SPE-139493-MS
description
Transcript of SPE-139493-MS
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Emergency Severance of Casing for Deepwater Operations: A Design Build and Test Programme of Novel Technologies N. Richmond, N.J.S. Bamford A.S. Bamford, SPE, Geoprober Drilling
Copyright 2011, SPE/IADC Drilling Conference and Exhibition This paper was prepared for presentation at the SPE/IADC Drilling Conference and Exhibition held in Amsterdam, The Netherlands, 13 March 2011. This paper was selected for presentation by an SPE/IADC program committee following review of information contained in an abstract submitted by the author(s). Contents of the paper have not been reviewed by the Society of Petroleum Engineers or the International Association of Drilling Contractors and are subject to correction by the author(s). The material does not necessarily reflect any position of the Society of Petroleum Engineers or the International Association of Drilling Contractors, its officers, or members. Electronic reproduction, distribution, or storage of any part of this paper without the written consent of the Society of Petroleum Engineers or the International Association of Drilling Contractors is prohibited. Permission to reproduce in print is restricted to an abstract of not more than 300 words; illustrations may not be copied. The abstract must contain conspicuous acknowledgment of SPE/IADC copyright.
SPE/IADC 139493
Abstract
In deep-water, emergency disconnection while running casing, is the action of last resort. It requires the casing to be sheared
and the well bore sealed. In an 18-3/4" BOP cutting casing sizes of 9-5/8" and above can be difficult and may impinge on the
bore of the BOP.
An Annular Cutting Tool (ACT) has been developed that can be implemented inside an API housing, spool piece or an
extension to a BOP ram body. The ACT has been designed to work with conventional drill pipe blind rams. The cutting
mechanism is swarf free and produces a good quality cut for later re-entry to the well.
After engineering design, a prototype tool to cut 7-5/8" casing was developed and tested. The system in its current state of
design, uses a rotating plenum driven by a sealed bevel gear cartridge, with six elliptical pistons each incorporating a cutting
wheel. The paper will describe the selection and testing of bearing and seals and how the drive and control system was
optimised to cut the casing in less than 45 seconds required by API RP 53. The effects will be illustrated of varying system
rotational speed and applied pressure to the cutting wheels.
Plans for future testing are described including; the effects of varying pipe grade, wall thickness, and casing load conditions
consisting of different combinations of tension and bending.
The ACT design has to ensure that there are two physical blocks between the wellbore pressure and the external seawater
environment; each of these blocks is independently tested.
Introduction
When drilling from a dynamically positioned vessel in deepwater, emergency disconnection
of the well requires shutting in the well and disconnecting the riser. API RP 53 requires that
this is carried out within 45 seconds.
With drill pipe or casing in the wellbore, this requires blind shear rams or casing rams to be
positioned in the subsea BOP stack. Figure 1 shows a typical deepwater subsea BOP stack
arrangement showing the position of these rams.
For large diameter casing, where there is a small clearance between the bore diameter of the
BOP stack and the casing this is a particular problem as ram type shear blades cannot operate
very effectively. For example shearing a 16 casing inside an 18-3/4 subsea BOP leaves
virtually no space for the shear blade to operate since the elongated sheared pipe cannot fit
inside the bore of the BOP. Generally, a tubular will flatten during shearing to a width equal
to about 1.51 times its diameter (experimentally derived) (West Engineering Services 2004).
If this is wider than the blade, shearing is jeopardized.
The Annular Cutting Tool can be implemented inside a subsea BOP to sever the casing with
no distortion. It can be placed in a housing that is an extension of the shear ram BOP and
replace casing shear rams; this reduces the BOP stack up height. Before severing the casing in
Figure 1: Typical deepwater subsea BOP stack showing possible location of ACT
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an emergency, it should be spaced out so that the casing collar or connector is landed out on the pipe rams and adequate
tension applied to the string at the surface to ensure that the cut is always made in tension.
The current technology development programme is part of a project sponsored by Statoil to develop a Drill-in Wellhead
System (the GEO-DWS). This is an exploration only wellhead system that allows a well to be established in a single trip. The
surface casing is drilled in and cut at the seafloor using the ACT and then sealed to the wellhead. This system will prove the
technology before implementation in a deepwater casing cutting tool.
System Overview
The ACT is a rotary pipe cutting tool which can be implemented inside a high-pressure housing. It consists of eight
subassemblies; the plenum, the cartridge and six identical elliptical pistons with cutting wheels. The prototype tool is
illustrated in figure 1. The housing for the tool could be configured as part of a subsea BOP stack up (see Figure 1).
Plenum
The plenum consists of a large thick walled ring. It contains six precision machined elliptical slots to fit the elliptical pistons.
