Final deficiency rept for Unit 1 & interim rept for Unit 2 ...
Monthly operating rept for Oct 1979. · Ni S: Scheduled A Equipment Failure (Explain) 1-Manual for...
Transcript of Monthly operating rept for Oct 1979. · Ni S: Scheduled A Equipment Failure (Explain) 1-Manual for...
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OPERATING DATA REPORT
DOCKET NO. 50-333DATE Nov. 1979
COMPLETED BY E. ZufeltTELEPHONE C315)342-3840
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OPERATING STATUSj
l. Unit Name: FitzPatrick Notes
2. Reporting Period: 791001 - 7910312436
3. Licensed Thermal Power (MWr): '
4. Nameplate Rating (Gross MWe): 8838215. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capacity (Gross MWe): 8308007. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:None
9. Power Level To Which Restricted,If Any (Net MWe): None
10. Reasons For Restrictions,If Any:
This Month Yr.-to.Date Cumulative
II. Hours In Reporting Period 745 7296 3736912. Number Of Hours Reactor Was Critical 745 3167.4 25229.613. Reactor Reserve Shutdown Hours 0 0 0
14. Hours Generator On-Line 745 3067.9 24355
15. Unit Reserve Shutdown Hours 0 0 0
16. Cross Thermal Energy Generated (MWH) 1661462 6079694 4829384217. Cross Electrical Energy Generated (MWH) 570610 2062720 1635759018. Net Electrical Energy Generated (MWH) 553620 1999585 15825570
19. Unit Service Factor 100.0% 42.0% 65.2%
20. Unit Availability Factor 100.0% 42.0% 65.2%21. Unit Capacity Factor (Using MDC Net) 92.9% 34.3% 58.8%22. Unit Capacity Factor (Using DER Net) 90.5% 33.4% 51.6%
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23. Unit Forced Outage Rate 0.0% 58.0% 21.8%24. Shutdowns Scheduled Over Next Months (Type. Date,and Duration of Each):.
Snubber inspection and refueling outage scheduled for March 1980
25. If Shut Down At End Of Report Period, Estimated Date of Startup:26. Units In Test Status (Prior ta Commercial Operation): -- ------ Forecast Achieved -- -
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INITIAL CRITICALITYINITIAL ELECTRICITYCOMMERCIAL OPERATION ./
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AVERACE DAILY UNIT POWER LEVEL*
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DOCKETNO. 50-333r
UNIT JAFNPP
DATE Nov. 1979
COMPLETED BY E. Zufelt'
TELEPflONE (315)342-3840
MON 7y October 1979
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL(MWe Net) (MWe Net)
721 37 808
2 735 18 807
3 787 39 802
4 778 20 802
5 759 21 808 _
6 660 22 806
7 76523 808
8 783 24 809
8129 777 25
10 798 26 768
g3 805 27 420'
12 802 28 404
13 803 49029
34 806 30 658
IS 808 33 658
I6 808 .
SUSNARY: Unit averaged 95% of rated output forthis reporting period.
Reduced power on October 26, 1979 to perform controlrod sequence exchange.
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UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO. S0-333UNITNAME JAFNPP
DATE November 1979.
REPORT MONTil October 1979 COMPLETED BY E. Zufelt*
TELEPliONE 315)342-3840
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4 u2 $*c m". E _e E 2 E "N bIC'83'' "*_
Cause & CorrectivecNo. Date g 3g g ,3 g 5 Event u? E3 Action to
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$E 5 j@g Report ar AG ju*Prevent Recurrence
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7 791026 5 0 11 4 N/A N/A N/A Reduced power to perform control rodsequence exchange
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-J l _ 3 4F: Forced Reason: Method: Exhibit G. instructionsNi S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of DataB Maintenance of Test 2 Manual Scram. Entry Sheets for Licenseeo C. Refueling 3 Automatic Scram. Event Report (LER) File (NUREG-*
g D Regulatory Restriction 4-Other (Explain) 0161)g E Operatur Training & Ucense Examination
F-Administrative 5G Operational Error (Explain) Exhibit ! Same SoureeiJ-Other (Explain)
POWER Alml0RITY OF UIE STATE OF NEW YORKJAMES A. FITZPATRICK NUCLEAR POWER PLANT
NARRATIVE SUMMARY OF OPERATING EXPERIENCE
OCTOBER 1979
The unit averaged 95% of the rated thermal power for theentire reporting period. Power was reduced on October 26, 1979to perform a rod sequence exchange.
