Steel Coated Product Limited, Vasind · 100% Subsidiary of JSW Steel India’s Leading Coated Steel...
Transcript of Steel Coated Product Limited, Vasind · 100% Subsidiary of JSW Steel India’s Leading Coated Steel...
CII National Energy Efficiency Circle Competition
Presenters:
Mr. Anish Karahe- Sr. Manager
Ms Aditi Chauhan- Jr. Manager
Steel Coated Product Limited, Vasind
Jindal SAW JSL StainlessJindal Steel and
Power
Mr. Prithvi Raj Jindal Mr. Sajjan Jindal Mr. Ratan Jindal Mr. Naveen Jindal
• Jindal ITF
• Jindal Waterways
• Jindal Transrail
• Jindal Water
Infrastructure
• Jindal Urban
Infrastructure
• Jindal Shipyards
• Jindal Rail
Infrastructure
✓JSW Steel
✓JSW Steel Coated
Products Ltd
✓JSW Energy
✓JSW Infrastructure
✓JSW Cement
✓JSW GBS
✓JSW Sports
✓JSW Foundation
• JSL Media
• JSL Lifestyle
• JSL Architecture
• Green Delhi BQS
• JSS Steel Italia
• PT Jindal
Stainless,
Indonesia
• Jindal Stainless
Steel ways
• Jindal Power
• Jindal Petroleum
• Jindal Steel
Bolivia
• Jindal Cement
Shri. O. P. Jindal
“Where others see walls…..,
I see doors…..”
O P Jindal Group
3
Steel
India’s Leading integrated
Steel Producer (18 MTPA)
Vijayanagar – 12 MTPA
Dolvi – 5 MTPA
Salem – 1 MTPA
SCPL
100% Subsidiary of JSW Steel
India’s Leading Coated Steel
Producer (1.8 MTPA) Vasind – 0.45 MTPA
Tarapur – 0.76 MTPA
Kalmeshwar – 0.6 MTPA
▪ Engaged across the value chain of power business (Operational plants’ capacity: 4,531 MW)
Energy
▪ Engaged in development and operations of ports (Operational capacity: 70 MTPA
Infrastructure
Cement
▪ Manufacture of PSC, OPC and GGBS cement, (Operational Plants capacity 10.3 MTPA)
JSW Group
s
2018
2017
2016
2015
2019
• Commissioning of PLTCM
• Capacity increased by 300%
• CII-GreenCO Certification• MEDA 12th State Level EC Award
• CGL Speed Increase
• CCL Local Burner Installation
• EMS 14001:2015 Certification
• EnMS ISO 50001:2011 Certification
• OSHAS 18001:2007 Certification
• CII-2017 Commendation Certificate
• IMC RBNQA-2016 Excellence
Trophy
• Installation of On Line Skin Pass
• CII Energy Audit
• Earned 1871 ESCerts in PAT -1
20112012
• Installation of Railway Yard
1994Installation of CGL-1 & CRM-4
2003 • Installation of CGL-2
1990 Installation of CRM-3
• Power Open Access
• RLNG Supply Line From
GAIL
• Installation of Colour Coating
Lines
1996 QMS ISO 9001 Certification
2013• Entitled as Designated
Consumer of PAT
Road Map
5
Energy
Sources
RLNG
Electrical
Power
6.49
Lacs MMBtu/A
885
Lac kWh/A
163147
GCal/A
81576
GCal/A
RLNG163147 GCal
69%
Power81576 GCal
31%
Energy consumed at Vasind
RLNG
Electrical Power
Energy Sources
GAIL
JSW Energy
Open Access
RLNGElectrical
Power
Total : 239764 GCal/A
1. Specific Energy Consumption
11%
12%
52%
23%
2%
Energy in GCAL
Pre-Rolling
Rolling
Galvanizing (GI/GL)
Colour Coating
Auxillary
Annual Consumption FY-18
CII National Energy Efficiency Circle Competition 6
6%
38%
39%
12%
5%
Process Wise Power Consumption kWh
Pre-Rolling
Rolling
Galvanising
Colour Coating
Auxilary
14%
58%
28%
Process Wise RLNG Consumption MMBtu
Pre Rolling
Galvanizing(GI/GL)
Colour Coating
Area Power(Lac kWh) RLNG(Lac MMBtu) Energy in Gcal
Pre-Rolling 50 0.90 27008
Rolling 333 0.04 29500
Galvanizing(GL/GI) 348 3.75 124368
Colour Coating 107 1.80 54723
Auxilary 47 4165
Grand Total 885 6.49 2,39,764
1. Specific Energy ConsumptionProcess wise Energy Consumption
7
Plant capacity Utilization & Reduction in Specific Energy Consumption (Year wise)
