JSW Steels Limited
Transcript of JSW Steels Limited
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JSW Steel Ltd(A Unit of O.P. Jindal Group of Companies)
A fastest Growing Steel plant in the country
Achieved annual turnover of Rs.19457crores
Won Prestigious Steel Ministers Trophy awardfor its Excellence in steel industry
On completion of Project Falcon, JSW Steelwill become largest steel plant in single
location
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HSM CRM
Billet Caster
Non - coking coal Coking coalIron ore
Fluxes
Coke oven
Converter LHF, RH Slab Caster
Sintering
HMPT
Pelletization
Beneficiation
Corex Blast furnace
Lumpore
Lumpore
JSW : Process Flow
Wire Rod / Re Bar Mill
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100% stamping in both recovery and non recovery type Coke
oven batteries
Energy Efficient Corex hot metal makin g unit
Highest No. of gas holders (6 No.s)
Largest Corex gas holde r (capacity: 1,00,000Nm3)
Handling 4 types of Gases
Common CV of 1850kcal/ Nm3 for all units
Captive power plant based on Waste heat generating 65MW
power
Captive power plant based on 100% byproduct gases
Zero consumption of Petroleum fuel for Iron ma king
Hot charging of slabs more than 65% in Hot strip Mill furnace
All 3 furnaces operating with Pulverized coal injection
Only Steel plant to deliver CDM benefits
Largest Blast furnace , Largest HSM in India
Uniqueness
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Sp Energy Consumption
6.4956.704Gcal/TcsSpecific Energy Rate1
13531475Rs/-Gcal Cost3
52572863082142TonsTotal Crude Steel Produced2
UOM
v Savings with respect to Energy Consumption over 2008-2009 is Rs 148.68 Cr
DescriptionSl No 2009-20102008-2009
Cost Analysis
6.98
6.847
6.704
6.495
6.2
6
6.2
6.4
6.6
6.8
7
7.2
2006- 07 2007-08 2008- 09 2009- 10 Ex pec ted
2010-11
Year
G
c
a
Reduction in Sp EnergyConsp over 2008-09 is3.12%
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Gap Analysis w .r.t Global Best
1.295 Gcal/ TcsGap
6.495Gcal/ TcsSp. Energy of Similar plant
JSW Steel, VijayanagarWorks
5.20Gcal/TcsSp. Energy of Similar plant
POSO, South Korea
Gap Analysis
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Gap Analysis (Contd..)
1.011Gcal/Tcs
TotalGap
Project are underimplementation
0.123100%Ni l100%
Heat recovery
from flue gasstoves and
sinter cooler
4
Project are underimplementation
0.186100%Ni l100%CDQ in recovery
type cokeoven
3
Projects are on forimplementation
in boilers0.32217%83%100%
BF gasUtilization
2
To reduce hot metalrate JSW Steel is
installing DRIPlant
0.3894
Kg/TLS1027933Hot Metal rate1
RemarksEffect in
Gcal/TcsGapJSWPOSCODescription
SlNo
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Coke ratio at Corex was lowered by 6.7% . This was achieved bybetter heating regime and consistent coal availability.
Coke rate at blast furnace was low ered by 9.3% by increasing thePCI. This was achieved by increased availability of Blast furnaceoperation.
LCP heat rate was low ered by 5.6% and powe r rate was lowered by6.8%. This has been achieved by increased availability of gases toCalcining plant.
LD gas recovery at BOF has improved by 1.7%. It was possible by100% gas holder availability and installation of gas boosters.
5. HSM heat rate was lowered by 4.2% and power rate w as loweredby 11.9% . This was achieved by eliminating idle hours of HSM due tonon availability of gas and by ensuring more availability of gas toreheating furnace.
Mills have stabilized its operation due to over all increase in valueadded products. Power rate of CRM has lowered by 13.25%
Corex gas utilization has improved from 97% to 97.94% by bettergas management.
Waste heat utilization at non-recovery type coke ovens waste heatrecovery power plant was improved and there was increase in powergeneration from 72.39MWh to 106.23MWh also with increased by-product gas utilization
Gas based captive power generation has increased with better gasmanagement.
