SIX SIGMA FOR SCRAP COST REDUCTION IN...

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SIX SIGMA FOR SCRAP COST REDUCTION IN REMANUFACTURING INDUSTRY MISSJULIANA BINTI MAT KIAH A project report submitted in partial fulfilment of the requirements for the award of the degree of Master of Engineering (Industrial Engineering) Faculty of Mechanical Engineering Universiti Teknologi Malaysia JANUARY 2015

Transcript of SIX SIGMA FOR SCRAP COST REDUCTION IN...

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SIX SIGMA FOR SCRAP COST REDUCTION IN REMANUFACTURING

INDUSTRY

MISSJULIANA BINTI MAT KIAH

A project report submitted in partial fulfilment of the

requirements for the award of the degree of

Master of Engineering (Industrial Engineering)

Faculty of Mechanical Engineering

Universiti Teknologi Malaysia

JANUARY 2015

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Specially dedicated to:

My beloved husband and son,

Mohd Zulkarnain bin Ab. Razak and Aiman Danish bin Mohd Zulkarnain

for their love and support

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ACKNOWLEDGEMENT

First and foremost, I would like to express my thanks to Allah S.W.T for His

Blessing and giving me strength to complete this project. The path from nothing to a

book of graduation is a challenging and tough experience for me. The experience of

the fulfilment of this project would not possible to happen without the help of my

very supportive supervisor, project team members, friends, and family.

My sincere and thousands of thanks to my project supervisor, Dr. Syed

Ahmad Helmi bin Syed Hassan for his enlightening supervision and countless hours

spent in sharing his insightful understanding, profound knowledge, and valuable

experiences in order to make sure my project is successfully completed. As a

supervisor, he has been a source of inspiration and courage towards the completion

of this project.

Thousands of thankfulness is credited to Dr. Tai Yiat Au for lending hands to

make this project success. I would also like to express my special thank you to my

family members for their generous understanding, priceless support, encouragement,

valuable advices, and unconditional love given to me. Last but not least, many

thanks to all my friends and to all people who have directly and indirectly involved

in making my research project successful.

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ABSTRACT

This project entails the adoption of Six Sigma Methodology in

remanufacturing industry. The improvement project is carried out at a service and

repair company for electronic product. Six Sigma is a set of quality management

tools and strategies, including statistical methods used for process improvement by

identifying and eliminating the causes of defects and reducing variability occurs in

manufacturing and other businesses process. The Six Sigma DMAIC methodology

consists of five phases which are Define (D), Measure (M), Analyse (A), Improve

(I), and Control (C) respectively. This case study focuses on implementing Six

Sigma methodologies into the motherboard repair process in to identify and

minimize the variation exists in the process and subsequently reducing the

associated scrap cost. As known, the original assembly process of motherboard is

comparatively straightforward. However, the repair process of malfunction

motherboard which requires troubleshooting of problem and replacement of

electronic devices can be much more complicated and often end-up scrapping the

whole set of motherboard itself. Realizing this great challenge, the DMAIC tools are

mounted in this study to solve the underlying problem stated. The objective of the

project is to reduce the overall scrap rate and to increase the sigma level of the

motherboard repair process. The existing scrap rate is 45.89% and process sigma

level is 1.84σ. It is proven that the method and tools chosen have successfully

reduced the scrap rate to 18.60% and increased the process sigma level to 2.46σ in

three months period after the improvement took place. This result indicates that Six

Sigma methodology is also applicable in remanufacturing industry as good as in

forward manufacturing industry.

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ABSTRAK

Projek ini melibatkan penggunaan Metodologi Six Sigma dalam industri

pembuatan semula. Projek perbaikan ini dijalankan di sebuah syarikat servis dan

membaiki produk elektronik. Six Sigma adalah satu set alat pengurusan kualiti dan

strategi, termasuk kaedah statistik yang digunakan untuk perbaikan proses dengan

mengenal pasti dan menghapuskan punca-punca kecacatan dan mengurangkan

kebolehubahan yang berlaku dalam industri pembuatan dan juga dalam sektor

perniagaan yang lain. Metodologi Six Sigma DMAIC terdiri daripada lima fasa

utama iaitu Define (D), Measure (M), Analyse (A), Improve (I), dan Control (C).