On the bottom face of the plenum a bevel crown gear is held on by a series of pins and threaded studs. This gear meshes with
the bevel pinion of the cartridge assembly and transmits torque from the motor to the plenum.
Elliptical Pistons
Located within the wall of the plenum are the six elliptical pistons. Each piston includes a cut out, within which sits a cutting
wheel. Each wheel (or blade) is held in place via a pin and is therefore free to rotate around its own central axis. The pistons
travel along the radius of the plenum. Therefore extruding the pistons indents the cutting wheels radially into the casing (see
figure 3).
Cartridge The cartridge assembly consists of an integrated pinion gear and shaft and a housing cartridge. The shaft is coupled to a
hydraulic motor and the whole assembly is located within the wall of the housing. The pinion meshes with the crown gear of
the plenum assembly. This transmits torque to the plenum, causing the wheels to orbit the casing.
Figure 2: 3D images of; the prototype tool assembly within sample test housing (left) and plenum assembly, including elliptical pistons (right)
Figure 3: Elliptical piston assembly including cutting wheel (left), view through bore of tool post-disconnection (middle) and cartridge assembly with attached motor (right)
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Cutting Mechanism
The tool operates by indenting a series of hardened steel cutting wheels radially into the outer surface of the casing. This
deformation can be likened to the brinell hardness test, in which a ball bearing is pressed into a piece of steel under a
controlled load; the hardness of the test piece is then found by evaluating the contact area between the ball and the indented
profile at the point which prohibits further plastic deformation. In the case of the ACT, the contact area between each cutting
wheel and the casing is kept below this critical level. Therefore the wheels are able to indent the casing to a depth greater than
the wall thickness of the test piece, thereby completing a successful severance.
A purely linear penetration of the cutting blades radially into the casing would result in an increasing contact area based on
their respective geometries and the depth of penetration. However, during operation, the wheels are also forced to orbit the
casing via a bevel gear arrangement and hydraulic motor. Combining these two directions of travel of the blades causes them
to follow a spiral trajectory through the casing wall. This rotation ensures the indented profile is steadily progressed around
the entire circumference of the casing, thereby optimizing the contact area to intensify the plastic deformation.
This method of cutting implies that work hardening of the material occurs at the cut surface; therefore the rate of penetration
may decrease towards the end of the cut.
The principal feature of the cutting tool is that no cuttings are created during its operation. This is a result of the indentation
method of cutting. Emitting no swarf during severance procedures ensures that the wellbore environment is not contaminated
post-disconnection.
The second advantage of the cutting tool over other disconnection methods is the resulting cut profile. This has been observed
to have very little deformation to the inner and outer diameter of the casing. This allows for simple re-entry to the well, and
eliminates the need for any time consuming and costly milling procedures that are commonplace when removing the crimped
stub created when disconnection is carried out using shear rams.
Figure 4a: Close up view of upper cut surface Figure 4b: Bore of Tool post-disconnection
Figure 4c: Top and bottom surfaces placed side by side
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Wellbore Sealing/Well Integrity
The tool requires torque to be transmitted to the plenum through the high pressure housing. A solution that was explored
which could potentially have allowed us to avoid a penetration is a magnetic coupling. This system does have a service history
within the industry, however preliminary design work showed that currently available magnetic couplings are not a feasible
solution. In order to meet space requirements significant material would have to be removed from the outside of the housing
causing areas of stress intensity which would reduce structural strength and fatigue performance.
One of the requirements of the ACT is that it must seal wellbore pressure. However this is only after a cut has been
completed; therefore there is no situation in which it must seal full wellbore pressure and cut simultaneously. This statement
has led us to a sealing concept in which the seals must be capable of holding hydraulic system pressure whilst rotating and
subsequently hold wellbore pressure statically. From this the cartridge concept was developed:
This system allows torque to be transferred along the shaft of the pinion. The pressure envelope integrity is maintained using
rotary seals between the shaft and the cartridge, and a static seal between the cartridge and the wellhead. The cartridge
assembly is secured to the wellhead with a bolted flange. The pinion shaft is kept concentric by back-to-back tapered roller
bearings, preloaded with a nut which is prevented from backing off using an anti-rotation washer.
In addition to the rotation a hydraulic force must be applied to the back of the pistons in order to drive the blades into the
casing to perform the cut. This requires two further sealing systems: rotary seals on the plenum and sliding seals on the
pistons; both must hold hydraulic system pressure from the inside whilst cutting and wellbore working pressure from the other
direction whilst static.
In order to be considered a true wellbore barrier by Norsok D-010 and industry standards, a second block element in the form
of an isolation valve is added to the two motor hydraulic lines and the single plenum pressure line. These are attached to the
outside of the housing using a standard flange and gasket arrangement. This isolation valve can be a commercially available
fail closed gate or ball valve; for the wellhead version of the annular cutting tool development work is currently being
undertaken to source an isolation valve that minimizes the footprint of the tool.