Energy Conservation Initiatives 2009-10.
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Energy Saving Projects
TotalAnnu
al
Savi
ng s
Invest .
Ma d
e
Units
Million
Rs
Milli
on
In terms
of
Quantity
or
Gcal/Tcs.
Rs
Milli
on
Rs
Millio
n
Rs
Millio
n
1
Third Booster to
improve LD gas
recovery.
2007-08 - -
105 Gcal
of energy
recovered
98 98 45
2 Sand heating in BOF. 2007-08 - -
Annually
550 tons
of LPG is
being
saved.
24.8 24.8 0.12
3
Replace of LPG by
Byproduct gas inBoiler Burners.
2007-08 - -
Annually
730 tons
of LPG isbeing
saved.
3 2.9 3 2.9
4
BF Gas Holder for
improving utilization
of BF Gas
2007-08
30,000
Nm3/hr
of gas
utilized
113 113 220
Sl
N
o
Title of Energy Saving
project implemented
Year of
Implementa
tion
AnnualElectrical
Savings
achieved
Annual thermal
savings
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Energy Saving Projectsotal
Annual
Saving
Invest. Made
UnitsMillion
Rs
Million
In terms of
Quantity orGcal/ Tcs.
Rs
Million
RsMillion
RsMillion
5Captive pow er generationhas increased from 86.87
MWh to 93.35 MWh.
2008-09 6.48 176.5
Bystabilization
of BF gaspressure
with thehelp of BFgas holder
- 176.5 Nil
6
Waste heat utilization andby product gas utilizationhas improved at Non
recovery type coke ovenbased captive power plantresulting in increase ofpower generation from59.16 MWh to 72.38 MWh
2008-09 13.22 360.2 - - 360.2 Nil
7
By effective control of o ffblast and increased plantavailability increase in theCDI rate by 18.39% overthe last year
2008-09 - -
Energy
Consumption has
increasedfrom 0.377
to 0.464Gcal/tcs.
262 262 Nil
8
LPG consumption has beenreduced from 12.61Tons/day to 10.9 Tons/day
by replacing LPG by Corexgas in BF flare stack pilot,sand heating system in BOFand in BF boiler bymodifying th e Corex gasline
2008-09 - -
EnergyConsumptio
n hasreduced
from 0.015
to 0.0125Gcal/ Tcs.
24.59 24.59 25
SlNo
Title of Energy Savingproject implemented
Year ofImplementat
io n
Annual Electrical
Savings achieved
Annual thermal
savings
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Energy Saving Projectsotal
Annua
lSaving
s
Invest
. Made
Units
Mill ion
RsMillio
n
In terms ofQuantity or
Gcal/Tcs.
RsMillio
n
Rs
Million
Rs
Million
9
Corex gas utilization has
been improved from 93%
to 94.18% by modifying
the controls in flaring
system
2008-09 - -
Energy
Consumptio
n has
reduced
from 1.455
to 1.393
Gcal/Tcs.
1003 1003 0.40.14
days
10
LD gas recovery increased
by 45.47% over the last
year. This has been
achieved by taking LD gas
holder capital repair and
changed the delivery mesh
and also additional booster
has also been installed totake care of LD gas
transport during booster
shutdow
2008-09 - -
Energy
Consumptio
n has
reduced
from 0.190
to 0.132Gcal/Tcs.
234 234 1Within 2
days
11
Replacement of h igh
pressure high CV corex gas
by low pressure low CV BF
gas for Ore Drying Furnace
2009 10
Energy
Consumptio
n has
reduced
from 0.015
to 0.012
Gcal/Tcs
73.58 73.58 305
months
12
Interconnection of 4mTPA-
7mTPA BF gas line networkfor ensuring BF gas to
CO#3, even during shut
down of BF#3 -7mTPA unit.
2009-1060,000Nm3/
Hr Flared
gas is used.