Plant Energy Consumption
Energy Unit FY 16 FY 17 FY 18
Electricity Lakh Kwh 749.3 887 885
ThermalMillion
Kcal136574 149571 163147
Specific Energy
Consumption MTOE/t 0.050 0.042 0.041
Plant Capacity Utilization
Year Unit FY 16 FY 17 FY 18
Installed Capacity Lacs ton 4.5 4.5 4.5
Actual Production Lacs ton 3.96 4.46 4.55
Capacity Utilization % 87.78 99.23 101.11
0.050
0.042 0.041
0.030
0.035
0.040
0.045
0.050
0.055
FY 16 FY 17 FY 18
Specific Energy Consumption MTOE/t
1. Specific Energy Consumption
87.78
99.23 101.11
80
85
90
95
100
105
FY-16 FY-17 FY-18
Capacity Utilization %
PAT-1Energy Consumption (MTOE/T) Energy
Saving
MTOE
ESCerts
AwardedNotified Notified
Target
Baseline
Verification
0.0594 0.0575 0.0545 2042.3 1875
PAT-2Energy Consumption (MTOE/T)
Notified Notified
Target FY 16-17 FY 17-18 FY 18-19
0.044 0.0413 0.042 0.041 0.039
0.0594
0.0545
0.05
0.042 0.0410.039
0.035
0.04
0.045
0.05
0.055
0.06
0.065
FY 13 FY 15 FY 16 FY 17 FY 18 FY 19
Energy MTOE/t
Perform Achieve Trade (PAT) Cycle
1. Specific Energy Consumption
9
0.0518
0.0463
0.0446
0.040
0.042
0.044
0.046
0.048
0.050
0.052
0.054
Tarapur Kalmeshwar Vasind
Energy Cosnumption (Mtoe/t)Parameter UNIT Tpr Klm Vsd
Total Plant Energy Consumption Mtoe 45728 32723 26143
Total Equivalent Production MT 882519 707310 586721
Energy Cosnumption Mtoe/t 0.0518 0.0463 0.0446
• Benchmarking of Energy data through Energy Report on a monthly basis.
• Adoption of best practices
2.Benchmarking
545 3.46
0.80
9.00
4.99
2.53
1.20
50.1
418
0.53 0.13
0.12 0.06
42.5
390
SEC
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Cra
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Inst
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Inst
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f Ec
on
om
izer
Bo
iler.
loca
l bu
rner
CC
L-1
Road Map of Specific Energy Consumption Reduction
Energ
y
Consum
ption
(Mega C
al/t)
34.9
loca
l bu
rner
CC
L-2
2.Benchmarking
12157
852
Rs Lac
FY 16 FY 17 FY 18
28322600
22241
GCal
FY 16 FY 17 FY 18
191
131
1095
Rs Lac
FY 16 FY 17 FY 18
Energy Savings & Investment
Energy Savings
Investment
Total Energy Saving (FY-16 to FY-18)
27673 GCal
Total Saving by Zero Investment Projects (FY-16 to FY-18) – 2170 GCal
Potential Investment in
FY 19 – 103.2 cr
Potential Saving In
FY19 – 86251.6 GCal
3.Energy Saving Projects Implemented
12
ENCON Measures.04Energy Saving(kWh)
Savings(Rs Million)
Investment (Rs Million)
Payback (Months)
Auto speed control of CCL Oven Recirculation Fan 89000 0.534 0 0
Speed Control of CAG1 blower with strip temperature
in CGL#184672 0.47 0 0
CAG-2,3,4 & 5 blowers operation with TPH in CGL#1 701568 3.9 0 0
Reduction of idle power consumption 120000 0.72 0 0
CGL2 and CRM3 unit water supply system connected
with each other and made CGL2 one 30 KW pump off180576 1 0 0
Installation of VFD in CRM#4 & CRM#3 Coolant pump 670000 4 1 3
Commissioning of On line SPM in CGL#1 1080000 6.48 10 18.5
Installation of VFD in Hot Air Generator 79000 0.474 0.3 7.6
Provision of drive for POR DC Motor cooling blower
CRM#3 & CRM#473000 0.438 0.05 1.4
Provision of AC Drive for Pickling Squeeze Roll Hyd Power
pack42000 0.052 0.2 46.2
Installation of LED Lights 64800 0.38 0.35 10.8
VFD Drives installation for CGL#1 Non ox blower with
pressure close loop108864 0.6 0.2 3.9
Total 3293480 19.05 12.1 7.6
ENCON Measures FY - l6
ZERO INVESTMENT Projects
3.Energy Saving Projects Implemented
13
