Hpht Well Norway
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Transcript of Hpht Well Norway
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7/27/2019 Hpht Well Norway
1/3World Oil / march 2012 77
MANAGED PRESSURE DRILLING
An extreme HPHT
exploratory well reached TD
with optimal hole size, using
MPD methods to maintain an
overbalanced wellbore and
handle breathing events.
S.K. NaeSheim, Frode LeFdaL, n ToryviNd oFTedaL, BG NorGe; n heNriK
SveiNaLL, Wtf intntnl Lt.
The Mandarin East well exhibited themost extreme temperature and pressureever encountered while drilling a Norwe-gian well. Planning for this exploratory wellhad anticipated a surface pressure of nearly1,000 psi and extremely high tempera-tures. To understand and control wellboredynamics while maintaining an overbal-anced wellbore, operator BG Norge in-stalled a managed pressure drilling (MPD)system to provide early kick detection andallow for wellbore breathing mitigation.
A key objective of using MPD was toset the 97/8-in. production casing shoe asclose to the reservoir as possible, to allowthe optimal -in. section to be drilled toTD within a very narrow (0.4-ppg) drill-ing window. Well breathing events pre-sented a significant challenge in this dif-ficult wellbore environment, which madepore pressure evaluation and kick detec-
tion critical to drilling.Using the service companys auto-mated MPD system to mitigate drillinghazards allowed the entire -in. sectionto be drilled to ,933 m (19,46 ft) TD.The system saved an estimated 10 rig daysand $. million, while reducing risk andimproving safety. Controlling gas influxesand precisely weighting up the mud sys-tem saved five of those days when com-pared to a conventional system.
PLANNING THE WELL
Once the constant bottomhole pres-sure (CBHP) methodology was selected,
rigorous planning and preparation wereinitiated. Prior MPD operations in Nor-
way were drilled while maintaining a stati-cally underbalanced mud weight. Annularfriction and surface backpressure wereused to maintain bottomhole pressureabove the pore pressure. These existingprocedures could not be applied directlyto the Mandarin East well. Maintenanceof an overbalanced mud weight limited
the operational envelope to an extent,but the extreme HPHT environmentprompted a cautious approach.
A project team of operator and MPDpersonnel was established four monthsahead of the spud date. A rig survey de-termined that major rig modifications
were required, because the area betweenthe rigs annular preventer and divertercouldnt accommodate the rotating con-trol device (RCD). Thus, the riser had to
be nippled down in the yard, and a new,shorter, overshot mandrel and packerassembly were manufactured to providethe necessary space between the annularand diverter.
Most of the existing MPD procedureshad to be modified, because underbal-anced drilling (UBD) techniques couldnot be applied at any stage, and surface
backpressure would only be applied if aninflux was detected. It was necessary to in-clude the MPD procedures in the conven-tional HPHT procedures and establishguidelines for the use of MPD and con-
ventional rig equipment. Several work-shops and HPHT training sessions wereconduced for rig and MPD personnel.
A full suite of integrated proceduresand decision trees was prepared. It wasdecided that any kicks above 1 bbl would
be handled by the standard rig equip-ment, due to a risk of taking a second-ary kick, if a kick greater than 1 bbl wascirculated undetected to the surface, Fig.1. The training, risk assessments, work-shops and discussions with the crewsprior to spudding were a very important
factor in the success of applying MPDtechniques.
MPD RIG-UP
Two rig surveys were conducted todetermine where the MPD equipment
would be placed. Due to limitations onvariable deck load, space and overshotmandrel modifications, none of the MPDequipment could be rigged up before theintermediate 135/8-in. casing had been run
and cemented in place. Norwegian regu-lations also specified that electric cablingon the rig must be upgraded to NORSOKstandards. A total of 2 km (1 mi) of newcables had to be put in place before theequipment could be installed.