367 367 903
months
13
Increasing BF #3 Gas
holder pressure from
1000mmWC to 1085mmWC
2009-10
This hasenabled to
generate
and use
additional
125,000Nm3
/Hr Mixed
gas
735 735 0.25 1 day
Payback
months
Sl
No
Title o f Energy Saving
project implemented
Year of
Implementat
io n
Annual Electrical
Savings achieved
Annual thermal
savings
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Team work in Encon 2009-10
Sl No P roject Description FY Responsible Agencies P roject status
1
Interconne ction of 4mT-7mT PA BF gas line
interconnection for ensuring BF gas for gas
mixing station at coke o ven#3 even w ith
BF#3 under down c ondition
2009-10
VP(EMD), Manager
(Coke oven), Manager
(EMD), Asst. Managers
and technicians
Project has
been
completed
2
Rep lacing HP a nd high CV corex gas by LP
and low CV BF gas for ore drying furnace of
pellet plant.
2009-10
VP(EMD),Sr.Manager
(EMD),Manager(EMD),
Asst.Managers(EMD),
Technicians
Project has
been
completed
3
Utilizing mixed g as in corex gas netw ork by
regulating Corex gas pressure in case of
one corex g as unit is under shutdow n.
2009-10
VP(EMD),Sr.Manager
(EMD),Manager(EMD),
Asst.Managers(EMD),
Technicians
Project has
been
completed
4
Increa sing the BF#3 Gas holder pressure
from 1000mmWC to 1085mmWC for
ensuring 100% opera tion of Gas mixing
station.
2009-10
VP(EMD),Sr.Manager
(EMD),Manager(EMD),
Asst.Managers(EMD),
Technicians
Project has
been
completed
Encon Team work
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Solid Waste Management 2009 - 10
Replacing iron ore5869858698Base mix yardMill scale6
-21212129744Pelle t plant & SPdust5
This is 2% of totalenergy for making
pellet103462199030Pellet plantsludge4
This is 25% ofenergy for making
sinter2544091372837
BOF as coolant,IM, PP & SP as f lux
Steelmaking slag
3
This is 80% of totalenergy for making
cement19256381996666
Cement making,ground granulated
BF slag
Iron makingslag
2
This is 31% of totalenergy for making
crude steel15858011558926
Power plant, BFs,Coke ovens & sold
Coal & cokefines
1
Equivalent ofEnergy
Quantityreused /
recycled, t
Generation, Tons
Waste used atType ofmaterial
Sl.No
Solid waste 2009-10
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Specific Water Consumption
2.182009-10
2.932008-09
3.132007-08
ConsumptionYear
Specific w ater consumption details (m3/ Tcs)
This has been achieved due to the follow ing:
1.Waste water utilization at ore Beneficiation plant#2
2.Waste w ater also utilized for ore w ashing at BF#3
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Carbon Emission Reduction initiatives
23%11 crores60 crores49 croresRs .
Percentage
Variance2009-102008-09
Sales
ofCarboncredits
This pertains to carbon credit earned against following projects:1.By-product gas uses for power generation at captive powerplant#1
2.Usage of Waste heat of non recovery coke plant for powergeneration at captive power plant#2
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Future CDM Projects for Green Environment
Total CO2
Reduction
Total
annualSaving Investment
Tons of
CO2/ YrRs. Rs.
Payback
months
1Waste heat from B F
Stoves2010 17975 78.8 200 31
2
Installation of Process
boiler for utilizing
60,000Nm3/H r of BF
gas
2011 290473 436.26 60 1.5
3
Utilization of BF Gas i.e.
100000 Nm3/hr forgenerating steam for
power generation
2011 484122 727.08 100 1.65
5CDQ for 1.2 mTPA Non
Recovery Coke Ovens2011 89878 378 750 24
SlNo
Projects
630 18Part oftotal
package
4 TRT for BF 4 2011 149796
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Renew able Energy at JSW
Traffic signals and Street Lighting at steel plant andTownships has been provided with Solar Energy.
All the Guest houses have been provided with solar hotwater facility.
Jatropa cultivation has been initiated at Vidyanagartownship and w ill be extended to around 75acres.
The total energy generated is about 390000 units and asaving of Rs. 1033500. by solar photo voltaic Cells.