ENCON Measures
Energy Saving
Saving
(Rs Million)
Investment
(Rs Million)
Payback
(Months)Electrical
(kWh)
Thermal
(Gcal)
Optimization of CGL#2 cooling towers 218000 1.3 0 0
VFD Installation in CRM#4 & CRM#3 Fume
Exhaust blower360000 2.16 1.8 10
Optimization of Air compressors at CGL#1 &
CRM#4680000 4.04 1.2 3.6
Installation of high efficiency 380 CFM
Compressor180576 1.01 1.2 14
Installation of booster pump for CCL AC
210000 1.26 0.2 1.9
Installation of LED Lights 198720 1.1 1 11
Installation of Economizer at 5 Ton Boiler. 1001 2.2 0.15 0.8
Installation of Bell mouth in Non ox blower 13000 0.078 0.2 30.8
TOTAL 1860296 1001 13.15 5.75 5.2
ENCON Measures FY – 17
ZERO INVESTMENT Projects
3.Energy Saving Projects Implemented
14
ENCON Measures
Energy SavingSavings
(Rs Million)
Investment
(Rs Million)
Payback
(Months)Electrical
(kWh)
Thermal
(GCal)
CGL #1 Line Fix Power Optimization by
increasing Line Speed from 120 to 150 MPM 862529 5.13 0 0
Induction oven output optimization 267000 1.6 0 0
CGL #2 Line Fix Power Optimization by increasing
Line Speed from 150 to 200 MPM .2131240 13.12 31.2 28.33
Closed loop speed control of CGL#2 APC Blowers by
using VVVF drive135000 0.8 0.6 9
Installation of LED Lights 105000 0.64 0.52 9.64
New Energy Efficient Pump(7.5 kW) Installed at ARP 23000 0.14 0.18 15.4
Provision of local burner at CCL-1 oven to reduce
fuel consumption 20,16000 17357 65 20 3.7
Pump Motor Speed Optimization by increasing VFD
in two nos Re-Circulation Pumps119184 0.73 0.12 1.9
Old motor of 11KW replaced with IE-3 efficiency 7.5
KW motor20106 0.12 0.025 2.42
Total 5679059 17357 109.56 85.28 9.3
ENCON Measures FY - 18
ZERO INVESTMENT Projects
3.Energy Saving Projects Implemented
15
ENCON Measures
Electrical
Savings
(kWh)
Thermal
Savings
(GCal)
Savings(Rs Million)
Investment(Rs Million)
Payback(Months)
Developing CGG Alloy to reduce RLNG and Power
consumption at Alloy Furnace73000 1334 3.8 0 0
Installation of 1.3 million ton Pickling Linked Tandem
Coldrolling Mill with advance energy efficient technology48000000 15120 374.5 1000 32.04
Replacement of conventional lights by 150 Nos LED
lights .85410 0 0.58 0.5 10.33
Using excess Steam of CCL at CRM 4 to heat Coolant in
place of RLNG.60000 1200 3.96 1 3.03
Modification of CGL-1 Pump house with Energy Efficient
Equipment and pipe line redesigning.49275 0 0.33 0.4 14.32
Installation of new common pump house for CRD &
CGL-2 with Energy Efficient Equipment63875 0 0.43 0.4 11.05
Reduction of Fuel consumption by optimizing Air Fuel
Ratio by installing Oxygen analyser at CGL-1 Stack0 257 0.75 0.5 7.94
Reduction of Fuel consumption by optimizing Air Fuel
Ratio by installing Oxygen analyzer at CGL-2 Stack0 171 0.5 0.5 11.88
Provision of local burner at CCL-2 oven to reduce fuel
consumption 2250000 17010 66 20 3.6
ENCON Measures Planned FY 19
3.Energy Saving Projects Planned
ZERO INVESTMENT Projects
16
ENCON Measures
Electrical
Savings
(kWh)
Thermal
Savings
(Gcal)
Savings(Rs Million)
Investment(Rs Million)
Payback(Months)
CGL-2 furnace modification to Operate in Strip Temperature
control mode, in place of Zone temperature control mode.0 1058.4 3.1 0.2 0.77
Replacement of CGL-1 Furnace water cooled type Hearth roll
with Non Water cooled Earth rolls (7 Nos)262800 5518.8 17.99 2.2 1.46
Installation of 200 KW VFD in CRM3 Air compressor and close
loop the motor speed with Header pressure to avoid unloading
of compressor.