APPENDIX-A shows the well integrity schematic for the wellhead version of the Annular Cutting Tool, it can be clearly seen
that two wellbore sealing requirements are through the plenum pressure gallery and the motor. Well integrity is implemented
in the first instance by the non-metal seals which are backed up by wellbore isolation valves.
Figure 5: Section view of cartridge assembly with mounted motor
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Design and Development
The annular cutting tool has been developed over a number of years. A logical progression has been followed from proof of
concept to the cutting tests. The various issues encountered throughout the development have been addressed.
Proof of Concept
A requirement to be able to sever casing without deforming the casing dimensions was identified during the concept design of
the Geoprober Deepwater Exploration Drilling System. Extensive research into non-mechanical methods of cutting pipe was
carried out. These methods involved using a chemical based cutting tool or even an arrangement of thermal torches. Although
testing of these methods was carried out, it soon became evident that due to the nature of the propellants used in both methods,
a mechanical solution was more appropriate.
The initial design concept was heavily based on a conventional plumbers pipe cutting tool with cutting wheels rotating around
the pipe under load. This concept requires power to drive the cutting wheels round and into the casing material.
To prove the concept that drill casing could be cut using a series of cutting wheels a manual test was carried out. This test
involved hiring a hinged pipe cutter and using it to cut a piece of 7-5/8 (33.7 lbs/ft) L80 API casing manually. This test was
successful, the final cut profile was clean and no cuttings were emitted during the process. However it was found that the
torque required to drive the tool was excessive.
The torque required to cut was crudely quantified at 590Nm for a four blade tool. Although the proof of concept test was
successful, cutting the pipe took over an hour. Attempts to speed this up failed as the increased loads damaged the cutting
wheels rendering them useless.
It was then decided to follow up this proof of concept test, with the design and build of an automated prototype tool. The
initial concept involved using a hydraulic motor via a straight bevel gear to rotate the cutting wheels around the pipe and
hydraulically energized pistons, to drive the cutting wheels against the pipe.
Blade Selection
In attempts to speed up the manual pipe cutting tests the original cutting wheels were found to be unsuitable and could not
withstand a load above 6.867kN. Although a cut was successful using these blades, it was necessary to reduce the total time to
cut pipe. To do this it would be required to increase the load on blades, therefore new blades had to be sourced.
A manufacturer of standard cutting wheels was contacted and it was learned that a stronger blade designed for cutting heavy
wall steel, was readily available. Some basic tests (same as proof of concept) using these blades showed that they were
suitable to cut the casing. Attempts to further speed up the cut were carried out and the blades were found to be capable of
withstanding much larger loads than the original blades provided.
Therefore it was decided to carry on the design using the stronger blades.
Future development of the tool will involve up scaling to cut larger diameter casing. To do this wheels with larger diameters
will be required. The manufacturer has been consulted on this and currently there are no off the shelf products available.
Therefore potential development could be carried out in designing custom cutting wheels.
Piston Design
To house the cutting wheels a simple bucket style piston was designed (see Figure 3). The wheels were held in place by a
retaining pin, allowing them to rotate around their central axis. This pin and the hollow which encased half of the wheel were
designed based on the dimensions of the off-the-shelf blades.
Figure 6: Hinged pipe cutting tool
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The working area of these pistons was sized based on a rough measurement of normal load applied to the blades. This was
measured by constructing a bracket for the hinged pipe cutter to hold a compressive load cell. The pipe cutter handle was then
turned until the torque required to cut (590Nm) could be applied by hand. The load cell then showed that the pipe cutter was
applying a normal load of 1400kg to the blades.
In line with sealing capabilities it was deemed appropriate to maintain a relatively low pressure to provide the normal load.
This was because, while this load was being applied, the tool and therefore the seals would be rotating; hence a lower pressure
would simplify the sealing process. The piston working area and hydraulic pressure were then optimized to give the required
load. The final piston working area was chosen at 2940mm2.
These pistons were housed within a thick walled ring (see figure 2); the thickness of the housing was dependent on the
required through bore of the tool and the necessary travel of the pistons to complete a cut.
It was important to maintain the correct alignment of the cutting blades within the cut groove. Therefore a circular shaped
piston was unsuitable, as it may twist. In line with basic sealing requirements no sharp edges could be included on the piston,
as this would damage the seal. These constraints led to an elliptical shaped design (see figure 3) to ensure the piston could not
rotate and to provide the minimum bend radius required when installing seals.
Machining these pistons was a difficult procedure due to the complicated tolerances involved with the sealing requirements of
the piston. Therefore all pistons and slots within the housing were machined at a specialist machine shop. This meant they
could be matched to fit before being sent back. For the first cutting tests three pistons were machined which meant three blades
were used to cut. After the cutting tests it was decided to increase this to six pistons this would enable further testing to be
carried out on the effect on cutting time by increasing the number of blades.