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POWER AlmiORITY OF Tile STATE OF NEW YORKJAMES A. FITZPATRICK NUCLEAR POWER PLANT
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Safety Related Electrical 6 Mechanical Maintenance Summary.
WORK REQUEST # REPAIRDATE SYSTEM
COMPONENT # 110W DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIME!!OURS
23 Sep 10 3168 OPS Dual position indication Aligned switch actuator 4
PCV-69A for valve 10-PCV-69A causedby misalighment of positionswitch actuator
25 Sep 23 2756 Visual Enlarged clearances Installed shim.; to reduce clearances 97h'
1123-23
25 Sep 46 2059_
Visual Shock III overstress Modified Detail "B" 72Detail "B"
8 Sep 23 3050 ST Binding in position switch Replaced position switch and 2
Gov. Valve actuating cable switch actuating cablePositionSwitch
26 Sep 10 1942 Visual NRC Bulletin 79-02 Repaired 1110-84B 1251110-84 B Inspection
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26 Seps 10 2068 Visual NRC Bulletin 79-02 Repaired il10-48A 184% ll10-48A Inspection
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< 27' Sep 10 2066 Visual NRC Bulletin 79-02 Repaired 1110-42 179 3/4# 1110-42 Inspection
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POWER Atml0RITY OF THE STATE OF NEW YORKJAMES A. FITZPATRICK NUCLEAR POWER PIANT
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Safety Related Electrical 4 Mechanical Maintenance Summary.
WORK REQUEST a REPAIRDATE SYSTEM It0W DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIMECOMPONENT #
10URS
2 Oct 10 2065 Visual NRC Bulletin 79-02 Repaired 1110-487 297h1110-487 Inspection
2 Oct 14 2721 Visual NRC Bulletin 79-02 Repaired 1114-46 6781114-46 Inspection
3 Oct 10 2070 Visual NRC Bulletin 79-02 Repaired 1110-484 1691110-484 Inspection
1 Oct 10 1936 Visual NRC Bulletin 79-02 Repaired 1110-43 621110-43 Inspection
4 Oct 71 1818 Visual /ST Slight drift of solid state _ Adjusted charger output 1
INV-3B logic
2 Oct 46 2063 Visual NRC Bulletin 79-02 Repaired !!46-188 2231146-188 Inspection
3 Oct g 10 2048 Visual NRC Bulletin 79-02 Repaired 1110-212 8.
" 1110-212 Inspection_a
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2 Oct 46 1817 Visual NRC Bulletin 70-02 Modified 1146-281 385C:3 1146-281 Inspect 3onWLJ1
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POWER Alm 10RITY OF TIE STATE OF NEW YORKJAMES A. FITZPATRICK NUCLEAR POWER PIANT
Safety Related Electrical 4 Mechanical Maintenance Summary.
WORK REQUEST # REPAIRDATE SYS M
COMPONENT # IION i.)ETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIME-
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4 Oct 10 1941 Visual NRC Bulletin 79-02 Repaired PFSK-816 50 3/4PFSK-816 Inspection
4 Oct 66 3239 Visual Filters dirty Replaced filters 5
UC-22 A-K
5 Oct 10 2039 Visual NRC Bulletin 79-02 Modified 1110-503 20h'
1110-503 Inspection
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5 Oct 10 2049 Visual NRC Bulletin 79-02 Repaired 1110-607 16
