HBC Response to consultant Comment

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A report respoding to comment of consultant related to beam crack incident.

Transcript of HBC Response to consultant Comment

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    Project: SAIGON CENTRE PHASE 2&3 PHASE 1 A&A WORK

    RESPONSE TO INSTRUCTION OF CONSULTANT RE: BROKEN BEAM SOFFIT

    Comment #1

    HBCs response:

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    Comment #2

    HBCs response:

    - We conducted testing for one bolt at top (out of 4 bolts).

    - There is not any crack found after testing.

    - Testing result:

    + The connection passed the test (required testing tensile force 85% strength of M16 8.8 106.7 kN)

    + Concrete is not broken or cracked

    Figure 1. Location of tested bolt

    Figure 2. Site quick report of testing for bolt #3

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    Comment #3

    HBCs response:

    - There is not any crack line found.

    Bottom side

    Side 1 face

    Side 2 face

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    Comment #4

    HBCs response:

    We have already conducted UPV test.

    Test result:

    - Horizontal direction: average pulse velocity 3.28 km/s (distance 40 cm, concrete grade C30)

    - Vertical direction: average pulse velocity 3.32 km/s (distance 60 cm, concrete grade C30)

    (See Appendix 2 for detail data).

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    Bolts

    Point of UVP3B15'1

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    Actual picture of testing work:

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    APPENDIX 1: SITE QUICK REPORT OF BOLT ANCHORAGE TESTING

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    APPENDIX 2: SITE QUICK REPORT OF UPV TESTING

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