Seal Selection
Since it was decided that the tool would be hydraulically powered it was then necessary to design a sealing solution. Due to the
disconnection procedure philosophy, it was clear that the seals would have to statically withstand wellbore pressure once a cut
was complete. The seals must also be able to withstand a lower pressure during the tools operation (i.e. while rotating or
sliding respectively). Due to the proposed deployment of the tool all seals had to be rated for sour service.
Six piston seals were required for the elliptical pistons. For these circular piston seals were sourced with the same
circumference as the elliptical shape, it was then possible to stretch the seals over the piston. It was also recognised that two
rotary seals would be required to seal the annulus behind the elliptical pistons. These were sourced from the same company as
the piston seals.
Once the test setup was machined and the seals installed, a pressure test was carried out to prove that the seals could hold 1.5
times wellbore pressure. All seals passed this test. A second pressure test was carried out to prove the rotary seals could
withstand operating pressure while rotating. This test was also passed.
In the early stages of the tools design the main sealing concerns were as detailed above. However as the design progressed, a
sealed cartridge was required to allow torque to be transmitted to the plenum while maintaining a pressure envelope. This
required a small diameter rotary seal between a rotating shaft and the bore of the static cartridge and a slightly larger static
shaft seal between the cartridge and the test housing. These seals were again tested to 1.5 times wellbore pressure this was
repeated ten times. Between hold periods the shaft was spun for one minute at 150RPM. No significant drop in pressure was
observed across any of the hold periods of the tool therefore the seals selected were labeled fit for purpose.
Bearing Selection
Since the tool contains a steel plenum rotating within a steel housing, a reliable bearing solution was required to prevent
galling. The first method used was a set of PTFE bearing strips. These were located within grooves above and below the
seals.
Figure 7: Hinged pipe cutting tool with attached load cell
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During installation it was found that these grooves were unsuitable and that locating the
bearing strips while installing the plenum within the test housing was difficult. This
bearing solution was used for the cutting tests, the strips were glued in place to stop
them falling out. The cutting tests were successful and the bearing strips successfully
prevented galling. However it was recognised that further work was required to
simplify the bearing installation.
The second bearing solution explored used a solid brass bearing ring press fit onto a
shoulder on the plenum. Installation of this bearing was relatively simple. However
once the plenum was installed within the test housing it was found that the plenum
could not rotate due to the friction between the bearing and the test housing. Rather than
persevere with the solid bearing ring it was decided to upgrade the bearing to roller
bearings.
To reduce friction and ensure correct alignment of the plenum within the test housing a set of deep groove ball bearings were
selected. These were again press fit onto the plenum but used a sliding fit on the test housing. Installation of these bearings
was more complicated than the solid bearing ring as they had to be installed in the correct orientation. However once the
plenum was installed within the test housing, it was found that it could be rotated by hand. Therefore this solution was
selected as the most appropriate for the tool.
Drive System
To drive the plenum a motor and gear design was required. It was estimated, using similar methods as the proof of concept,
that a torque of 1050Nm was required to drive the plenum. This included cutting torque and a conservative estimate of all
resistive friction involved in turning the plenum.
To achieve this torque a straight bevel gear arrangement was decided upon to
allow rotation to be transferred through 90. This allowed the motor to be
mounted to the outside of the test housing. The arrangement would consist of a
crown-mounted gear on the plenum and an integral pinion and shaft coupled to
the rod end of a hydraulic motor. The gears used for the cutting tests had a ratio
of 4:1 between the pinion and crown. The safety margins on these gears were
relaxed due to space requirements within the tool. The gears were manufactured
and used during the cutting tests, no problems were encountered that could be
accredited to the gears.
During further development of the tool involving its placement within a
wellhead, the decision was taken to revisit the design of the gears particularly the
crown gears mounting onto the plenum. By changing the gear to a thicker
section and including a mounting procedure using threaded studs and spring pins
in the back face of the crown. It was possible to increase the face width of the
gears; this allowed the safety margin to be restored in their design. The new gears
have a ratio of 40:7.
This wellhead arrangement also included overhanging the crown gear onto the pinion to allow the tools protrusion through the
wellhead to be closer to the seabed. Therefore to set the mounting distance from the back of the crown to the centre of the
pinion, a series of tight tolerances were required as the plenum could not be shimmed back. The mounting distance from the
back of the pinion to the centre of the crown could be set by shimming.
