A
A
A
AAAAAA
A
A
A
A
A
A
A
A
A
A
AA
AA
A
A
A
A
A
A
A
A
A
AA
A
A
A
A
A
A
AAAAAAAA
A
A
AAA
AAAAAA
A
A
A
A
A
AAAAAA
A
A
A
A
AAAAAA
AAAAAAAAAA
AAA
AAAA
AA
A AA
AA
A
A
AAAA
AAAAAAAAA
A
Mean = 0.98
Figure 36: Scatter plot - measured data
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77
SUMMARY OF URINALS
a. The researcher compared the water-volume per flush of all phases in the urinals.
Figure 37 shows the means in the urinals. The result of the mean values is
As-is (1.463 gpf) > Tune-up (1.413 gpf) > Low-auto (0.978 gpf) > Low-manual (0.670 gpf).
Table 64 shows the comparative water-volume of other phases when it is assumed that
the mean of as-is phase is 100%.
1.463 1.413
0.670
0.978
0.00
0.20
0.40
0.60
0.80
1.00
1.20
1.40
1.60
gpf
as-is(1.5gpf) tune-up(1.5gpf) low-manual(1.0gpf)
low-auto(1.0gpf)
Figure 37: Graph - measured means in urinals Table 64
As-is vs. comparative values of other phases in urinals Phase As-is Tune-up Low-manual Low-auto
Mean 1.463 gpf 1.413 gpf 0.670 gpf 0.978 gpf
Each / As-is (%) 100 % 96.58 % 45.80 % 66.85 %
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b. However, statistical analysis has a different result.
A Bonferroni test was conducted:
H : μ as-is = μ tune-up = μ low-manual = μ low-auto, o
H : at least one of the means differs from rest. a
The null hypothesis was rejected (see Table 65).
The result of statistics analysis is
As-is = Tune-up > Low-automatic > Low-manual.
Table 65
Bonferroni test - urinals Dependent Variable: DATABonferroni
.0506 .09262 1.000 -.2053 .3065
.7927* .09262 .000 .5368 1.0486
.4847* .09262 .000 .2288 .7406-.0506 .09262 1.000 -.3065 .2053.7421* .09262 .000 .4862 .9980.4341* .09262 .000 .1782 .6900
-.7927* .09262 .000 -1.0486 -.5368-.7421* .09262 .000 -.9980 -.4862-.3080* .09262 .011 -.5639 -.0521-.4847* .09262 .000 -.7406 -.2288-.4341* .09262 .000 -.6900 -.1782.3080* .09262 .011 .0521 .5639
(J)2.003.004.001.003.004.001.002.004.001.002.003.00
(I)1.00
2.00
3.00
4.00
MeanDifference
(I-J)Std.Error Sig. Lower Bound Upper Bound
95% Confidence Interval
The mean difference is significant at the .05 level.*.
1: As-is, 2: Tune-up, 3: Low-manual, 4:Low-automatic
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c. Most phases of the urinals have different actual water-volumes than their standards
(see Figure 38). The tune-up, low-manual, and low-automatic phases show significant
differences between the standards and the actual water-volumes of flushing (see Table
66).
1.5 1.5
1.0 1.0
1.4631.413
0.670
0.978
0.0
0.2
0.4
0.6
0.8
1.0
1.2
1.4
1.6
As-is Tune-up Low-manual Low-auto
gpf
Standard Mean
Figure 38: Graph - measured mean vs. standard in urinals
Table 66
The standard vs. measured means in urinals Phase As-is Tune-up Low-manual Low-auto
Mean 1.463 gpf 1.413 gpf 0.670 gpf 0.978 gpf
Standard 1.5 gpf 1.5 gpf 1.0 gpf 1.0 gpf
Mean / Std. (%) 97.53 % 94.20 % 67.00 % 97.83 %
Sig. (2-tailed) .157 .048 .000 .037
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d. There is a tendency in the low-consumption fixtures to have a lower coefficient of
variance (CV). New fixtures in the low-manual and low-automatic phases have a low
CV but old fixtures in the as-is and tune-up phases have high rate (see Figure 39 and
Table 67). It is assumed that the results are related to the management status of the
fixtures.
20.046
23.946
9.973
3.230
0
5
10
15
20
25
30
as-is(1.5gpf) tune-up(1.5gpf) low-manual(1.0gpf) low-auto(1.0gpf)
(%)
Figure 39: Graph - coefficient of variance in urinals
Table 67
Coefficient of variance in urinals Phase As-is Tune-up Low-manual Low-auto
Std. Deviation 0.2933 0.3382 0.0669 0.0316
Mean 1.463 gpf 1.413 gpf 0.670 gpf 0.978 gpf
CV 20.046 % 23.946 % 9.973 % 3.230 %
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CONCLUSIONS
The researcher directly measured the actual water-volumes (gpf) of the as-is, tune-up,
low-consumption manual, and low-consumption automatic water closets and urinals
applied to the restrooms of the Langford Architecture building A. Consequently, some
results were found.
a. First, there are significant differences between the standards and the actual water-
volumes—directly measured means (see Table 68). It means that other studies using the
standards are not correct. Therefore, this study provides practical and precise standards
of water closets and urinals.
Table 68
The standards vs. actual water-volumes Phase As-is Tune-up Low-manual Low-auto
Mean 3.305 gpf 4.174 gpf 1.599 gpf 1.980 gpfWater closet Standard 3.5 gpf 4.5 gpf 1.6 gpf 1.6 gpf
Mean 1.463 gpf 1.413 gpf 0.670 gpf 0.978 gpfUrinal
Standard 1.5 gpf 1.5 gpf 1.0 gpf 1.0 gpf
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b. Second, Figure 40 shows that the actual water-volumes of the low consumption
fixtures are much less than those of the old (high-consumption) fixtures. Moreover, there
is no significant difference, statistically, between the low-manual and low-automatic
phases in water closets even though the mean of the low-manual phase is less than the
low-automatic phase’s (see Table 69).