146000 0 0.99 0.7 8.4
Installtion of VFD for LT and CT operation of crane in 3 nos
cranes.54750 0 0.37 1.5 48.3
Replacement of Old motors with Energy efficient IE-3 motors
(45 KW 8 Nos)112128 0 0.76 1.6 25.1
Replacement of inefficient old ventilation blowers of CRM-4 mill
motor with high efficiency blowers.429240 0 2.91 1.5 6.1
Replacement of inefficient old ventilation blowers of CRM-3 mill
motor with high efficiency blowers.254040 0 1.72 1.5 10.4
Total 51840518 41668.8 478.69 1032.5 25.8
ENCON Measures Planned FY 19
3.Energy Saving Projects Planned
Power 107 kWh/t
Cold Rolling PicklingHRS Pickling Linked Tandem Cold Mill (PLTCM)
RLNG0.1
MMBtu/t
Power 60 kWh/t
RLNG0.05
MMBtu/t
BEFORE IN FY - 19
Energy Consumption0.081 Gcal/t
Energy Consumption0.064 Gcal/t
Turn
around
Estimated Energy Saving-42792 Gcal/A @ 1.3 Million Ton Production
Investment Rs.800 Cr
Combination of three
process
Use of Energy
Efficient AC motors
MV VFD drives & advance
Level –II automation
Pickling Linked Tandem Cold Mill
18
Project Selection
A) Annual Saving Potential of Energy
Consumption in GCal
5 More than 1000 GCal
4 More than 500 GCal
3 More than 250 GCal
2 More than 100 GCal
1 Less than 100 GCal
0 Not Identified
B) Investment required (Rs. In
lacs)
5 Less than 10 lacs
4 More than 10 lacs
3 More than 15 lacs
2 More than 25 lacs
1 More than 50 lacs
0 Not Identified
C) Required down time (excluding lead time
of resources.)
5 Less than One day
4 Less than three days
3 Less than five days
2 Less than seven days
1 More than seven days
0 Not Identified
" * " = Priority of SEU to be decided based on above methodology in descending order of score . Eg. P1 top priority and so on…
Projects
Annual
Energy
Savings
Investment
Required
Required
Down
Time
Annual
Energy
Saving
Investment
required
Required
down
time
Score
Priority
(P1..P2
… etc.,)
GCal Rs in Lacs Days A B C A X B X C *
Speed Optimization of CAG 676.2 0 1 4 5 5 100 P1
CGL #1 Line Fix Power Optimization 741.8 0 1 4 5 5 100 P1
Closed loop speed control of CGL#2 APC
Blowers 116.1 8 0 2 5 5 50 P2
Pickling Pump Motor Speed Optimization 102.5 1.2 1 2 5 5 50 P2
Provision of local burner at CCL-1 oven 19090.8 200 6 5 1 2 10 P3
CGL #2 Line Fix Power Optimization 2062.5 312 10 5 1 1 5 P4
4.Innovative Projects Implemented
176
Received
45
Selected
29
Implemented
16
Planned
Suggestions
19RTOPrimary Heat
Exchanger
Secondary Heat
Exchanger
Waste Heat
Recovery Boiler
Hot By Pass Valve
Oven Zone
RC Fan
Chimney
Project Area
Localize Heating Arrangement in Colour Coating Line
• No of Ovens – 2 Nos
• Each Oven - 5 Zones
VOC to RTO
Combustion Blower
Fresh Air
To Process
Steam
Innovation Project and Case Study-
Before
4.Innovative Projects Implemented
20IM
Major Challenges
In CCL all zones of prime and finish ovens were heated with centralised RTO (Regenerative Thermal Oxidizer). The Temperature Required in Ovens is approximately 400 deg C, For achieving the same we need to increase the RTO Temperature more.
Huge Losses due to indirect heating and to Maintain Oven temperature, Required High Volume of hot air Resulting High RLNG Consumption- 0.86 MMBtu/t
To fulfil high hot air volume in Ovens, All Blowers running at full speed resulting High Power Consumption - 47 kWh/t
Less Utilization due to Frequent Maintenance required for the RTO System
It takes longer time, around 4 hrs for Oven heating during Line start up
Solution Proposed
Provision of ZONE WISE LOCAL BURNER in Ovens
Provision of FIRING CONTROL
Installation of LEL (Low Explosion Level) Sensor to
monitor VOC Concentration
Use of Hot Air bypass only for safety
Optimization of Valve Blower Speed wrt Product Mix
Before AfterSaving
(Rs Lac/A)
RLNG Consumption (MMBtu/T) 0.86 0.65 263
Power Consumption (KWh/T) 47 43 46
309
Avg Production Per Month 11000 12500 1260
Diversion due to RTO Tripping (%) 0.2 0 30
RTO Tripping (Nos/ Month) 8 0
Productivity ( Ton/Hr) 20 25
1290
1599
Saving in Energy
Saving due to Productivity
Total Saving
Potential Saving
Localize Heating Arrangement in Colour Coating LineInnovation Project and Case Study-
4.Innovative Projects Implemented