Selecting a gear ratio meant that a torque rating could be chosen for a drive motor. It was decided to allow a range of torques
to be tested to see what could be used to perform the fastest cut. After consultation with a manufacturer a low speed/high
torque orbital motor was acquired. This included a 25mm straight keyed shaft, 1/2 BSP
hydraulic ports and a two bolt mounting arrangement. This then allowed a motor
mounting bracket and a shaft coupling mechanism to be designed.
Shock Absorber
During system shakedown of the tool it was noticed that once the blades had broken
through the inner diameter of the casing the pressure sensors were reading aggressive
fluctuations in plenum pressure. It was observed that as the breakthrough point
propagated circumferentially around the casing, any blades passing the broken through
section would be forced into their fully extended position. This caused a sudden
expansion of hydraulic volume (pressure drop). Once the blade had passed the broken
through section it was forced by the casing groove to retract causing a sudden contraction
of hydraulic volume causing a pressure spike in the region of 10bar.
Figure 8: Flat hacksaw blade bridging between the bearing strips
Figure 9: Crown gear design as used in cutting tests
Figure 10: Image of blades protruding through casing
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These fluctuations meant that the operator could not accurately monitor the plenum pressure, and the system was prone to
stalling. To counter this issue a 320ml diaphragm shock absorber pre-charged to 15bar was introduced to the system. The
flexibility of the diaphragm absorbed the pressure spikes and damped the fluctuations to amplitudes of below 5 bar (see Figure
10) making the control system easier to work with and prevented the system from stalling.
Once the cutting tests had been completed further design work was carried out on modifying the tool for subsea use. This
involved ensuring all components could function at operational water depth. As a result of this it was recognised that the
current shock absorber was not suitable for offshore deployment, as it could not be pressure compensated.
A custom shock absorber suitable for subsea use was designed in-house. This used the same principle of the fluctuating
volume being absorbed by the flexibility of the shock absorber. This flexibility was provided via a spring loaded piston open
to the plenum line-in. When the plenum pressure spiked, a load was exerted on this spring via the piston, this load caused the
spring to retract, allowing the volume of the piston to expand. Thereby absorbing the pressure spikes created during the tools
operation. This design allowed the back of the absorber to be open to the environment and was therefore naturally pressure
compensated.
Cutting Tests
Programme
A test procedure was devised to deduce the relationship between various system parameters and the total time to cut pipe.
These included the plenum pressure and system rotational speed. Other parameters that were considered were the number of
blades used to cut and the deterioration of the blades after they complete a series of cuts.
It was considered a prerequisite for the other tests to find how the number of cuts previously performed by a blade affected the
cut performance. A blade register could then be kept to allow a correction factor to be included with further test results based
on the number of cuts previously performed by the blades.
It was decided to test the relationship between the plenum pressure and the cut time. The system speed would be set at a
relatively low value (15RPM) and the pressure would be increased up to the maximum decided test value (55bar). From the
pressure value the load on blades normal to the casing can be found using the working area of a single piston.
It was also decided to complete a series of cuts with varying rotational speed whilst maintaining a constant plenum pressure.
Due to limitations with the hydraulic power unit it was necessary to maintain a lower plenum pressure (30bar) to allow the
velocity to reach its maximum test value (35 RPM). It should be noted that the system speed is representative of the load on
blades tangential to the casing. This load could be evaluated by measuring the pressure drop over the hydraulic motor and the
motors rotational speed; these could be used to find the motor torque, which could then be combined with the gear ratio to give
the plenum torque. The plenum torque could then be combined with the elliptical pistons stroke length at any point during
operation to give the total load on all blades. This could then be divided by the number of blades to give the load on a single
blade tangential to its orbit.
Figure 11: Damped plenum pressure readings for a six blade cut
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One idea for the tools further development was to show the effect of increasing the number of blades used to cut from three to
six. A simple method of measuring this relationship was to carry out tests using one to three blades, while keeping all other
parameters constant. The relationship could then be plotted graphically and the effect of six blades could be extrapolated from
the results.
One issue with carrying out the number of blades test was that the tool requires a symmetrical orientation of blades. This is
necessary to ensure the radial loads exerted outwards on the plenum by the contact with the casing are balanced. Therefore it
was not possible to simply remove cutting wheels from the pistons; instead a pair of rollers were designed and manufactured to
maintain the load balance when cutting with less than three blades.
These rollers were designed to fit into the same hollow within the elliptical pistons as the cutting wheels. They also featured a
groove which ensured no contact would be made with the cut edge of the pipe. The contact area between the roller and the
casing was evaluated using an approximation of the hertzian contact stress between two cylinders (Shigley 2008). The load on
blades was then combined with this area to ensure no plastic deformation occurred to the casing as a result of the presence of
the rollers.
Once the structured test programme was complete it was decided to attempt to achieve a cut in less than 45 seconds. This
would involve increasing both the system speed and plenum pressure to the maximum that could be provided from the
hydraulic power unit.