1110-607 Inspection
8 Oct 46 2057 Visual NRC Bulletin 79-02 Repaired 1146-171B 168,
Il46-171B Inspection
7 Oct 15 2047 Visual NRC Bulletin 79-02 Modified 1115-124 485.
1115-124 Inspection,
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$-4 8 Oct x 10 2060 Visual NRC Bulletin 79-02 Repaired 1110-6 74k3 111 0 - 6 Inspection
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ff 8 Oct 15 2036 Visual NRC Bulletin 79-02 Modified 1115-7 231
111 5 - 7 InspectionC7s
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POWER AU1110RITY OF Ti!E STATE OF NEW YORKJAMES A. FITZPATRICK NUCLEAR POWER PLANT
Safety Related Electrical 6 Mechanical Maintenance Summary*
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WORK REQUEST e REPAIRDATE SYSTEM fl0W C'ITECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIME
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COMPONENT g10URS
4 Sep 10 1423 Visual NRC Bulletin 79-02 Repaired 1110-38 37011110-38 Inspection
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, 12 Oct 10 2041 Vi=ual NRC Bulletin 79-02 Modified 1110-478 233 3/4| 1110-478 Inspectioni
16 Oct 19 2798 Visual NRC Bulletin 79-02 Modified 1119-228 621119-228 Inspection
j 16 Oct 10 2801 Visual Shock III analysis Removed PFSK-726 12
j PFSK-726
i|' 16 Oct 10 2802 Visual Shock III analysis Removed PFSK-725 14
PFSK-72S e
16 Oct 10 2803 Visual i'ock III analysis Removed PFSK-723 11i
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- 18 Octs 10 3481 OPS Valve operator open limit Adjusted valve operator open limit 14
rs ~MOV-13C switch was out of adjust- switch to limit valve travel beforement valve reached backseat. Also
CZ) performed PM cn valve operator.WN
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POWER Alfil10RITY OF TIE STATE OF NEW YORKJAbES A. FITZPATRICK NUCIEA'l POWER PLANT -
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Safety Related Electrical 6 Mechanical Maintenance Summary
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| WORK REQUEST a REPAIRDATE SYSTEM 110W DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIMECOMPONENT #
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20 Oct 10 4017 OPS During previous maintenance Auxiliary open limit for tripping P-3C 4
MOV-13C G (WRED 10/3481) suction if suction valve is closed was
j P-3C valve open liait switch was correctly adjusted. Maintenanceadjusted. Auxiliary open personnel were advised of the necessityi
limit switch for pump trip to check all valve operator position,
was not readjusted as it rotors when adjusting single rotors
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19 Oct 10 2022 Visual Shock III analycis Modified 1110-466 S01110-466
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'21 Oct 10 2026 Visual Shock III analysis Modified PFSK-727 160k
PFSK-727
21 Oct 10 2028 Visual Shock III analysis Modified 1110-468 28S<
1110-468
|i 18 Oct 10 2029 Visual Shock III analysis Modified il10-86CN 102 3/4
Il10-86CN! ~
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18 Oct 10 2804 Visual Shock III analysis Removed 1110-462 10
c:? 1110-462W-O3
21 Oct 10 2808 Visual Shock III analysis Modified 1110-140 2971110-140
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POWEk Atml0RITY OF TIIE STATE OF NEW YORKJAMES A. FITZPATRICK NUCLEtR POWER PLANT
Safety Related Electrical G Mechanical Maintenance Summary
WORK REQUEST # REPAIRDATE SYSTEM
COMPONENT # 110W DETECTED CAbSE OF MALFUNCTION At. TAKEN TO PRECLUDE RECURRENCE TIME-
QOURS
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18 Oct 71 3432 ST Low ICV on battery pilot Performed quarterly ST-16F on entire 24
| BAT-3B cell battery and put on equalize charge!