The MPD equipment package fea-tured an MPD manifold unit that includ-ed computer-controlled chokes, Coriolisflowmeters and an Intelligent ControlUnit. A passive, self-lubricating, large-
bore RCD (able to handle pipe up to 65/8-in. OD) was connected to the BOP annu-
lar. A removable bearing assembly for theRCD allowed for an 1.69-in. ID when
Record HPHT Norwegian well drilled with
MPD fow detection and controlFig. 1. conventionl well ontol o mPDetods? Tis deision tee desibeste pt to king tt ll o engineesdilling n extee hPhT well osoeNowy.
Drilling in securestandard (auto
control on)chokes fully open
Influx largerthan 1 bbl
Influx detected
- Stop drilling
- Space outdrill string- Close upper
pipe rams- Stop drilling- Reduce rotation
to 10 rpm- Keep circulating
Divert returns toMGS when influx
at 1,200 m
Evaluate if toincrease mud weight
to accommodateincreased pore
pressure
Further influxdetected
Combinedinflux > 1 bbl
Commence wellcontrol operation
Circulateout Influx
Resume drillingensure chokesare fully open
NoYes
NoYes
NoYes
Oiginlly ppeed inWorld Oil
march 2011 issue, pgs 77-80. Posted wit peission.
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7/27/2019 Hpht Well Norway
2/378 march 2012 / WoldOil.o
MANAGED PRESSURE DRILLING
the bearing was removed. The RCD mod-el used is the first certified to API 16Dspecification. Its pressure rating is 2,000psi static and 00 psi at 200 rpm, Fig. 2.
The equipment package also includedvarious MPD sensors in the flowlines andmud pits. Hard, flexible piping was usedto connect the MPD equipment to theRCD, the rigs choke manifold, the triptank and the rigs poor-boy degasser. Atop flange tied the RCD back to the rigs
bell nipple. This equipment was rigged upprior to drilling out of the 135/8-in. casing.
About four days were lost, because of rigspace limitations that required installa-tion of MPD equipment after intermedi-ate casing was landed.
DRILLING THE SECTION
An extensive flushing, pressure test-ing and fingerprinting program was con-ducted prior to drilling out of the 135/8-in.casing. The MPD system was engaged forthe bottom 600 m (1,969 ft) of the 12-in. hole to acquaint crews with new pro-cedures and equipment in advance of thelower, more difficult section.
Before drilling out of the 97/8 x 10-in. production casing, the 1.-ppg
OBM used for drilling out the cement andfloats was fingerprinted again. At ,40 m(1,40 ft), a LOT to 19. ppg was ob-tained. Drilling continued toward the res-ervoir at about ,90 m (1,340 ft) with a1.-ppg mud weight circulating throughthe MPD system. Background gas (BG)
was moderate, with levels of about 1%.From approximately , m to ,60 m(1,22 to 1,241 ft), a gradual 1-to-%increase in BG levels was experienced.Two flow checks were negative. At ,62m (1,24 ft), a sudden 10% increase in
the gas level was observed. Drilling wasstopped, and the well was circulated with-
out any significant decrease in gas levels.Surface backpressure (SBP) was added
in 100-psi increments until the gas flowstopped. The flow and density param-
eters stabilized at 30 psi SBP, indicatinga pore pressure of 1.-1.6 ppg. To verifyan underbalanced state, the MPD choke
was opened briefly. The bottom-up gaswas about 33%, and underbalanced con-ditions were confirmed.
The bit was held stationary at ,62 m(1,24 ft), and the mud weight was in-creased from 1. ppg to 1.0 ppg in onecirculation cycle, to slowly reduce the SBPon the MPD system to an equivalent 1.6-ppg dynamic mud weight. To confirmthat formation integrity had not changedat the casing shoe (19. ppg), the MPDequipment was used to perform an openhole leak-off test. The 19.1-ppg test figureindicated that the pore-pressurefracturegradient window had been reduced toonly 0. ppg. Mud weight was ramped upto 1.2, 1.3, 1.4 and 1.6 ppg to care-fully maintain a bottom hole circulatingpressure less than 19.0 ppg, ensuring a 0.1ppg safety margin, Fig. 3.
