Cold Extrusion 1

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    MANJUMANJU

    DOGRADOGRA

    Reg.No-Reg.No-7080854570808545

    Productivity Enhancement onProductivity Enhancement on

    the Cold Extrusion Pressthe Cold Extrusion Press

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    BRIEF HISTORY OF

    THE PROJECTToday, industries are reducing their cost in each area due to

    more compitionWe have decided to reduce Set up time on extrusion line because,

    we are manufacturing heavy items like Rear axle shaft etc.in whichset up time is important thing

    We have already made different quality circle teams in differentdepartments from initial process to final process so we areimproving each area to reduce cost, improve productivity, improve

    safety etc.

    Here we have taken project To bring down the the Set Up timefrom current average 176 mins to 90 mins.

    To eliminate the Straightening Process after ColdExtrusion.

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    PROMOD KUMARPROMOD KUMARExtrusion Shop

    Project in progressProject in progress

    In picturesIn pictures

    PROJECT TEAMPROJECT TEAM

    TeamTeam

    MembersMembers

    Manju DograManju DograTeam leaderTeam leader

    HARJEET SINGHHARJEET SINGHExtrusion Shop

    RAJINDER KUMARRAJINDER KUMARExtrusion Shop

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    Project Start : April 2011

    Working Area : Extrusion Shop

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    5

    ProblemStatement

    Low Productivityon the Extrusion

    Press 350T

    BusinessCase

    Company ishaving Two

    Extrusion Pressesof 350T & 250 T.The Capital Costof the machine isvery high. Thereis strong demand

    for the extrudedaxle shafts. If wecan increase theproductivity by10% we cancreate additional

    capacity of 20,000axle shafts pa.

    GoalStatement

    To bring down thethe Set Up time

    from currentaverage 176 minsto 90 mins.

    To eliminate theStraightening

    Process after ColdExtrusion.

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    Month Apr - May11

    Jun Jul 11 Aug-11

    Sl.No.

    Activities W1-2

    W3-4

    W1-2

    W3-4

    W1-2

    W3-4

    W1-2

    W3-4

    W1-2

    W3-4

    W1-2

    W3-4

    1 Identifying the Work RelatedProblem PLAN

    2 Selection of Problem

    3 Define Problem

    4 Analysis of Problem DO

    5 Identification of Causes

    6 Finding out the Root Causes

    7 Data Analysis

    8 Developing Solution

    9 Foreseeing possible resistance CHECK

    10 Trial implementation &

    MilestonMileston

    eses

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    ProcessProcess

    MappingMapping

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    METHODOLOGY FOR PROBLEM SOLVING

    Identification of different problems by team members & discussion of problems inIdentification of different problems by team members & discussion of problems in

    meetingmeeting

    Selection of problem which have more rejection , more wastage & more costSelection of problem which have more rejection , more wastage & more cost

    effectiveeffective Identification of concerned members to solve the problem & other departments helpIdentification of concerned members to solve the problem & other departments help

    requirement.requirement. Brainstorming by different members to identify the root causes & identification ofBrainstorming by different members to identify the root causes & identification of

    suitable root causes of the problems & analysis using different Q.C. Toolssuitable root causes of the problems & analysis using different Q.C. Tools Action plan on the root causes identified as per the target dates decided by teamAction plan on the root causes identified as per the target dates decided by team

    MembersMembers Implementation of action plan as per the decided target datesImplementation of action plan as per the decided target dates After implementation, identification of status before & after onAfter implementation, identification of status before & after on

    specified formatspecified format

    Review & Follow up of action plan implementedReview & Follow up of action plan implemented

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    Problem FocusProblem Focus

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    MAN MATERIAL METHOD

    MEASUREMENT MACHINE TOOLING

    HIGH SET UPTIME

    LONG CYCLETIME

    CUMBERSOMETOOLING

    IMPROPROPERTOOLING

    INADEQUATESURFACE TREATMENT

    ABSENTISM

    UNSKILLED MANPOWER

    NONCALIBERATEDINSTRUMENTS

    NON CALIBERATEDGAGES

    MACHINEBREAKDOWN

    INADEQUATEPROCESSQUALIFICATION

    LOWPRODUCTIVIT

    Y

    HIGH RUN OUT ONOUTPUT AXLE

    SHAFTS

    Ishikawa Cause & EffectIshikawa Cause & Effect

    AnalysisAnalysis

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    Root CauseRoot Cause

    Analysis-NGTAnalysis-NGT

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    Set Up SymptomsSet Up Symptoms

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    Set Up Process-AsSet Up Process-As

    IsIs

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    Month Total

    Available Time

    Run

    Time

    Product

    ion

    Set

    UpTime

    Down

    Time

    Waiting

    Time (ifany)