Kajian kes ini memberi tumpuan kepada perlaksanaan metodologi Six Sigma dalam

proses pembaikan motherboard untuk mengenal pasti dan mengurangkan variasi

yang wujud dalam proses dan seterusnya mengurangkan kos sekerap. Seperti yang

diketahui, proses pemasangan motherboard pada asasnya tidaklah begitu rumit.

Walau bagaimanapun, proses pembaikan motherboard rosak yang memerlukan

pengenalpastian jenis kerosakan dan penggantian alat-alat elektronik boleh menjadi

lebih rumit dan sering berakhir dengan pelupusan keseluruhan motherboard itu

sendiri. Menyedari cabaran yang besar ini, metodologi DMAIC telah digunakan

dalam kajian ini untuk menyelesaikan masalah yang dinyatakan. Objektif projek ini

adalah untuk mengurangkan kadar sekerap secara keseluruhan dan meningkatkan

tahap sigma proses pembaikan motherboard. Kadar sekerap yang sedia ada ialah

45.89% dan tahap sigma proses adalah 1.84σ. Terbukti bahawa kaedah dan

metodologi yang dipilih telah berjaya mengurangkan kadar sekerap kepada 18.60%

dan meningkatkan tahap sigma proses kepada 2.46σ dalam tempoh tiga bulan

selepas aktiviti perbaikan berlaku. Keputusan ini menunjukkan bahawa metodologi

Six Sigma juga boleh diaplikasikan dalam industri pembuatan semula sebagaimana

aplikasinya yang meluas dalam industri pembuatan biasa.

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TABLE OF CONTENTS

CHAPTER TITLE PAGE

DECLARATION ii

DEDICATION iii

ACKNOWLEDGEMENTS iv

ABSTRACT v

ABSTRAK vi

TABLE OF CONTENTS vii

LIST OF TABLES xi

LIST OF FIGURES xii

LIST OF APPENDICES xiv

1 INTRODUCTION 1

1.1 Introduction 1

1.2 Definition of Terms Used 2

1.3 Background of Research 4

1.4 Problem Statement 6

1.5 Research Objectives 7

1.6 Scope of Research 8

1.7 Significance of Findings 9

1.8 Organization of Thesis 9

1.9 Conclusion 13

2 LITERATURE REVIEW 14

2.1 Introduction 14

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2.2 Essential Terms 15

2.2.1 Quality 15

2.2.2 Total Quality Management (TQM) 17

2.2.3 Six Sigma Understanding 18

2.2.3.1 What is Six Sigma 18

2.2.3.2 Historical Perspective of Six

Sigma

20

2.2.3.3 Sigma as a Quality Measure 20

2.2.4 DMAIC (Define-Measure-Analyse-

Improve-Control) Approach

21

2.2.4.1 Define Phase 22

2.2.4.2 Measure Phase 25

2.2.4.3 Analyse Phase 27

2.2.4.4 Improve Phase 31

2.2.4.5 Control Phase 33

2.3 Previous Case Study 37

2.3.1 Case Study 1 38

2.3.2 Case Study 2 39

2.3.3 Case Study 3 41

2.4 Six Sigma in Various Industries 42

2.5 Conclusion 48

3 METHODOLOGY 49

3.1 Introduction 49

3.2 Research Framework 49

3.3 Project Methodology 51

3.3.1 Identification Stage (Define-Measure-

Analyse)

53

3.3.2 Categorization Stage (Analyse) 57

3.3.3 Optimization Stage (Improve) 59

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3.3.4 Standardization Stage (Control) 61

3.4 Conclusion 62

4 DATA ANALYSIS AND PROBLEM

IDENTIFICATION

64

4.1 Introduction 64

4.2 Identification Stage (Define-Measure-

Analyse)