21RTOPrimary Heat
Exchanger
Secondary Heat
Exchanger
Waste Heat
Recovery Boiler
Hot By Pass Valve
Oven Zone
Chimney
VOC to RTO
Combustion Blower
Fresh Air
To Process
Steam
RC FanMainPilot
Main RLNG Valve
After
Localize Heating Arrangement in Colour Coating LineInnovation Project and Case Study-
4.Innovative Projects Implemented
22
0.86
0.55
0.45
0.3
0.4
0.5
0.6
0.7
0.8
0.9
Without Local Burner With Local Burner After ProcessOptimization
RLNG Consumption (MMBtu/T) 47
41
35
30
34
38
42
46
50
Without Local Burner With Local Burner After ProcessOptimization
Power Consumption (KWh/T)
Saving/Annum RLNG- 68880 MMBtu ( Rs 5.1 Cr) Saving/Annum Power- 20.1 Lac KWh (Rs 1.5 Cr)
Achieved -Total Energy Saving-19091 Gcal (Rs 6.5 Cr) at CCL-1
Potential- Total Energy Saving-18945 Gcal (Rs 6.6 Cr) at CCL-2
Before AfterAfter Process
Optimization
Saving
(Rs Lac/A)
RLNG Consumption (MMBtu/T) 0.86 0.55 0.45 513
Power Consumption (KWh/T) 47 41 35 137
650
Avg Production Per Month 11000 14000 14000 2520
Diversion due to RTO Tripping (%) 0.2 0 0 30
RTO Tripping (Nos/ Month) 8 0 0
Productivity ( Ton/Hr) 20 25 25
2550
3200
Saving in Energy
Saving due to Productivity
Total Saving
Localize Heating Arrangement in Colour Coating Line Innovation Project and Case Study-
Innovative Projects
Energy Rs Lac
1.7 0.8 67500 500
95 65 2250000 150
4200 6000 1512
0.2 0 14
8 0
8 12.5
1526
2176
Before After Saving Per Annum
650
H
O
R
I
Z
O
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T
A
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D
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P
L
O
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M
E
N
T
At
CCL-2
23
PROBLEM STATEMENT
61%
39%
Fixed Power Variable Power
High Fixed Power Consumption, 60% t of Total Power Consumption
Specific Power Consumption-130 kWh
Huge Variation in Product Mix Causing Less Productivity
Furnace controlling with Zone Temperature Control (ZTC)
No. of Break Downs were high
Energy
Consumption
Product Mix
Automation
Previous Galvanizing Line Flow Diagram
Power Distribution
Fixed Power Can be Optimized by Speed Increase
Reduction of Power Consumption in CGLInnovation Project and Case Study-
4.Innovative Projects Implemented
24
Solution Proposed
One more Recoiler and Bridle added to reduce coil
changeover time at exit section
Welding time reduced from 160 to 120 secs by
reducing the sequence time
PID closed loop logic made by taking TPH and
Output in closed loop for Induction Oven
Drive parameter optimization for process line speed
200 MPM
Furnace operation In Strip Temperature Control
(STC) in place of Zone Temperature control (ZTC)
New Pendant Blower(75 kW) added in place of After
Coating Blower(160 kW) to reduce fixed power
optimization
Furnace Length increase
Both Exit and Entry Looper Height increase to
increase the accumulation capacity
Mix Product Wise Power Consumption
and Production
Identification of Fixed and Variable Power
Consuming Equipment's
Sheet Accumulation Capacity of
Accumulators
Timings of Welding and Cutting during Coil Change Over
Data Collection
Average Power Consumption
130 kWh/T
Variable Power-39%
Fixed Power-61%
Induction Oven consuming 100%
Power at all products.
Sheet Accumulation Capacity of
Accumulators-350mtr
Timings of Welding and Cutting during Coil Change Over-
160 sec
Analysis
Implemented
Budget Req
330 Lac
Dropped
Budget Req
700 Lac
Reduction of Power Consumption in CGLInnovation Project and Case Study-
4.Innovative Projects Implemented
25
Total Energy Saving of 48 Lac kWh/A.
Highest Production in FY 18- 2.17 Lac Ton
Energy Saving of Rs 280 Lac per Annum.
Productivity Increased by 18%
Total Energy Consumption Reduced by20 kWh/t from 120 kWh/t to 101 kWh/t.
Reduction of Power Consumption in CGLInnovation Project and Case Study-
4.Innovative Projects Implemented
26
CA
G-
CAG-3 CAG-2 CAG-1
Colling After Galvanization BlowerInnovation Project and Case Study-
4.Innovative Projects Implemented
Earlier all CAG blowers use to run at full speed despite of low TPH resulting excess power consumption – 174 Unit /Hour.