Total rig time was only 40 hr from theinitial small gas influx at ,62 m (1,24
ft) through a sequence of steps that ac-curately determined the pore pressure(at 1.6 ppg) with full pressure control,
weighted up from 1. ppg to 1.6 ppg,and accurately determined the new forma-tion integrity. Handled conventionally, theprocess might have taken to 6 days. Keep-ing ECD below 19.0 ppg required that theflowrate be maintained below 200 gpm forthe remainder of the well. Small losses wereexperienced through the sandy intervals.
After the gas incident had been re-solved, confidence in the system increased.
It was decided to apply SBP on connection,to reduce wellbore breathing and time re-
quired to circulate the gas out of hole. Theavailable pressure window did not allowfor a trip margin when pulling the BHA for
bit changes and coring. Swabbing the wellwas avoided by stripping out pipe throughthe RCD with a backpressure equivalent to19.0 ppg from TD to approximately 1,400
m (4,93 ft) inside the production casing.A heavy, 20.0-ppg mud cap pill was placedat 4,000 m (13,123 ft) to give the neces-sary margin for the rest of the trip. Whiletripping back in, the pill had not strung outmuch in the wellbore, and it had to be cir-culated out in steps, very carefully, to avoidlosses. Although some losses were experi-enced, they decreased toward the bottomof the pill and completely stopped once thepill was out of the hole.
Extensive use of the MPD system andthe application of new techniques for
tripping enabled the -in. hole to reachTD at ,932 m (19,463 ft) in to 10 dayssooner than offset wells, where an inter-mediate liner was required. The -in.hole size benefited wireline logging, cor-ing, fishing operations and DST testing,compared to carrying out the same opera-tions in a 6-in. or 5/8-in. hole. The MPDstripping technique was much faster thanthe standard process. It saved an estimat-ed, minimum 12 hr on every trip.
The MPD operations were also usedin the well's P&A phase. Common experi-ence is that placing balanced cement plugsat almost 6,000 m (19,6 ft) is very dif-ficult; often no plug is found when runningin to tag. On the Mandarin East well, witha solid float in the cement string, the MPDsystem was used to hold roughly 0-psi
backpressure on the plugs when pullingout of the cement. This kept the plugs inplace, and, in fact, all the deep plugs weretagged on the first attempt. In addition,the 2,000-psi static pressure rating of theequipment allowed its use to pressure-test
the cement plugs after tagging.
COST SAVINGS
Using MPD led to significant opera-tional and economic advantages. In total,using the MPD system saved 1. days orabout $13.9 MM. Less the time for MPDrig-up and testing the net savings were 10days and about $. MM.
Four days, or about $3.0 MM, weresaved compared to a conventional set-up
when controlling gas influxes, determin-ing the pore pressure and enabling con-
trolled weighting up. About tens days($. MM) were saved by successfully
Fig. 2. Te mPDpkge, inluding oke niold,coiolis owete,intelligent ontol unitnd otting ontoldevie.
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MANAGED PRESSURE DRILLING
drilling the -in. hole to TD in the nar-row pore pressurefracture gradient mar-gin. The elimination of gas check trips
when pulling out for bit changes and cor-ing saved 2 days ($1. MM) The MPDsystem allowed stripping out with back-pressure to control swabbing. Other sav-ings include two days, because no dummyconnections were required, and a half-dayfrom conducting open hole LOTs andpressure tests of cement plugs.
Time savings were achieved by lockingin the ECD pressure during connections,
which totally eliminated long circula-tion periods. However, this is difficult toquantify and is not included in the timecalculation. A total of . days was spenton critical rig time for rigging up, flushing,
pressure testing, fingerprinting and carry-ing out a full-scale drill.
OPERATIONAL ADVANTAGES
Using MPD and sophisticated flowdetection equipment allowed the well to
be safely drilled to TD in an in. holewith a 0.4-ppg pressure window. Doing soadded significant value to the formationevaluation program, and in case of a DST.
