Cold Extrusion 1
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Transcript of Cold Extrusion 1
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8/4/2019 Cold Extrusion 1
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MANJUMANJU
DOGRADOGRA
Reg.No-Reg.No-7080854570808545
Productivity Enhancement onProductivity Enhancement on
the Cold Extrusion Pressthe Cold Extrusion Press
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BRIEF HISTORY OF
THE PROJECTToday, industries are reducing their cost in each area due to
more compitionWe have decided to reduce Set up time on extrusion line because,
we are manufacturing heavy items like Rear axle shaft etc.in whichset up time is important thing
We have already made different quality circle teams in differentdepartments from initial process to final process so we areimproving each area to reduce cost, improve productivity, improve
safety etc.
Here we have taken project To bring down the the Set Up timefrom current average 176 mins to 90 mins.
To eliminate the Straightening Process after ColdExtrusion.
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PROMOD KUMARPROMOD KUMARExtrusion Shop
Project in progressProject in progress
In picturesIn pictures
PROJECT TEAMPROJECT TEAM
TeamTeam
MembersMembers
Manju DograManju DograTeam leaderTeam leader
HARJEET SINGHHARJEET SINGHExtrusion Shop
RAJINDER KUMARRAJINDER KUMARExtrusion Shop
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Project Start : April 2011
Working Area : Extrusion Shop
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ProblemStatement
Low Productivityon the Extrusion
Press 350T
BusinessCase
Company ishaving Two
Extrusion Pressesof 350T & 250 T.The Capital Costof the machine isvery high. Thereis strong demand
for the extrudedaxle shafts. If wecan increase theproductivity by10% we cancreate additional
capacity of 20,000axle shafts pa.
GoalStatement
To bring down thethe Set Up time
from currentaverage 176 minsto 90 mins.
To eliminate theStraightening
Process after ColdExtrusion.
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Month Apr - May11
Jun Jul 11 Aug-11
Sl.No.
Activities W1-2
W3-4
W1-2
W3-4
W1-2
W3-4
W1-2
W3-4
W1-2
W3-4
W1-2
W3-4
1 Identifying the Work RelatedProblem PLAN
2 Selection of Problem
3 Define Problem
4 Analysis of Problem DO
5 Identification of Causes
6 Finding out the Root Causes
7 Data Analysis
8 Developing Solution
9 Foreseeing possible resistance CHECK
10 Trial implementation &
MilestonMileston
eses
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ProcessProcess
MappingMapping
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METHODOLOGY FOR PROBLEM SOLVING
Identification of different problems by team members & discussion of problems inIdentification of different problems by team members & discussion of problems in
meetingmeeting
Selection of problem which have more rejection , more wastage & more costSelection of problem which have more rejection , more wastage & more cost
effectiveeffective Identification of concerned members to solve the problem & other departments helpIdentification of concerned members to solve the problem & other departments help
requirement.requirement. Brainstorming by different members to identify the root causes & identification ofBrainstorming by different members to identify the root causes & identification of
suitable root causes of the problems & analysis using different Q.C. Toolssuitable root causes of the problems & analysis using different Q.C. Tools Action plan on the root causes identified as per the target dates decided by teamAction plan on the root causes identified as per the target dates decided by team
MembersMembers Implementation of action plan as per the decided target datesImplementation of action plan as per the decided target dates After implementation, identification of status before & after onAfter implementation, identification of status before & after on
specified formatspecified format
Review & Follow up of action plan implementedReview & Follow up of action plan implemented
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Problem FocusProblem Focus
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MAN MATERIAL METHOD
MEASUREMENT MACHINE TOOLING
HIGH SET UPTIME
LONG CYCLETIME
CUMBERSOMETOOLING
IMPROPROPERTOOLING
INADEQUATESURFACE TREATMENT
ABSENTISM
UNSKILLED MANPOWER
NONCALIBERATEDINSTRUMENTS
NON CALIBERATEDGAGES
MACHINEBREAKDOWN
INADEQUATEPROCESSQUALIFICATION
LOWPRODUCTIVIT
Y
HIGH RUN OUT ONOUTPUT AXLE
SHAFTS
Ishikawa Cause & EffectIshikawa Cause & Effect
AnalysisAnalysis
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Root CauseRoot Cause
Analysis-NGTAnalysis-NGT
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Set Up SymptomsSet Up Symptoms
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Set Up Process-AsSet Up Process-As
IsIs
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Month Total
Available Time
Run
Time
Product
ion
Set
UpTime
Down
Time
Waiting
Time (ifany)
