HBC Response to consultant Comment
-
Upload
thanh-khiet-ung -
Category
Documents
-
view
219 -
download
0
description
Transcript of HBC Response to consultant Comment
-
Page 1
Project: SAIGON CENTRE PHASE 2&3 PHASE 1 A&A WORK
RESPONSE TO INSTRUCTION OF CONSULTANT RE: BROKEN BEAM SOFFIT
Comment #1
HBCs response:
-
Page 2
Comment #2
HBCs response:
- We conducted testing for one bolt at top (out of 4 bolts).
- There is not any crack found after testing.
- Testing result:
+ The connection passed the test (required testing tensile force 85% strength of M16 8.8 106.7 kN)
+ Concrete is not broken or cracked
Figure 1. Location of tested bolt
Figure 2. Site quick report of testing for bolt #3
-
Page 3
Comment #3
HBCs response:
- There is not any crack line found.
Bottom side
Side 1 face
Side 2 face
-
Page 4
Comment #4
HBCs response:
We have already conducted UPV test.
Test result:
- Horizontal direction: average pulse velocity 3.28 km/s (distance 40 cm, concrete grade C30)
- Vertical direction: average pulse velocity 3.32 km/s (distance 60 cm, concrete grade C30)
(See Appendix 2 for detail data).
3
2
1
6
5
4
9
8
7
12
11
10
18
12
9
6
3
15
11
8
5
2
14
10
7
4
1
13
17 16
6
Bolts
Point of UVP3B15'1
-
Page 5
Actual picture of testing work:
-
Page 6
-
Page 7
APPENDIX 1: SITE QUICK REPORT OF BOLT ANCHORAGE TESTING
-
Page 8
APPENDIX 2: SITE QUICK REPORT OF UPV TESTING
-
Page 9