65

4.2.1 Team and Project Selection 66

4.2.2 Measurement System Qualification 71

4.2.3 Data Collection and Defect

Prioritizing

78

4.2.4 Identifying Possible Root Causes of

Defect Occurrence

83

4.2.4.1 Cause and Effect Analysis 87

4.2.4.2 Analysis of Tooling Used in

BGA Rework Process

90

4.3 Conclusion 92

5 IMPROVEMENT AND COUNTERMEASURE

DEVELOPMENT

94

5.1 Introduction 94

5.2 Categorization Stage (Analyse) 95

5.2.1 Potential Improvement Actions

towards Solution

95

5.2.2 Establishing Significant Root Causes

and Actions towards Solution

98

5.3 Optimization Stage (Improve) 103

5.4 Standardization Stage (Control) 107

5.5 Conclusion 108

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6 CONCLUSION AND FUTURE

RECOMMENDATION

110

6.1 Introduction 110

6.2 Conclusion 110

6.3 Future Recommendation 112

REFERENCES 114

APPENDICES A - B 118-126

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LIST OF TABLES

TABLE NO. TITLE PAGE

2.1 Summary of the tools useable in DMAIC approach 32

2.2 Polycarbonate unit energy reduction project 38

2.3 Stream trap implementation project 38

2.4 Angus site energy reduction project 39

2.5 Six Sigma adoption in forward manufacturing

industry

40

3.1 Attribute agreement analysis execution sheet 48

3.2 Acceptance guideline for attribute agreement analysis 48

3.3 Procedure for designing an experiment 51

3.4 Details of project execution strategy 53

4.1 Acceptance guideline for attribute agreement analysis

used in the study

62

4.2 Attribute agreement analysis execution table 63

4.3 Visual inspection result for month of May ~ July

2014

67

4.4 Sigma level from May ~ July 2014 68

5.1 P-value of each factor 88

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LIST OF FIGURES

FIGURE NO. TITLE PAGE

1.1 Organization of thesis 10

2.1 Example of control chart 23

2.2 Example of fishbone diagram 25

3.1 Research frameworks for Master Project 2 43

3.2 Project methodology 44

3.3 Example of project charter for motherboard repair

process improvement

46

4.1 Pareto chart of scrap rate by product type 57

4.2 Project charter for motherboard repair process

improvement

58

4.3 Process flow diagram of motherboard repair process 60

4.4 Attribute agreement analysis result 64

4.5 Attribute agreement analysis graph (within

appraisers)

65

4.6 Attribute agreement analysis graph (appraiser versus

standard)

65

4.7 Trend chart of overall defects in motherboard repair

process before improvement

69

4.8 Pareto chart of scrap rate by rework process type 70

4.9 Pareto chart for defective rate of BGA rework

process

70

4.10 Three-layer tree diagram for project selection 71

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4.11 Detailed process flow diagram of BGA rework

process

73

4.12 Cause-and-effect diagram of lifted pad occurrence in

BGA rework process

75

4.13 Common tweezers used for epoxy removal 77

4.14 Iron tip and solder wax used for dressing of BGA

area

78

4.15 Common stencil used for solder paste application 78

5.1 Special fabricated SST tweezers used for epoxy

removal

82

5.2 Flat surface iron tip used for dressing of BGA area 82

5.3 Special fabricated removable SST stencil and

squeegee used for solder paste application

83

5.4 Graph of defect mean versus type of tweezers 85

5.5 Graph of defect mean versus type of iron tip and

solder wax usage

85

5.6 Graph of defect mean versus type of stencil 86

5.7 Graph of defect mean versus baking time and

temperature

86

5.8 Graph of defect mean versus machine air pressure 87

5.9 Graph of defect mean versus nozzle size 87

5.10 Normal plot of the standardized effects 90

5.11 Optimization plot of baking time and oven

temperature

90

5.12 Trend chart of defects in motherboard repair process

(before and after improvement)

91

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LIST OF APPENDICES

APPENDIX TITLE PAGE

A Attribute agreement analysis for inspector 1,

inspector 2 & inspector 3

118

B Analysis of variance (ANOVA) 120

C Design of experiment (DOE) 123

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CHAPTER 1

INTRODUCTION

1.1 Introduction

This chapter explains on the introduction of developing Six Sigma (6σ) to

reduce the scrap cost in motherboard repair process in remanufacturing industry. In

general, all companies concern about the process performance for example quality,

efficiency, productivity, and capability to meet customer’s requirement. This chapter

provides an introduction, problem statement, objectives, scope, flow of the report,

and also conclusion for this chapter.