The MPD system accurately de-termined the pore pressure in the well
without the need for any wireline tools,
including a sudden rise in pore pressurefrom 1. to 1.6 ppg. Locking in the
ECD pressure during connections in acontrolled, safe way eliminated all extracirculation time resulting from gas from
wellbore breathing during connections.MPD procedures can be tailored for
the application and can be used to savetime and cost, even when UBD is notrequired. Using MPD-controlled strip-ping techniques can eliminate the needfor the conventional pump out to theshoe check trip. The MPD flowlines onthis extreme HPHT well raised crew con-fidence, because gas was not escaping atthe bell nipple on every bottoms-up.
An advanced MPD flow detection de-vice successfully detected an influxlossof less than bbl. The faith gained in theMPD flow detection equipment eliminat-
ed the need for dummy connections nor-mally used when drilling HPHT wells.Lessons learned included the impor-
tance of a line large enough to avoid ex-cessive backpressure, when large gas vol-umes are circulated through the rigs poor
boy system. Experience also illustratedthat it is essential to minimize off-centerdrill pipe versus the rotary table. Mis-alignment of more than 2 in. could leadto time-consuming problems to install anRCD sleeve or bearing. So that the ECDpressure can be accurately locked in dur-
ing connections the system should usea 2-in., ,000-psi line from the rig stand
pipe to the MPD choke manifold.The MPD flowlines should also be
tied in with the rigs trip tank system. Thisallows circulation across the wellhead us-ing the trip tank system with the RCDelement installed. A 2-in. NRV should beinstalled in the line.
CONCLUSION
The change to a closed-loop, MPD sys-tem provided the data and control to drill
within a very narrow window in this ex-treme wellbore and still maintain an over-
balanced mud weight throughout the op-eration. Understanding pore pressure and
well dynamics provided information for anautomated control system using annular
backpressure to effectively manage smallinfluxes and losses. This capability allowedthe well to reach TD with the optimal hole
diameter.
SIGVE KROHN NAESHEIM is
wells pojet nge o teKn Developent wit BG
Goup in Nowy. he s oe
tn 30 yes o expeiene, in
vious positions onsoe nd
osoe, wit bot dillingonttos nd jo opetos. his expeiene
oves Euope, te U.S., Sout aei, te
middle Est nd Soutest asi. he olds n mS
degee in petoleu engineeing oUnivesity o Stvnge.
FRODE LEFDAL is well
engineeing nge o BGGoup in Nowy. he olds nmS degee in petoleu
engineeing o Nowegin
Univesity o Siene nd
Tenology. he s 15 yeso industy expeiene wit jo opetos,
woking in Euope nd Sout aei. he
is BGs Subjet mtte Expet o nged
pessue dilling.
TOR YVIND OFTEDAL is ie
well engineeing nge o
BG. he is petoleu enginee
o roglnd Univesity nds 32 yes o expeiene wit
te ollowing opnies:
Pillips Petoleu, SgPetoleu, Nosk hydo, conooPillips ndBG. he s eld engineeing positions in:
plto/pipeline inspetions, dilling nd
wokoves, well intevention nd plto
opetions in Nowy, Denk nd UK. he s
been nge/supeviso sine 1986.
HENRIK SVEINALL is te
Podut nd Sevie Line
nge o Weteods
Seue Dilling Sevies inNowy. he stted is ee
wit Weteod s UBD
tinee enginee, nd s
woked s n enginee nd pojet nge onUBD nd mPD pplitions in Not aei,
ontinentl Euope nd osoe in te Not
Se. he olds n mS degee in petoleu
engineeing o Univesity o Stvnge.
Fig. 3. Sue bkpessue (SBP) (wite line) ws inesed until tue pessuews edued, oped to te oiginl test. One te SBP eed 500 psi, te ed linediveged o te blue line. Te blue l ine sows tt uid ws injeted into te otionnd tt te lek o pessue ws identifed. One SBP is eoved, te well etuns to nol stte wit no losses o gins.
Article copyright 2012 by Gulf Publishing Company. All rights reserved. Printed in U.S.A.
Not to be distributed in electronic or printed form or posted on a website without express written permission of copyright holder