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Environment projects-2009-10
3 new de-dusting systems at RMHS#2 (crusher building,screening building & proportioning building) to control thefugitive emissions.
Tyre washing facility near beneficiation plant #1 to arrest thecarry over of dust from the truck tyres on to the road.
Installation of pneumatic conveying system at BF#1 de-dusting system. This has resulted in reducing the do wntime ofthe de-dusting system due to the problems encountered atthe dust conveying arrangement.
5 de-dusting systems of Coke ovens Installed at the coalcrusher house, coke screening & coke cutter house.
10 no. of stack monitors to monitor the dust level on acontinuous basis.
3000 m3/ hr. Compressor to cater to the new de-dustingsystems & dry fog dust suppression systems
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AAQ at 3 stations to monitor PM 2.5, PM 10, TSP, SO2,Nox & CO on a continuous basis
SGP at SMS1 to granulate the slag.
DSS at RMHS junction houses & yards to control the
fugitive emissions from yards & junction houses.
Gas cooling at SP1 to control the temperature & hencereduce the damage to the electrodes.
Pneumatic conveying at PP to utilize the bag filter dustsfrom various plant units.
Environment projects-2009-10
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ISO - NCRs for 2009-10( OCT09- Mar10)
To collect the dust generated during hot metal handling.Present Level: SPM 3763 microg/m3
Target : SPM 1500microg/ m3.
Objective :To collect the dust generated during blow ing.
Present level: SPM 4063 m icrog/m 3 during blowing
Target: SPM 1500 microg/m 3
1. No action plan to implement the above evidenced.
2. SPM le vel not monitored since January 2009 to till date.
3. Since it is significant environment aspect auditee needsto take measures to control and bring it to the target level /norms as required by the applicable Environment act (EPAct 1986 amended in 1999).
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ISO Corrective action 2009-10
Management to take the decision reg. Performance ofSecondary De-dusting Systems for Mixer and Converter 2.
EMD being central authority for monitoring dust levelshelp from EMD required to monitor the dust levels in theseareas.
Risk assessment of SP1- JB1C2 conveyor being reviewedand revised with immediate effect.
Testing has been done but test report is aw aited. As soonas the test certificate is recd. same w ill be submitted forinspection
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ISO Preventive action 2009-10
As per the MOM of MRM No.36 dt.23/ 07/ 09, a circular hasbeen issued to ensure usage of P PES in the w ork zone tillthe desired levels are a chieved. The copy of the circular isattached. 2. EMD has agreed to continue monitoring thedust levels in these areas as it was done earlier.
Henceforth, corrective and preventive action shall betaken after any incident after reviewing the riskassessment of the concerned activity.
Test Certificates will be avl. in time. Follow up will beinitiated with Safety Dept. so that test certificates arerecd. in time.
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Energy Based Innovative projects 2009-10
Installation and commissioning of BF gas networkinterconnection of 4mTPA and 7mTPA operating at variedoperating pressure with control system:
Net Saving: Rs 36.792Crores
Replacement of high pressure and high CV corex gas by lowpressure and low CV BF gas for ore drying at Pellet plant:
Net saving : Rs 91.98crores
Up gradation of BF gas holder pressure from 1000mmW C to1075mmWC
Net saving: Rs 168.192crores
Utilizing 970mmWC mixed gas in 1000mmWC corex gas
network during one Corex gas unit under Shutdowncondition by controlling pressure in Corex gas networ k
Net saving: Rs 50crores
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Up gradation of BF gas ho lder pressure from1000mmWC to 1075mmWC (Innovative project)
BF#3 gas holder was designed for a pressure of 1000mmWC
Before commissioning of gas holder, BF gas network was operatedwith a pressure of 1150mmWC.
It w as experienced that, there was fluctuation of BF gas pressure inthe upstream side of gas mixing station near Oxygen plant.
Outlet of this mixing station was against Corex gas networkpressure of 950 to 980mmWC.
Due to fluctuation of upstream pressure 970 to 10 00mmWC at Gasmixing station, mixed gas generation i.e BFG+COG was varying inbetween 30000Nm3/Hr to 40000Nm3/Hr.