One of the most innovative developments that emerged out of the total

quality movement is the Six Sigma concept introduced by Motorola in the mid-

1980s. Six Sigma consists of five phases to complete the methodology and this study

conducts all the phases for improvement based on quality aspect and yield

performance. The purpose of Six Sigma is to improve the performance of processes

to the point where the defect rate is 3.4 per million or less.

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So, this project focuses on reducing the scrap cost in motherboard repair

process through the adoption of Six Sigma methodology in remanufacturing

industry. Next, the definition of terms used, background of case study, problem

statement, objectives and scope are defined.

1.2 Definition of Terms Used

To further understand this topic, each terms used in this project title is briefly

explained as below;

i) Six Sigma – A set of strategies, techniques, and tools used for process

improvement. It was developed by Motorola in 1981, and became

famous when Jack Welch; the chairman and CEO of General Electric

between 1981 and 2001 made it central to his successful business

strategy at General Electric in 1995. Today, it is adopted in many

industrial sectors with phenomenal outcomes as a result of its adoption.

ii) Sigma – The Greek letter used to describe the standard deviation of a

data distribution. The standard deviation is defined as a measure of the

amount of variation or dispersion from the average of the observations

of a data distribution.

iii) DMAIC – The strategic approach for reducing variation and achieving

improvement used in Six Sigma. DMAIC is an acronym for Define,

Measure, Analyse, Improve, and Control phases of Six Sigma

methodology.

iv) Critical to Quality (CTQ) – The characteristic of a process or product

that has a direct impact on the customers’ perception towards quality.

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v) Defect – Failure to meet a customer-defined requirement. Defining

what constitutes a defect for a particular process or product is the first

step in quantifying the number of defects, leading to calculation of a

sigma level, which is the number of defects out of one million

opportunities.

vi) Defects per million opportunities (DPMO) – The number of defects

out of one million opportunities for defects.

vii) Scrap costs – A manufacturing reality impacting organizations across

all industries and product lines. Scrap cost are caused by many things.

It may be generated, regardless how severe it is when the wrong parts

are ordered, when engineering changes are not effectively

communicated, when designs are not properly executed on the

manufacturing line, or when the process is out of control. No matter

why scrap occurs, its impact on an organization is always the same,

where it wasted time and money.

viii) Motherboard – A printed circuit board containing the principal

components of a computer or other devices, with connectors for other

circuit boards to be slotted into. Sometimes, it is alternatively known as

the main board, logic board, or system board.

ix) Remanufacturing – The series of business activities required to

retrieve a used product from a customer, either to dispose or repair and

reuse it.

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1.3 Background of Research

In today’s highly competitive electronics industry, a company must be able

to adapt to its customers’ ever changing needs and improve the quality of its

products and services in order to survive (Abdollah, 2011). As customer demands

higher quality, more reliable process at higher yield and quality levels becomes

much more critical.

Besides that, day by day competitiveness is growing and in consequence,

organizations are increasingly becoming ‘process-centred’ and process improvement

efforts are crucial to increase efficiency, standardize practices, and reduce variance.

Every business is required to optimize its processes in order to increase the

efficiency and productivity of operations to maximize the profit.

In order to make process optimization a reality, Six Sigma (6σ) philosophy is

developed into the process to achieve 3.4 defects per million opportunities (DPMO).

Six Sigma’s framework known as DMAIC (define-measure-analyse-improve-

control) is employed to assist in improving the process yield and thus reduce the

scrap rate associated to it.