Optimization and controlling of
CAG blowers speed in accordance of TPH
PROBLEM STATEMENT Solution Proposed
Installation of VFD at all the CAG Blowers
Logic can be made by taking TPH in closed loop
with the speed of the blower
Solution Implemented
Installation of VFD at all CAG Blowers
Logic made for CAG-2,3,4 &5 by taking Blower
Speed and TPH in Closed Loop
Logic made for CAG-1 by taking Blower Speed and
Strip Temperature in Closed Loop with the help of
pyrometer
Colling After Galvanization BlowerInnovation Project and Case Study-
4.Innovative Projects Implemented
28
174 174 174 174 174 174 174174
155
120
95
75
5845
0
20
40
60
80
100
120
140
160
180
200
35 & MORE
33-35 30-32 28-30 25-28 20-25 LESS THAN 25
Pow
er
Consum
ption
Line TPH Before After
Power Consumption Vs Line TPH
Results
Annual Power Consumption
4167
2458 2356 2247 2314 2245
APRIL TO NOV
DEC JAN FEB MARCH APRIL
Pow
er
Consum
ption
(kW
h)/
Da
y
Months FY-16
Colling After Galvanization BlowerInnovation Project and Case Study-
4.Innovative Projects Implemented
Total Energy Saving of 676.16 GCal/A. Energy Saving of Rs 43.7 Lac/A
FY Total Power (MU)
RPO TARGET REC PURCHASEDValue Rs LacSOLAR
NON SOLAR
SOLARNON
SOLAR
FY 16 72 364 6196 379 6442 109
FY 17 84 847 8469 868 8431 156
FY 18 84 1671 8771 1671 8771 118
TOTAL 240 2882 23436 2918 23644 383
29
Roof top Solar Power
Project has finalised to install 1500 kWp roof top
solar power system in FY-19
4.07 Lac Units Solar power purchased through Open access from M/s Modern
India
Use of Transparent
Sheet for natural
lighting in plant
Installation of Root Top
Solar Panels JVM
School
Roof top Solar Power
School
Renewable EnergyInstallation of 1500 KWp Roof Top
Solar Power system is on progress
Use of
ECO -VENTILATORRain Water Harvesting
Rain Water Collection From
Plant Shed
Capacity- 300 KL
Size- 10 M*10M*3M
5.Utilization of Renewable Energy Sources
30
SOLAR ROOF TOP SURVEY
5.Utilization of Renewable Energy Sources
31
Year Name of Fuel Quantity Used
(MT)
GCV
(KCal/Kg)
Energy Utilized
Gcal/Year2015-16 Paint Solvant 3240 7000 22680
2016-17 Paint Solvant 3892 7000 27244
2017-18 Paint Solvant 3988 7000 27916
22680
27244
27916
20000
21000
22000
23000
24000
25000
26000
27000
28000
29000
2015-16 2016-17 2017-18
Weast Energy Utilized Gcal/Year
6.Utilization of Waste Material
32
91.6
72.4
84.5
15-16 16-17 17-18
GHG Emission Scope-1 (Kg Co2 /Ton)
0.56
0.59
0.57
15-16 16-17 17-18
GHG Emission Scope-2 (Kg Co2 /Ton)
Installation of RTO
Tree Plantation
Installation of WHR Boiler
7. GHG Inventorization
33
Facilitate a railway yard in premises for cost and Energy
efficient transportation of finish goods and raw material.
Total material transported through train- 70000 MT/Month,
Reduction in cost of transportation w.r.t. Road-100 Rs/T
Saving in transportation cost – Rs 70 Lacs/Month
Reduction in Energy consumption -30.3 Gcal/Month-KM(@ 8.2 KWh/1000T-KM by Train and @ 0.04 Ltr/T-KM by road Source-irfca.com)
Procurement of Energy Consuming Products based on Life
Cycle Cost and considering most Energy Efficient Product
Install RLNG line from GAIL station to convert fuel type from LPG to RLNG, to reduce transportation cost and wastage of fuel during loading and unloading. Also the cost of RLNG is cheaper then LPG.
(Total Production 4.45 Lac/Annum ,Saving on Fuel cost 199 Rs/T,
Total Saving – Rs 881 Lac/Annum)
PR To Payment Total Paperless Invoicing
8. Green Supply Chain
34
You shall comply with the Business
Responsibility/Sustainability policies of JSW
Steel Coated Products Limited which can be
referred to on our website:
"http://www.jsw.in/companies/Sustainability_P
olicy.shtml"
We expect our supplier to be in line with JSW
Vision, Mission & Values to achieve common
goal of the Organization.
Vision: Nurture Leadership in Coated
Products by Creating Value for Stake Holders
in Environmentally Sustainable Way
Mission: Supporting India's growth in core
economic sectors with Speed and Innovation
Values:
Transparency, Strive for Excellence,
Dynamism & Passion for Learning.