To set the system parameters to their maximum, the tool was first set to rotate with no contact between the blades and the
casing. The flow restricting valve controlling the system RPM was opened to full and the maximum speed was recorded at
around 45RPM. Since both parameters were powered from the same hydraulic power unit, increasing the plenum pressure
whilst the RPM was at its maximum resulted in a drop in speed. Therefore it was not possible to test cuts across the total
range of system parameters
Equipment
The main test equipment as used during the cutting tests are as follows; the prototype tool including a steel test housing, a
7kW hydraulic power unit (HPU) connected to a set of hydraulic valves, a set of pressure sensors to monitor the pressure in
and out of the motor as well as within the plenum, a magnetic gear tooth sensor to monitor the system RPM, and a desktop
computer with graphical programming environment software.
The data acquisition system allows the Graphical User Interface to be adapted quickly by the operator in accordance with
changes in test procedures, equipment and measurement priorities. Additional tests were carried out to prove the seals on the
cartridge; this required a dedicated pressure testing can.
Figure 12: Elliptical piston assembly with roller insert
Figure 13: Prototype tool being installed in test housing Figure 14: Cartridge pressure test can
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Results
Bluntness of Blades
To test this it was decided to repeat a cut with the same parameters six
times. The time to break through the casing and the total time to cut
were recorded and plotted using spreadsheet software. The plenum
pressure was kept constant across all six cuts at 30bar, and the system
speed was kept at 20 RPM. The same blades were used for all tests.
The results of the bluntness test series are shown in figure 15. No
significant variation in the cutting performance of the blade could be
found after six cuts. It was therefore decided that further test results
need not be corrected for the effect of blade bluntness. However it was
also decided that after six cuts all blades would be replaced to ensure
that none were used excessively.
Plenum Pressure
For this test the system speed was set at 15 RPM. The cutting wheels
were replaced and used throughout the entire test series. Six cuts were
made with increasing pressure from 30 to 55bar in increments of 5bar.
Figure 16 displays the results for the breakthrough and complete
cutting time of the plenum pressure test series. A significant drop in
both breakthrough and cutting time is seen for increasing pressure up to
45bar. For pressures higher than 45bar this decrease flattens off.
System speed
For these tests the plenum pressure was set to a constant 30bar, and the
system speed was increased from 5 to 35RPM in increments of 5 RPM.
Figure 17 depicts the results of both the breakthrough and complete
cutting time of the RPM test series. A decreasing slope in both can be
seen. After 20 RPM this slope flattens out and becomes more or less
constant. This shows that after an initial increase of RPM the gain in
cutting time becomes insignificant. It is noted that the missing data
points for complete cutting time at 5 and 10 RPM are due to the fact
that it was not possible to complete a cut at these settings. During these
tests the motor kept stalling and the tests were aborted after 15 minutes.
Number of Blades
For these tests the plenum pressure was kept at a constant 30bar
throughout the tests, and the system rotational velocity was kept at a
constant 20RPM. The cutting wheels were replaced with rollers and
cuts were made with 1-3 blades.
As expected it was found that increasing the number of blades, reduced
the total cut time (see figure 18).
Optimisation
A series of optimisation cuts were attempted by increasing the system
parameters to the maximum limit of the hydraulic power unit. The first
cut of this test series was successful and the casing was severed in 42
seconds. The cut was performed at 45bar plenum pressure and 35RPM
Further optimisation cuts were carried out with varied system
parameters, a 3D graph of breakthrough and cut times for all accepted
tests can be seen in APPENDIX-B.
Increasing the system speed above the plenum pressure meant that the
parameters were restricted to 35bar and 40RPM. This gave a
successful cut in 75 seconds. A cut was attempted with 50bar and
30RPM. This could not be completed at these settings as the motor
repeatedly stalled.
Figure 15: Results from bluntness tests
Figure 16: Results from Pressure Tests
Figure 17: Results from system speed tests
Figure 18: Results from No. Blades tests
Figure 19: Data for a 42 second cut
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However initial break-through of the casing was achieved in 32 seconds. It was then decided to increase the plenum pressure
further to 70bar and let the speed fall to 20RPM; again a cut could not be achieved due to motor stalling however the initial
break-through occurred in 22 seconds.
Discussion Pressure
The plenum pressure test series results can be explained by the development of the contact area between the blades and the
casing at a certain depth of penetration. Limiting the rotational velocity to 15RPM means that the blades were allowed to
penetrate further into the casing wall per degree of rotation. The contact area was therefore increased and further
improvements on cut time were not possible beyond 45 bar.