Montgomery in his seventh edition Statistical Quality Control: A Modern

Introduction has listed the following tools used in DMAIC approach;

• Project charter – Define phase

• Process maps & flow charts – Define & measure phases

• Cause-and-effect analysis – Measure phase

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• Process capability analysis – Measure phase

• Hypothesis tests, confidence intervals – Analyse phase

• Regression analysis, other multivariate methods – Analyse phase

• Gauge R&R – Measure phase

• Failure mode & effects analysis – Analyse phase

• Designed experiments – Analyse & improve phases

• SPC and process control plans – Measure, analyse & control phases

This case study is conducted at a service and repair company for electronic

product located at Senai Industrial Park III, Johor, Malaysia. The company’s nature

of business is sub-contracting the repairing and testing of in-warranty (IW) and out-

of-warranty (OW) electronic products from many well-known giant original

equipment manufacturer (EOM) companies like Western Digital (WD), Hewlett-

Packard (HP), Sony and many more. The company is specialized in troubleshooting

and repairing of many types of electronic products like hard disc drive (HDD), LCD

panel, motherboard, server and etc.

Previously, this company was operated in Chai Chee, Singapore since 1989

until the top management had decided to close the plant and transfer it to Malaysia.

It was transferred to Senai Industrial Park III in June 2011. Initially, the processes,

equipment, tooling, testers, and materials were successfully transferred to the new

plant in Malaysia, except the specialists which many of the employees have decided

to take retrenchment package and leave the company.

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1.4 Problem Statement

It is known that troubleshooting of electronic products especially the

motherboard that is mounted with hundreds of small but complicated components on

it requires high-skilled technical personnel to identify one or more problematic

components that has led to malfunction of the product. Once the troubleshooting

team able to identify the problem, repair team consisting of high-skilled repair

technicians needs to do the repairing jobs like component change, component re-

soldering, BIOS upgrade, open trace closure and etc.

During the motherboard rework process, QA inspection has found numbers

of un-repairable defects on the PCBA area such as lifted pad which is the first top

defect, board delaminating, burnt board, warped, and so on due to many weaknesses

occurred in the process. These un-repairable defects have caused the PCBA to be

scrapped.

In average, 45.89% of the received motherboards for repair are scrapped due

to un-repairable defects encountered during the repair process. The high scrap rate in

the motherboard repair process has caused the company to loss its profits

approximately up to USD32, 400.00 per month. Besides that, it also creates much

intangible loss to the company where customer trust to the company’s capability is

put in doubt and company image is greatly tarnished.

Therefore, in order to overcome the challenge, the management decides to

adopt and apply the Six Sigma methodology in the motherboard repair process with

an objective to reduce the high scrap cost associated with high defect percentage

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occurred in the repair process. By reducing the scrap rate of motherboard repair

process, the organization expects to gain back customer trust on their capability in

repairing and servicing customer products. This is to ensure continuous business and

profit coming into the company.

The management has a great confidence that the stated problem can be

solved by employing the Six Sigma methodology in the process by reviewing the

overall repair process, assessing the possible actions to take, implanting the

appropriate actions and monitor the process after improvement took place through

its DMAIC (Define-Measure-Analyse-Improve-Control) approach. Six Sigma

methodology is a helpful approach that can be used to solve the existing problem

regarding the quality. Starting from the Define phase until the final Control phase,

the entire problem can be virtualized especially the root causes, wastes, and potential

failures.

However, even though Six Sigma is proven to be a useful tool to solve any

quality issues in many forward manufacturing companies, but so far hardly any

research ever done to prove that it also works well in remanufacturing industry.

1.5 Research Objectives

The core objective of this research is to reduce the overall scrap rate for

motherboard repair process and to increase the current process sigma level through

the deployment of Six Sigma methodology in remanufacturing industry.

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In order to achieve the main objective, three specific objectives of this case

study are set as below;

• To analyse the current-state of motherboard repair process performance

• To establish the significant causes of highest defects in motherboard

repair process, and

• To solve the significant causes of highest defects in motherboard repair

process.

1.6 Scope of Research

The focus of the research is to improve the quality and reduce the defect in

order to bring down the overall scrap rate and increase the sigma level of

motherboard repair process. Since there are too many aspects that need to be

improved, this case study is precisely focus on;

i. Ball Grid Array (BGA) component rework process only.

ii. The research is focused on reducing the lifted pad issue which give

the highest number of defect.

iii. Minitab software as a tool employed to do the data analysis for the

entire improvement project.

iv. DMAIC approach as a methodology to improve the repair process

within the research period of 8 months.

v. Data to trace the main defect are limited to three months data only

and data collected for after improvement of repair process are also

limited to three months data only.