With 1000mmWC pressure of gasholder, there would be drop inpressure up to 10mmWC and it would not have been possible togenerate mixed gas.
Therefore, a proposal was made that gasholder pressure to be1200mmWC.
Accordingly a static load on piston was calculated and was foundthat, column found ation and structural cant take that much of load.
Further, it w as found that, pressure of 1075mmW C w ill be suitableas around 200Tons of weight on gas holder piston w ill be safe withexisting foundation and columns.
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But it was found that, there is not much area on top of thepiston to accommodate concrete load of 200Tons.
Therefore a decision was taken to use pig iron available atplant site. Hence pig iron w ere anchored by concrete.
The pressure achieved w as 1075mmWC.
This has enabled us to generate mix gas up to 160000Nm3/ Hr.Otherwise the gas was being flared.
So there is gain of 125000Nm3/ Hr of mixed gas.
This has helped us also in generating mixed gas for largestHSM reheating furnaces.
Overall mixed gas generation was possible up to165000Nm3/Hr
Cost of mixed gas Rs. 1.22/ Nm3
Cost of modification Rs. 25Lakhs
Benefit works out to be 168crores/ Anum
This work is one of its kind in any steel plant. This hasmade the gas network viable and for generating desiredquantity of mixed gas fo r stable operation of plant.
Up gradation of BF gas ho lder pressure from1000mmW C to 1075mmWC (Contd..)
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PistonDome
Pig Iron added toincrease the weight
of Piston
Concrete Blocks
Concrete
Rubber Seal
Shell
Piston RestBlocks
Gasholder Dome
Designed Pressure -1000 mmWCPressure Increased by Adding Pig Iron -1075 mmWC
BF-3 Gasholder (Innovative project)
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Energy Conservation projects 2010-2011
0.2468Total
0.1Rs 8 MillionBF gas to power plant for
power generation5
0.02Rs 8 MillionUp gradation of EMC SCADA4
0.0128Rs. 8 Million
Replacement of H P Corexgas by BF gas for 2ndOre drying furnace of
pellet plant
3
0.05Rs 50 Million
Interconnection O2 and N2header of all Oxygenplant for flexibility of
operation so as tooperate all units
2
0.064Rs.600 MillionInstallation of 2 No.s of BF
gas fired boilers forprocess Steam
1
Effect on Sp.Energyin Gcal/ Tcs
InvestmentProject DescriptionSl No
A
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Energy Conservation measures 2010-2011
B
Total Effect on Sp.Energy Consumption = A+B= 0.347Gcal/ Tcs
0.1002Total
0.02Increasing TRT power generation
from 3MWh to 8MWh3
0.012Increasing the utilization of
Corex gas from 97.94 to98.94%
2
Reduction of BF coke rate from518 to 480kg/ THM
0.0682
Increasing BF Coal rate from66. 23 to 100kg/TH M
1
Effect onSp.Energy in
Gcal/ TcsProject Description
Sl
No
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Best Practices Observed On Energy Front
Preparing Energy budget with regard to by- product gasyield, Gas CV, Heat rate, Power rate, Utility utilization inshops. Budget as per experience and Energy improvementprojects
Energy Managem ent through SCADA.
Delay strategy followed by shops during short and longshutdowns.
Low cost, No cost solutions for energy related problems.
Planning and implementation of Energy conservationprojects under Capex.
Continuous work for Energy security.