As-isTune-up
Low-manualLow-auto
3.313.31
1.461.46
4.174.17
1.411.601.60
0.67
1.981.98
0.98
0.0
0.5
1.0
1.5
2.0
2.5
3.0
3.5
4.0
4.5
gpf
WC Urinal
Figure 40: Graph - actual water-volumes Table 69
The experiment result of the actual water-volumes (gpf)
Mean Tune-up > As-is > Low-auto > Low-manual WC
Bonferroni Tune-up > As-is > Low-manual = Low-automatic
Mean As-is > Tune-up > Low-auto > Low-manual Urinal
Bonferroni As-is = Tune-up > Low-automatic > Low-manual
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c. Third, Table 70 shows the water-volumes (gpf) of other phases compared to the as-is
phase when it is assumed that the mean of the as-is phase is 100%. Accordingly, this
study presents that retrofitting an original water closet (3.5 gpf) with a low-consumption
fixture (1.6 gpf) can save water-cost up to 51.62 %, and retrofitting an original urinal
(1.5 gpf) with a low-consumption (1.0 gpf) fixture can save water-cost up to 50.44 %.
Table 70
As-is vs. comparative values of other phases Phase As-is Tune-up Low-manual Low-auto
Standard 3.5 gpf 4.5 gpf 1.6 gpf 1.6 gpf
Mean 3.305 gpf 4.174 gpf 1.599 gpf 1.980 gpfWC
Comparative 100 % 126.29 % 48.38 % 59.91 %
Standard 1.5 gpf 1.5 gpf 1.0 gpf 1.0gpf
Mean 1.463 gpf 1.413 gpf 0.670 gpf 0.978 gpfUrinal
Comparative 100 % 96.58 % 45.80 % 66.85 %
Finally, this study provides the actual water-consumptions (gpf) of sanitary fixtures and
proves that retrofitting with low-consumption fixtures can save on water costs. The
results will present practical standards to facility managers and other building
professionals and will also contribute to determining the availability of retrofitting water
closets and urinals.
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REFERENCES
Clarke, R. (1996). Environmental management: A guide for facility managers. New York: UpWord Publishing, Inc.
International Union for Conservation of Nature and Natural Resources. (2000). Vision
for water and nature: A world strategy for conservation and sustainable management of water resources in the 21st century. Cambridge, UK: Author.
Lewis, B. (2000). Facility manager’s potable handbook. New York: McGraw-Hill. Parker, K. (2002). Determination of maximum flow rate in a building water supply
system by means of acoustic observation. Ph.D. Dissertation, Texas A&M University.
Pratt, A. (1979). The water economy of a low flush toilet in a water deficient region.
Virgin Islands: Caribbean Research Institute, College of the Virgin Islands. Reid, R. (1996). Water quality & systems: A guide for facility managers. New York:
UpWord Publishing, Inc. Rocky Mountain Institute. (1991). Water efficiency: A resource for utility managers,
community planners, and other decision makers. Snowmass, Colorado: Author. United States General Accounting Office (USGAO). (2000). Water infrastructure:
Water-efficient plumbing fixtures reduce water consumption and wastewater flows. Washington, DC: Author.
Vickers, A. (2001). Handbook of water use and conservation. Amherst, Massachusetts:
WaterPlow Press.
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APPENDIX A
DEFINITION
Flushometer-valve toilet
A tankless toilet with the flush valve attached to a pressurized water supply pipe. When activated, the connecting pipe supplies water to the toilet at a flow rate necessary to flush waste into the sewer
GPCD Gallons per capita per day GPD Gallons per day GPF Gallons per flush Gravity-flush toilet
A toilet with a rubber stopper (flapper valve) that releases water from the toilet tank, after which gravity forces the contents of the toilet bowl through a trap way for discharge into the wastewater system
Low-consumption water closet
A toilet that uses no more than 1.6 gallons per flush; also referred as low-flow toilet
Low-consumption urinal
A urinal that uses no more than 1.0 gallon per flush; also referred as low-flow urinal
Water meter
An instrument that measures water use; often installed by a water utility to measure end uses, such as uses by a household, building facility, or irrigation system
Retrofit
To change, alter, or adjust plumbing fixtures or other equipment or appliances to save water or make operate more efficiently.
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VITA
Byoung Hoon Hwang
Geovill #601, 53 Jukjun 1 dong Yongin, Kyunggi 449-161, South Korea 1-31-266-8787, [email protected]
EDUCATION
Master of Science in Construction Management Texas A&M University, USA, August 2003
Bachelor of Science in Architectural Engineering Hanyang University, Korea, February 1997
PROFESSIONAL EXPERIENCE
Doosan Construction & Engineering, Seoul, Korea Project Engineer, 09/1997 ~ 04/2000
Hyungjin Construction, Seoul, Korea Project Engineer, 03/1997 ~ 07/1997
QUALIFICATION
Facility Management certificate, Texas A&M University, 2003
Safety certification, Occupational Safety & Health Administration, 2003
First class architectural engineer, Korea, 1996
AWARDS & SCHOLARSHIPS
Woods Graduate Research Scholarship, Texas A&M University, 2003
Herman J. Smith Scholarship, The National Housing Endowment, 2002
Construction Law Section Scholarship, The State Bar of Texas, 2002
Prize Winner in the thesis competition, Daedong construction, 1997
Scholarships, Hanyang University, 1995/ 1994