We are an ISO 9001:2015 company. We
take utmost care of our environment. We
encourage our suppliers to have QMS and
EMS certification, please inform us if you
need any type of assistance in the
process of certification. Please help us to
save our environment
Communication Through Purchase order-
Regular engagement with different stakeholder groups forms an integral part of our business
strategy. With best of our efforts, we strive towards transforming our stakeholder engagement
into an active two-way dialogue.
We strive to be a responsible corporate citizen and conduct our business with this aim in mind.
Our policies are based on the ideology of maintaining transparency and openness in the
Management and Board dealings. Our executives contribute to the ideologies and work towards
embedding robust corporate governance principles in their practices. Cutting edge technology
combined with our application and customer service skills help us to create value for all our
stakeholders.
With growing scarcity of primary and non-renewable sources of energy, we are striving
to minimize our energy consumption through process optimization and energy
conservation initiatives while deploying new technologies.
Since inception, we have consistently aggregated competencies from diverse cultures,
educational backgrounds and domain experience with a singular objective: to accelerate growth.
We reinforced this focus through an institutionalized multi-hierarchical training extending from
steel manufacturing to holistic personality development which commences from day one of
employment, followed by specialized trainings at regular intervals.
We strive to maintain the highest standards for the safety and wellbeing of our employees which
minimize injuries and casualties during day-to-day operations. Our safety team conducts regular
training programmes to instil the concept of maintaining safe operations among our employees
and to educate them on the safety norms and procedures to be followed in case of any incident.
The JSW group believes in the policy of ‘People First’ and the objective of our activities is to
make a tangible difference in the lives of the people in the areas surrounding our operations. As
a responsible organization, we are committed to investing a minimum of 2 percent of our PAT
towards community development. Employees are encouraged to contribute upto 40 hours
towards community development activities per employee per year.
Promoting on a wider platform The JSW Earth Care Awards is aimed at highlighting action of
direct relevance to tackle challenges posed by climate change. The award extending over
SAARC region is for excellence in climate change mitigation and adaptation.
JSW is fundamentally committed to sustainable business and the 9 principles of National
Voluntary Guidelines on Social, Environmental and Economic Responsibilities of Business
(NVGs) it has been pursuing in spirit while at JSW Steel Limited reporting on GRI framework
assured by third party independently (since FY 2005) on International Standards for Assurance
Engagements (ISAE) 3000. The policies in the context of these principles are Board approved
and a Committee of Board comprising 3 Independent and 3 Executive Directors is overseeing
the same, quarterly. CSO structure implements the sustainability oversight reporting.
All of us at the JSW Group are committed to live by these tenets.
Corporate Citizenship at JSW
Supplier Meet
8. Green Supply Chain
35
Engagement With Stack Holders
Installed 400
Nos LED
Street Lights
in Vasind
Village
Distribution of Energy
Efficient 2500 Chulha
in Near By Villages It
is High Efficiency and
Low Smoke Generate
Energy Awareness and Recognition to Employee and Society.
8. Green Supply Chain
Energy Management System (EMS)
• The EMS is On-line real time measuring
system, captures data from 170 nos.
Digital power & RLNG 7 meters.
• Unit wise online
reporting.
• Unit wise average power
consumption as required.
• Diagnostic facility available for any
interruption in system.• SAP Integrated.
• Facility to analyse
variable.
9. Team Work, Employee Involvement & Monitoring
Management of energy conservation programs
Energy Policy Board Displayed Awareness sessions
ISO 50001 Energy Review, SEU , EnPI
Annual Objective EC--> COC→ OPCOM→ Individual KRA
Review SPICE, Daily, Weekly, Monthly
Reward Quiz, Suggestion, Slogan, Best performer
Benchmarking Processes, Practices
Training Internal, External, Technical, EnMS trainings
Audits Internal Cross location audits, External Audits
Monitoring Power & Fuel consumption Monitoring through EMS
Review
Safety Systems, Compliance & Governance
People
Customer Delight
Energy, Environment & Safety
S
P
I
C
E
Innovation & Quality Management
ISO Audits
Audit
BEE Energy
Audit
External
Audits
Energy Conservation Awareness
Society
2250 Nos. Energy Efficient Chulla Distribution
40 Nos Solar Street lights in near by Villages
2500 Nos LED Bulbs distributions
Auditors Training,
Awareness
Technical Trainings (Drive/ PLC/ automation
In House Trainings
Trainings
9. Team Work, Employee Involvement & Monitoring
Energy Conservation Target Setting & Monitoring
38
Management
Commitment
▪ Appointment of MR, Scope &
Boundaries
▪ Energy Management Team – 10 Nos
▪ Establishment of Energy Policy,
Resources
Assess current
situation
▪ Energy Review, Base Line calculation
▪ Power chart preparation
▪ SEU identification:JJ-EnMS-PR-01
▪ Upcoming Energy conservation
measures
Goal Setting
Implementation Monitoring Review
▪ Monthly review in EC/COC/OPCOM bytop management
▪ Monthly review by EMT ▪ CAPA preparation for deviation
▪ SPICE based goal from topManagement.