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Energy Security Efforts at JSW
Optimizing the P CI ( Pulverized Coal Injection) to reducecostly coke in all Blast furnaces
Utilizing more than 15% non coking coal in coke ovens
Corex gas utilization is > 98.4%
Efforts are on for BF gas utilization > 95% by 2012
Has Instal led TRT @ BF#3 i.e. for High To p pressure blastfurnace
About to install CDQ for recovery type coke ovens andproduce 50MWh pow er generation
JSW Steel is set to get Natural gas, another importantmeasure for Energy Security
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Energy Report
On Dat e T il l d at e Parameter Unit Target On Date Till dateCO 1&2 Gross Coke % 74 70.8 71.2No of pushing Nos 112 108 108Waste heat power Mwh 64 55.6 53.5Pow er Rate Kw h/ tp 12 16.42 16.51CO3 Gross Coke % 74 72.4 72.5Specific heat Gcal/ Tdc 0.65 0.61 0.61CO 3 gas yield Nm3/ tdc 310 332 315Tar yield % of tdc 3.2 2.85 2.91No of pushings Nos 224 221 216.5Pow er Rate Kw h/ tp 55 57 57Gaseous Hea t ra te Gca l/ T 0.007 0.007 0.007Coke Breeze Heat Gca l/ T 0 .388 0.402Pow er Rate KWh/ T 40 42 39Gaseous Heat rate Gca l/ T 0.007 0.006 0.006
Coke Breeze Heat Gcal/ T 0.194 0.150Pow er Rate Kw h/ T 40 38 39G ase ous F ue l ra te Gcal / T 0.12 0.13 0.131Pow er Rate KWh/ T 70 65 67
10600 293540
Sinter Plant 1 6469 184574
Pellet Plant
Sinter Plant 2 7838 207757
For June 28, 2010
ProductionShops
1165724265
Coke oven 1&2
Coke oven 3
Energy Management Department
673482409
Daily Plant Energy MIS
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Energy Report
On Da te T il l d at e Parameter Unit Target On Date Til l dateCoal Rate Crx 1 Kg/ Thm 815 900 867Coke Rate Crx 1 Kg/ Thm 170 185 199Oxygen Ra te Crx 1 Nm3/Thm 560 615 744Nitrogen Rate Crx-1 Nm3/Thm 125 144 288Gas yield Crx 1 Nm3/ Thm 1680 1,638 1,817Coal Rate Crx 2 Kg/ Thm 815 963 899Coke Rate Crx 2 Kg/ Thm 170 159 191Oxygen Ra te Crx 2 Nm3/Thm 560 630 615Nitrogen Rate Crx 2 Nm3/Thm 110 122 118Gas yield Crx 2 Nm3/ Thm 1680 1,812 1,798Corex gas C V Kcal/ Nm3 1855 1,870 1,898Pow er Rate KWh/ Thm 85 109 113Coke Rate BF 1 Kg/ Thm 520 452 466CDI Rate BF 1 Kg/ Thm 80 100 90Gas yield BF 1 Nm3/ Thm 1750 1,609 1,675Oxygen Rate BF 1 Nm3/ Thm 70/100 48 46N it rogen Rate BF 1 Nm3/Thm 50 48 46Heat rate (stoves) Gca l/Thm 0.63 0.45 0.44
Coke Rate BF 2 Kg/ Thm 520 469 452CDI Rate BF 2 Kg/ Thm 120 100 77Gas yield BF 2 Nm3/ Thm 1885 1,793 1,930Oxygen Rate BF 2 Nm3/ Thm 55 55 45N it rogen Rate BF 2 Nm3/Thm 50 65 83Heat rate (stoves) Gca l/Thm 0.50 0.59 0.60Pow er Rate KWh/ Thm 50 48.8 53.55
Blast Furnace 2 3609 86029
Blast Furnace 1 2841 74352
Corex 1 2207 55246
Corex 2 2003 56535
For June 28, 2010
ProductionShops
Energy Management Department
Daily Plant Energy MIS
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Energy Report