24 Oct 76 4027 OPS None. Fire alarm circuit Reset alarm circuit. Sun shields were 8,
TIB for main transformer previously installed but under certainI alarmed due to sun and load conditions of ambient temperature and
j hyat from transformer loading, a detector still alarms
24 Oct 66 2834 Visual Shock II.I analysis Removed 1166-62 31166-62 -
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24 Oct 10 2062 Visual Shock III analysis Modified il10-32A 2841
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2S Oct 46 2800 Visual Shock III analysis Modified 1146-263 31S1146-2 6 3
'2S Oct 46 2806 Visual Shock III analysis Modified 1146-1 209\
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26 Oct 76 2818 Visual Shock III analysis Modified 1176-61 40C) 1176-6144
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POWER AUTil0RITY OF THE STATE OF NEW YCRKJAMES A. FITZPATRICK NUCLEAR POWER PLANT
Safety Related Electrical 6 Mechanical Maintenance Summary
WORK REQUEST 4 REPAIRDATE SYSTEM 110W DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIME
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COMPONEfff #!!OURS,
26 Oct 46 2799 Visual Shock III analysis Modified il46-267AN 367 3/4Il46-267AN
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25 Oct 10 2809 Visual Shock III analysis Modified ll10-175N 137
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JAMES A. FITZPATRICK NUCLEAR POWER PLANT,
Maintenance Summary
i October 1979 - I6C
W rk Request # Cause of Results of Action taken to RepairDate System How DetectedComponent # Malfunction Malfunction Preclude Time
Recurrence (!!ours)
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RECALI
10-3-79 02 iT9-72A I6C DRIFT OLTT OF TOLERANCE F-ISP-3-2 20.0|
2692 DIFFERENCE IN PREFORMED ISP 29-1
in 70-74 02-3 LT-201 A/B/C OPS UNKNOWN RFADINGS FOUND OK 10.02696 LAMP WILL NOT .
10-22-79 03 RPI LIGilTS OPS BROKEN CLIP STAY IN SOCKET REPLACED 6.0
3022 LAMP UNIT
10-23-79 03 ROD 30-47 OPS BROKFN POOR INDICATION REPLACED 6.0;
3416
10-23-79 03 ROD 18-07 OPS UNKNOWN DOUBLE INDICATION FOUND OK 4.0,
4016,
10-23-79 03 RPI #4 LITE OPS BROKEN CLIP NO INDICATION REPLACED 2.0
3341 ALARM Blfr NO
10-4-79 07 "F" APRM OPS UNKNOWN llALF SCRAM IMP 7.6 6.0,
! 3369'
10-5-79 07 "A" RBM OPS UNKNOWN INOPERABLE FOUND SAT. 1.0
'3389 ALARM BUT NO'
10-9-79 07 "A" APRM OPS UNKNOWN llALF SCRAM IMP 7.6 10.0
3374
10-17-79 07 15 VOLT REG. IGC FAILED TRANSISTOR IDW GUTFlTr REPAIRED 20.0
3420
10-9-79 07 "A" "D" APRM OPS DRIFT FAILED ST-5Q IMP 7.6 9.0
3350
10-10-79 10 | LS-100 OPS UNKNOWN FAILED ST FOUND SAT. 14.0
JAMES A. FITZPATRICK NUCLEAR POWER PLANT -,
Maintenance Summaryi
October 1979 - ISC
W rk Request # Cause of Results of Action taken to RepairDate System How DetectedComponent # Malfunction Malfunction Preclude TimeRecurrence Diours)
288t- REPLACED
hey {gRggg110-12-79 11 TS-50 ISC AGE / USE DOES NOT RESPOND,
24.0! 3295
10-4-79 20 P-1A/1B OPS DRIFT NO AUTO START RE-CAL 32.0; 3366 BURNED OUT
10-17-79 76 CP-107B OPS LIGIIT BUI.B FAILED ST REPLACED BULB 13.0
2735/3388
10-10-79 99 COMPUTER SEC UNKNOWN COMPUTER CRASIIED RE-PROGRAMED 20.02736
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10-10-79 99 IAC-122/123 SEC AMPLIFIER FAILURE NO RESET REPAIRED 10.03214 FOREIGN MATERIAL !
FALLING INTO10-23-79 99 X-RAY I6C DESIGN FI FFTRONICS COVERED GPENING 2.0
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