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1.7 Significance of Findings

The purpose of this study is to reduce the number of scrapped motherboard

so that the scrap cost can be reduced and give a great contribution for cost saving.

Financial controls play important role in business management. This is because, as

competition between competitors becomes tighten time to time, cost has become a

major concern by the management to review. Analysis of current process and tracing

the potential failures exist in the process can lead to solving the problem from its

root.

The result of this project is very important as a proof that Six Sigma is not

only applicable to forward manufacturing, but also to other business segments like

remanufacturing industry as long as we are dealing with processes and its efficiency

and productivity.

1.8 Organization of Thesis

This thesis is classified into five chapters which are introduction, literature

review, methodology, results and discussion, and conclusion and future

recommendation.

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Chapter 1: Introduction

Chapter 1 is an introduction to the research which explains the background

of case study, problem statement, research objectives, scope of the case study,

significance of findings, organization of thesis, and conclusion. Furthermore,

problem statement also explicates the high scrap issue facing by the company before

Six Sigma is developed into the repair process.

Chapter 2: Literature Review

The literature review of the research is discussed in the second chapter. It

contains several related issues found in the journals, books, internet, and also actual

situation in the repair process at the company. Definitions, principles, and

approaches are used in conducting the research. Broad areas are discussed beginning

from the meaning of quality, Total Quality Management (TQM), Six Sigma

understanding, and DMAIC (Define-Measure-Analyse-Improve-Control) approach

that is used to improve the overall quality of motherboard repair process.

Besides that, Design of Experiment (DOE), Gauge Repeatability and

Reproducibility (GR&R), and Statistical Process Control (SPC) are covered in this

chapter as they are very useful for data analysis and are widely used to help in

making the right decision for process improvement. The purpose of review is to

study on how those tools are used in other areas and businesses and what results it

gives. Besides that, this chapter also briefly discusses about the implementation of

Six Sigma in various industries.

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Chapter 3: Methodology

The methodology of the research is discussed in the third chapter. Concept

and problem solving tools used during the research process are described in this

chapter. Case study, data collection method, conceptual framework, process flow,

charts, and diagrams are used to explain the problem for better understanding of

issue.

Chapter 4: Data Analysis and Problem Identification

Chapter 4 describes the data collection, analysis of data, and problem

identification. This chapter discusses in details about one out of four implementation

stages in DMAIC approach which is identification stage consisting of three DMAIC

phases which are define, measure, and analyse phase that are used to improve the

quality of the reworked motherboard.

Chapter 5: Improvement and Countermeasure Improvement

This chapter continues the next three stages of Six Sigma DMAIC approach

which are categorization, optimization, and standardization stage. Categorization

stage consists of analyse phase, optimization consists of improve phase, and

standardization stage consists of control phase and horizontal implementation or

‘yoko-tenkai’ of action to other areas. This chapter discusses about the proposed

solution and recommendation of improvement. Furthermore, the results of the

experiment are evaluated and analysed using related Six Sigma tools.

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Chapter 6: Conclusion and Future Recommendation

This is the last chapter that concludes and summarizes the whole research on

the benefits and advantages grabbed as the result for implementing Six Sigma

including reduction of scrap cost, increasing of rework process yield, and also on the

future plan for research. The organization of thesis is summarized in Figure 1.1.

Figure 1.1: Organization of thesis

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1.9 Conclusion

This chapter explains a general introduction about the entire research. It

begins with the introduction of the project, then followed by the background of

research, problem statement, research objectives, scope of research, significance of

findings, organization of thesis, and ended with the conclusion. This chapter also

presents the importance of quality not only in manufacturing industry, but also in

remanufacturing sector and other types of business. However, executing continuous

quality improvement only is not enough to compete in this highly competitive

world. Therefore, culture change is needed in the organization to build the quality

along the whole process in order to succeed in this challenging market. Six Sigma

methodology is the quality improvement tool consists the both elements as

mentioned above and is applied during this project. The next chapter focuses on

literature review related to the case study.

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