On Dat e T il l da te Parameter Unit Target On Date Till dateCoke Rate BF 3 Kg/ Thm 525 437 450CDI Rate BF 3 Kg/ Thm 150 105 87Gas yield BF 3 Nm3/ Thm 1800 1,601 1,782Oxygen Rate BF 3 Nm3/ Thm 50 90 84.87BF 3 Ni trogen Rate Nm3/Thm 50 36 58B F 3 Power rate KWh/Thm 160 147 160Heat r ate (st oves ) Gcal / Thm 0.50 0.49 0.53B F gas C V Kcal/ Nm3 750 750 750Heat rate Gcal/ Ton 0.75 0.75 0.79Power rate KWh/ Ton 34 37 35Oxygen rate Nm3/ Tls 54 57 59Nitrogen rate Nm3/ Tls 28 50 46Power Rate KWh/ Tls 45 42 43Hot Metal rate Ton / Ton 1.027 0.996 1.024LD Gas Recovery Nm3/ Tls 100 113 107Argon Rate Nm3/ TSla 2.00 1.20 1.39Power Rate KWh/ TSla 18 18 19
Oxygen rate Nm3/ Tls 54 59 59Nitrogen rate Nm3/ Tls 28 45 39Power Rate KWh/ Tls 45 70 69Hot Metal rate Ton / Ton 1.027 1.216 1.235LD Gas Recovery Nm3/ Tls 100 0 0.00Argon Rate Nm3/ TSla 2.00 1.82 2.15Power Rate KWh/ TSla 18 30.6 30.0Heat rate Gcal/ Tp 0.27 0.279 0.368Power Rate KWh/ Tp 90 80 88
SMS 2 7140 177882
CCP 2 7049 174687
HSM-1 227290
LCP 1875 46786
9903
259675
256235CCP 1
SMS 1 10238
10153
192424B las t Fu rnac e 3 8 27 3
For Jun e 28, 2010
ProductionShops
Energy Management DepartmentDaily Plant Energy MIS
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Energy Report
On Dat e T ill d at e Parameter Unit Target On Date Ti l l dateHeat rate Gcal/ Tp 0.27 0.863 0.402Pow er Rate KW h/ Tp 90 419 190Heat rate Gcal/ Tp 0.35 0.31 0.372Pow er Rate KW h/ Tp 160 156 212Heat rate Gcal/ Tp 0.4 0.29 0.552Pow er Rate KW h/ Tp 110 109 175Heat rate Gcal/T p 0.298 0.90 0.165
380 66113 Pow er Rate KW h/ Tp 95 613 129BF gas co nsum pti on Nm 3/h r 165000 10 3,90 8 94 ,6 69Corex Gas Cons Nm3/ Hr 85000 98,513 96,305To tal Generat ion M Wh 100 104 99Corex Gas Cons Nm3/ Hr 25000 19,410 21,454BF gas co nsum pti on Nm 3/H r 175000 1 36 ,3 33 1 20 ,1 11To tal Generat ion M Wh 120 111 107Plant load MWh 360 291 285Speci f ic power KWH/ Tcs 560 406 447
r on 4 mT PA B F # 3 SMS #1 SMS # 2 HSM-1 CRM Total/ day3.90 0.05 3.80 3.90 0.52 0.39
Losses (% ) Corex gas 1.65 CO Gas 0.11 BF 1 & 1 6.62 B F 3 Gas 15 .5 6
Specific Energy Consumption 6.67 (w ith BP norm) On date 6.34 Ti l l Date 6.50
Energy Management Department
Electricity
HSM-2 728 79444
Daily Plant Energy MISShops
LP G
For June 28, 2010
Remarks: 1)Good Hot metal rate in SMS -1 i.e 0.996 Thm/ Tls. 2) Good Coke rate in Blast Furnace -1,2 & 3. 3) Good CDI rate of Blast Furnace -1 i.e 100 Kg/ Thm.
14.87W RM & Others JPOCL BOC # 1 & 20.20
Production
10 4
CRM CPL
CRM CCM
2796
W RM 1702
1.91 0.20
29025
CPP-2 111 2976
BRM 2094 29892
CPP-1
34Saving in Everything W e Do Sep-2010
ENERGY A Major Thrust at JSW
JSW Steel Since inception has taken care of Energy Efficienttechnologies
JSW Steel Cares for Energy
Daily Energy Review during ED(O) & HODs Meeting
Energy is reviewed during w eekly cost meeting
SEC is the Key Result Area for Senior and Top Management
CEO Review s Energy during weekly production performancemeeting
CEO Reviews Energy during monthly production meeting
MD Reviews performance of Energy conservation activities,future plans and encourages team for achieving set goals.
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8/6/2019 JSW Steels Limited
18/18
18
35Saving in Everything W e Do Sep-2010