Due to the pre-decided test values no cuts above 55bar were undertaken. Testing beyond this pressure would allow the depth
versus rotation theory to be further tested, as at some depth of penetration at a low RPM, the indenting contact area may reach
the critical level at which plastic deformation can no longer occur. This would be recognizable by the motor stalling
RPM
The rotational speed test series results confirm the theory on the cutting mechanism. As it shows that above a certain ratio of
load on blade to system speed the system stalls. This is due to the depth of blade penetration per degree of rotation allowing
the contact area to reach the critical level at which plastic deformation cannot occur. It also shows that below a certain ratio
the cut time does not drop significantly. Therefore at these system speeds the cut time can only be reduced by further
increasing the plenum pressure, as the contact area is kept at its minimum.
Due to the pre-decided test values no cuts above 35RPM were undertaken. It would be beneficial to perform further RPM
tests to see if the cut time stayed at this constant, this would further prove the cutting mechanism theory. Also it may be
possible to perform a series of very low RPM and very low pressure tests, to prove that a cut is possible and that the motor
does not stall as long as the required ratio between parameters is maintained.
No. Blades
The results found were not considered sufficient to predict the cut time using more than three blades, as there were not enough
data points for an accurate linear approximation. Therefore it was deemed necessary to carry out further tests using up to 6
blades. For the next version of the tool it was decided to increase the number of blades to six to allow further testing of this
relationship to be carried out.
Optimisation
The first optimisation cut achieved complete casing severance in 42 seconds.
Setting the maximum possible system parameters for this cut highlighted the limitations of the test setup. During all previous
tests the hydraulic flow to the motor was restricted and therefore altering the plenum pressure had little effect on the system
speed. Once the flow restrictor was fully opened, the motor line-in was susceptible to the alterations made to the plenum
pressure. Also the nature of the tool requires that the system be set to rotate before the plenum pressure is applied. This meant
that achieving maximum system speed and load on blades was a delicate process.
As the first optimisation test cut in less than 45 seconds it was decided to carry on optimizing the cut performance instead of
proving the 42 second cut could be repeated. This involved experimenting with different system parameters. Cuts were
attempted using a lower plenum pressure to allow the system speed to be higher than 35RPM. Cuts were also attempted using
an increased plenum pressure while allowing the system speed to drop below 35RPM. Although not all tests yielded a
successful cut, these results further prove the cutting mechanism theory. When the load on blades was significantly higher
than the system speed the motor stalled. When the system speed was higher than the load on blades the cut time was affected
purely by the plenum pressure.
Conclusions and Recommendations
The tests showed that a complete severance of 7-5/8 casing could be completed in under 45 seconds with the tool. They also
suggest that this could be further improved, however in doing so the power requirements may increase excessively. Therefore
optimisation of the cut performance should be carried out in line with an assessment of the various loads exerted on the tool.
The results heavily support the cutting mechanism theory. Further tests should be performed to confirm the theory and define
the optimum ratio between the two loads acting on the blades. To carry out these tests it would be necessary to upgrade the
current test setup. The main upgrade would be to acquire a second hydraulic power unit. This would allow the system speed
and plenum pressure to be independent of each other and a wider range of parameters could then be tested.
To understand the cutting mechanism theory from first principles a method of finding the actual tangential load on the blades
should be found. The main problem to overcome with this is measuring the piston stroke throughout operation. A software
program could then be written which allows the user to maintain the appropriate ratio between load on blades normal to the
casing and tangential to the casing.
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Future Development
Dual Cylinder Arrangement
During the cutting tests it was found that the setup procedure between tests was laborious and time consuming. This was
mainly due to the fact that it was required to drive the elliptical pistons back by hand. During subsea operation the pistons
must be capable of automatic retraction to allow re-entry to the well. Therefore it was practical to design a system which
could be implemented to both the workshop test rig and the final offshore version of the tool.
A coupled dual cylinder arrangement was devised to be implemented outside the pressure housing as part of the control
system. This included two equally sized double acting cylinders with a coupling between their rod ends. The cylinders were
restrained within a u-shaped channel.
When hydraulic pressure is applied to the rod end of cylinder A the mechanical link between the rods causes the rod of
cylinder B to extend. The plenum pressure line is connected to the cylinder end of cylinder B. This means that a negative
pressure is established within the well causing the blades to be retracted. The system is designed to operate in at least 100m of
water where the hydrostatic pressure assists in retraction of the blades; however during workshop tests the blades were shown
to retract without this pressure.
To understand the cutting mechanism theory from first principles a method of finding the actual tangential load (caused by the
motor) on the blades should be found. The main problem to overcome with this is measuring the stroke of the elliptical
pistons throughout operation. This stroke could be combined with a cutting torque to find the tangential load on blades.
This dual cylinder arrangement allowed for a simple method of monitoring the penetration rate of the blades. The stroke
length of the elliptical pistons is proportional to the stroke length of the dual cylinder arrangement. The ratio between the
working area of one of the dual cylinders and the total area of all the elliptical pistons can be used to convert between the two.