    Number of

    Changeovers

    Hrs Hrs Numbers

    Hrs Hrs Hrs No's

    Jan-11600

    46419,500 81 10 45 25

    Feb-11600

    49121,263 76

    231 24

    Mar-11600

    47520,536 79

    739 25

    Apr-11600

    47321,277 62 26 39 25

    May-11600

    49021,210 67

    636 26

    TOTALS 3,000 2,393 103,786 366 51 190 125

    Set Up TimeSet Up Time

    CalculationCalculation

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    Set Up TimeSet Up Time

    CalculationCalculation

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    ActionsActions

    ImplementedImplemented

    1. Fixed Plate installed instead ofmovable to control the distortions.

    2. This plate accommodate allmodels.

    3. This reduced the Set Up time.

    1. The thickness of the Die ClampingPlate reduced

    1. The thickness of the OCD ringincreased

    BEFORE AFTER

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    Run Out on

    Extruded AxleShafts foundvarying from 4~5mm against therequired 1~1.5mm

    StraighteningStraightening

    High Run Out is onaccount axle shaftbeing dragged byram non-uniformlyafter coldextrusion.

    Average Production permonth

    20,757

    Cost of Straightening2.00

    Rs

    Total Monthly Cost41,514.40

    Rs

    Yearly Saving Rs Lacs

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    Distortion on pieceson account of piecesgetting dragged by

    Top and Bottommovable Plates. Thisdemands for theStraighteningoperation after ColdExtrusion

    Distortion AnalysisDistortion Analysis

    BEFORE AFTER

    Fixed Plate placedthat does not allowany transversemovement of axleshaft during thebackward

    movement of RAM.

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    BeforeBefore AfterAfter

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    S.No.

    Set Up Activities Time inMins

    Proposed Actions Time in Mins

    1 UNSCREWING OFMOVABLE PLATES (2 INNO.)

    10.00

    UNSCREWING OF OCDRINGS

    15.00

    2 UNSCREWING OFRESTING BLOCKS(4 INNO.)

    36.00

    UNCREWING OF DIECLAMPING PLATES

    10.00

    3 UNSCREWING OF OCDRINGS

    10.00

    UNLOADING OFSPACERS/DIES

    20.00

    4 UNCREWING OF DIECLAMPING PLATES

    12.00

    LOADING OF NEWDIES/SPACERS

    20.00

    5 UNLOADING OFSPACERS/DIES

    20.00

    6 LOADING OF NEWDIES/SPACERS

    20.00

    SCREWING OF DIECLAMPING PLATES

    10.00

    7 SCREWING OF DIE

    CLAMPING PLATES

    10.00

    SCREWING OF OCD

    RINGS

    15.00

    -8 SCREWING OF OCD RINGS10.00

    9 SCREWING OF RESTINGBLOCKS(4 IN NO.)

    40.00

    10 SCREWING OF MOVABLEPLATES (2 IN NO.)

    10.00

    -

    176 90

    Set Up Time-Set Up Time-

    Before/ AfterBefore/ After

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    GainsGains

    1 SET UP TIME REDUCED FROM AVG 176 mins TO 90 mins

    2 REDUCING SET UP TIME ON AN AVERAGE CREATED CAPACITY OFADDITIONAL 20,000 AXLE SHAFTS PER YEAR.

    3 ELIMINATION OF THE STRAIGHTENING PROCESS THAT LEADS TOANNUAL SAVING OF AROUND Rs. 5 LACS PER ANNUM

    4 LEAD TIME FOR THE TOTAL PROCESS REDUCED

    5 COST OF THE SET UP REDUCED ON ACCOUNT OF LESSCONSUMTION OF TOOLINGS

    6 SIMLIFICATION OF THE SET UP PROCESS LEADS TO HIGH

    MORALE OF OPERATORS.

    7 THE RESULTS CAN BE IMPLEMENTED ON 250 T PRESS ALSO-HORIZONTAL DEPLOYMENT

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    S. No. Equipment Cost-Rs

    1 Material cost of newPlates

    8000.00

    2 Fabrication of Plates 4050.00

    3 Cost of Ring Plates-new 2000.00

    Total 14,050.00

    Cost of ProjectCost of Project

    NEWPLATE

    RINGPLATE

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    Month TotalAvailable

    Time

    RunTime

    Production

    Set UpTime

    DownTime

    WaitingTime (if

    any)

    Numberof

    Changeovers

    Set UpTime/Changeover

    Production/hr

    Hrs Hrs Numbers Hrs Hrs Hrs No's mins No's

    Jan-11600 464 19,500

    8110 45 25 195 42

    Feb-11600 491 21,263

    762 31 24 189 43

    Mar-11600 475 20,536

    797 39 25 190 43

    Apr-11600 473 21,277

    6226 39 25 149 45

    May-11600 490 21,210

    676 36 26 156 43

    TOTALS3,000 2,393 103,786

    36651 190 125 176 43

    Month Total

    AvailableTime

    Run

    Time

    Producti

    on

    Set Up

    Time

    Down

    Time

    Waiting

    Time (ifany)

    Number

    ofChangeov

    ers

    Set Up

    Time/Changeover

    Produc

    tion/hr

    Hrs Hrs Numbers Hrs Hrs Hrs No's mins No's

    JUL-11 600 524 32,55

    8

    429 25 26 97 62

    Impact of theImpact of the

    ActionsActions

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    24/24THANKSTHANKS