▪ Prioritizing Opportunities▪ Objectives & Action Plan▪ Verification Plan- EMT
▪ Process Owner▪ Action plan and monitoring of
energy Targets▪ Review Metering Plan▪ Energy conservation projects
▪ Daily energy consumption monitoring
through EMS▪ Calibration of measuring Equipment▪ Audits▪ Energy conservation projects
PLAN
CHECK DOACT
9. Team Work, Employee Involvement & Monitoring
Budget Allocation and Review Meetings
Energy Conservation Measures
for FY 18
Budget
Allocated
(Rs Lac)
CGL #2 Line Fix Power Optimization by increasing Line Speed from 150 to 200 MPM .
312
CGL #1 Line Fix Power Optimization by increasing Line Speed from 120 to 150 MPM
0
Induction oven output optimisation for CCL PPGI material 0
Closed loop speed control ofCGL#2 APC Blowers by using VVVF drive
6
Installation of LED Lights 5.2
New Energy Efficient Pump(7.5 kW) Installed at ARP 1.8
Provision of local burner at CCL-1 oven to reduce fuel consumption 200
DOL Starters replaced with VFD at Pickling Recirculation pumps and optimized energy consumption by reducing speed to 1075
1.2
Old motor of 11KW replaced with IE-3 efficiency 7.5 KW motor 0.25
Total 326.4
RPO Compliance
Solar REC
(Nos)
Non Solar
REC (Nos)
Budget
(Rs Lacs)
1685 8846 202
Review Meetings
9. Team Work, Employee Involvement & Monitoring
Review by HOD & EnMS
M.R. with Energy
Management Team (10 Nos)
MONTHLY REVIEW
Review by Plant
Head with all HOD's
Review by
Departmental Head
with Energy Team
DAILY REVIEW
Review at Director level in
EC Meeting
Review at President level in
COC Meeting
Review at Plant Head level in
OPCOM meeting
Fig 8
40
150
357
450
0
100
200
300
400
500
FY 15-16 FY 16-17 FY 17-18
No. of people trained
5
1416
25
7
0
5
10
15
20
FY 16 FY17 FY 18
No. of Energy training
No. of In house Training External Trainings
Awareness & Involvement of Employees in Energy Conservation programme
Contd….
9. Team Work, Employee Involvement & Monitoring
Energy Exhibition Mega Quiz
Slogan
Awareness & Involvement of Employees in Energy Conservation programme
9. Team Work, Employee Involvement & Monitoring
42
Steel Coated Products Ltd.
Energy Policy
We are committed to efficient utilization of all types of
energy. We shall achieve this through continual
improvement in energy performance by:
• Monitoring and controlling consumption of all types
of energy.
• Setting energy conservation objectives and targets
and provision of information and resources for their
implementation.
• Purchase of energy efficient products and services.
• Use of energy efficient designs in new, modified and
renovated equipments and processes.
• Comply with all applicable legal and other
requirements related to energy use, consumption and
efficiency.
• Reviewing Energy Policy, Energy Objectives &
Targets annually and updated as necessary.
We shall encourage use of renewable energy and
promote awareness of energy conservation among
persons working for and on behalf of our organization.
Date : 01.11.2015 Dileep Bhatt Revision No. 5 President
10. Implementation of ISO
QMS 9001 2015
EnMS 50001 2011
OHSAS 18001 2007
EMS 14001 2015
I
S
O
FY-18
Turn Over - 2867 cr
ENCON Spent – 8.52 cr
43
Using advance Technology PLTCM First in Maharashtra, Estimated Energy Saving of 42792 Gcal/A .
Achieved 1875 ESCerts in PAT-1 and already achieved 0.042 MTOE/T by FY-18 in PAT-2
Total 29 Energy Conservation Measures completed.
Total Energy Saved- 27673 Gcal, Rs 1417 Lac.
Total 9004 Tons CO2 Emission reduced by reducing Energy Consumption.
Ro Installation of Roof Top Solar Power of 1500 kWp, Procured 4.07 Lac Solar Units & 100% RP RPO Compliance.
PLTCM
PAT
ENCON
Saving
CO2
Emission
Renewable
Energy
Highlights
CFBP – Council for Fair Business Practices Award-
2017
44
IMC RBNQA -2016Excellence Trophy
CII -2017Commendation
Certificate
MEDA 12th State Level EC Award
Awards….
45