A stroke sensor can then be mounted on the dual cylinder arrangement to monitor the extension of the rod end of cylinder A.
Further Testing
A second test program will be devised and undertaken. The scope of this will be to prove the reliability and the repeatability
of a cut performance of less than 45 seconds. This testing will also be more focused on proving the cutting mechanism theory.
Testing the full range of system speeds and plenum pressures will enable us to find the optimum ratio between the loads on
blades that will enable the fastest cut to be performed.
Testing into the effects of various casing conditions will also be undertaken. For differing hardness values of drill casing the
contact area which prevents plastic deformation due to a controlled load will change and therefore the ratio of loads on blade
will need to be adjusted accordingly.
A B
Figure 20: Dual Cylinder Arrangement
Figure 21: Plenum pressure readings during blade retraction process
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SPE/IADC 139493 13
In order to be adapted to cut different casing strings within the BOP stack several elements of the annular cutting tool design
must be improved and modified. First, adapted pistons must be designed capable of much further radial travel, this requires
either a thicker housing, which may be acceptable as part of a BOP stack, or the use of telescopic pistons. The cutting blades
currently being used are a commercially available product but the standard sizes are limited. Future work will concentrate on
Geoprober designing custom blades capable of cutting greater wall thicknesses; this will lead to optimisation of shape,
material selection and heat treatment specific to the application to provide the maximum reliability and performance.
For the operational load conditions on casing, it is currently believed that tension will assist the cutting mechanism and
therefore could result in a lower cut time. However the effects of this tension on the final cut profile are of interest to
Geoprober, and work on adapting the current test setup to accommodate tension cuts is ongoing. Once a range of tension cuts
have been performed a new test rig will be devised which will allow all casing offset variables to be tested. For example
fluctuating casing tension, bending moment and pipe offset. These are the main load conditions expected during offshore
operation.
Increased No. Blades Since the completion of the cutting tests a basic comparison between six blades and three blades has been carried out to prove
the linear relationship between cut time and number of blades. All other system parameters were kept reasonably constant
during this test. Although a difference in plenum pressures was recorded, these tests were considered comparable
Figure 22: Graph with plenum pressure readings for 3 blade and 6 blade cuts superimposed on one graph
The result of increasing the number of blades from three to six is evidently linear. A total time to cut for 3 blades was
approximately 140 seconds and for 6 blades was approximately 70 seconds. Therefore it is believed that in further six blade
tests when the plenum pressure and system speed are replicated for the 42 second cut, a 21 second cut should be achievable.
Conclusions
The prototype tool has clearly shown that mechanically severing casing in less than 45 seconds is possible. Therefore using the tool as a primary means of disconnection is feasible.
The results from the cutting tests support the cutting mechanism theory. This means more focused testing can be carried out in the future to further prove the theory and to define the optimum blade loads ratio which maximizes the
intensity of the plastic deformation.
Optimum cutting parameters can then be chosen based on the limitations of other components. Providing the fastest most reliable cut.
The fastest cutting time could be improved beyond 42 seconds, potentially by simply increasing the number of blades.
Future development into testing under tension and bending is required to gain a full understanding of the cutting process in real life conditions
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Unit conversion
Symbol When you know Multiply By To find symbol
mm millimetres 0.039 inches in
mm2 square millimetres 0.0016 square inches in
2
mL millilitres 0.034 Fluid ounces fl oz
kg kilograms 2.202 pounds lb
N newtons 0.225 pound force lbf
bar bar 14.5 Pounds per square inch PSI Table 1: Unit conversion factors
Acknowledgements
GDL would like to thank Statoil for their support in the development of the Annular Cutting Tool. We especially thank Scott
Kerr and Glenn Gabrielsen for their involvement with the project.
GDL would also like to thank Neptune Deeptech, for their services during the cutting tests and the ongoing work on the
prototype tool.
References
Shigley. J.E., Budynas. R.G., Nisbett. J.K., Shigleys Mechanical Engineering Design Eight Edition, McGraw-Hill, NY, 2008, Section 3-19, page 119.
Nelemans, A. M. B., GDL09-01-0001-REP-ACT A.C.T. Phase 1B Test Results June 2009.
Verhoven. J. D., Steel Metallurgy for the Non-Metallurgist, The Materials Information Society, OH, U.S.A. , 200.7
Wasilewski, R. F., Power Transmission Design, How to Install Bevel Gears for Peak Performance March 1994.
West Engineering Services, Shear Ram Capabilities Study For U.S Minerals Management Service, Sept 2004.
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SPE/IADC 139493 15
APPENDICES
APPENDIX-A GEO-DWS Well Integrity Schematic
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APPENDIX-B Cutting Test Results