Number of
Changeovers
Hrs Hrs Numbers
Hrs Hrs Hrs No's
Jan-11600
46419,500 81 10 45 25
Feb-11600
49121,263 76
231 24
Mar-11600
47520,536 79
739 25
Apr-11600
47321,277 62 26 39 25
May-11600
49021,210 67
636 26
TOTALS 3,000 2,393 103,786 366 51 190 125
Set Up TimeSet Up Time
CalculationCalculation
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Set Up TimeSet Up Time
CalculationCalculation
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ActionsActions
ImplementedImplemented
1. Fixed Plate installed instead ofmovable to control the distortions.
2. This plate accommodate allmodels.
3. This reduced the Set Up time.
1. The thickness of the Die ClampingPlate reduced
1. The thickness of the OCD ringincreased
BEFORE AFTER
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Run Out on
Extruded AxleShafts foundvarying from 4~5mm against therequired 1~1.5mm
StraighteningStraightening
High Run Out is onaccount axle shaftbeing dragged byram non-uniformlyafter coldextrusion.
Average Production permonth
20,757
Cost of Straightening2.00
Rs
Total Monthly Cost41,514.40
Rs
Yearly Saving Rs Lacs
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Distortion on pieceson account of piecesgetting dragged by
Top and Bottommovable Plates. Thisdemands for theStraighteningoperation after ColdExtrusion
Distortion AnalysisDistortion Analysis
BEFORE AFTER
Fixed Plate placedthat does not allowany transversemovement of axleshaft during thebackward
movement of RAM.
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BeforeBefore AfterAfter
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S.No.
Set Up Activities Time inMins
Proposed Actions Time in Mins
1 UNSCREWING OFMOVABLE PLATES (2 INNO.)
10.00
UNSCREWING OF OCDRINGS
15.00
2 UNSCREWING OFRESTING BLOCKS(4 INNO.)
36.00
UNCREWING OF DIECLAMPING PLATES
10.00
3 UNSCREWING OF OCDRINGS
10.00
UNLOADING OFSPACERS/DIES
20.00
4 UNCREWING OF DIECLAMPING PLATES
12.00
LOADING OF NEWDIES/SPACERS
20.00
5 UNLOADING OFSPACERS/DIES
20.00
6 LOADING OF NEWDIES/SPACERS
20.00
SCREWING OF DIECLAMPING PLATES
10.00
7 SCREWING OF DIE
CLAMPING PLATES
10.00
SCREWING OF OCD
RINGS
15.00
-8 SCREWING OF OCD RINGS10.00
9 SCREWING OF RESTINGBLOCKS(4 IN NO.)
40.00
10 SCREWING OF MOVABLEPLATES (2 IN NO.)
10.00
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176 90
Set Up Time-Set Up Time-
Before/ AfterBefore/ After
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GainsGains
1 SET UP TIME REDUCED FROM AVG 176 mins TO 90 mins
2 REDUCING SET UP TIME ON AN AVERAGE CREATED CAPACITY OFADDITIONAL 20,000 AXLE SHAFTS PER YEAR.
3 ELIMINATION OF THE STRAIGHTENING PROCESS THAT LEADS TOANNUAL SAVING OF AROUND Rs. 5 LACS PER ANNUM
4 LEAD TIME FOR THE TOTAL PROCESS REDUCED
5 COST OF THE SET UP REDUCED ON ACCOUNT OF LESSCONSUMTION OF TOOLINGS
6 SIMLIFICATION OF THE SET UP PROCESS LEADS TO HIGH
MORALE OF OPERATORS.
7 THE RESULTS CAN BE IMPLEMENTED ON 250 T PRESS ALSO-HORIZONTAL DEPLOYMENT
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S. No. Equipment Cost-Rs
1 Material cost of newPlates
8000.00
2 Fabrication of Plates 4050.00
3 Cost of Ring Plates-new 2000.00
Total 14,050.00
Cost of ProjectCost of Project
NEWPLATE
RINGPLATE
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Month TotalAvailable
Time
RunTime
Production
Set UpTime
DownTime
WaitingTime (if
any)
Numberof
Changeovers
Set UpTime/Changeover
Production/hr
Hrs Hrs Numbers Hrs Hrs Hrs No's mins No's
Jan-11600 464 19,500
8110 45 25 195 42
Feb-11600 491 21,263
762 31 24 189 43
Mar-11600 475 20,536
797 39 25 190 43
Apr-11600 473 21,277
6226 39 25 149 45
May-11600 490 21,210
676 36 26 156 43
TOTALS3,000 2,393 103,786
36651 190 125 176 43
Month Total
AvailableTime
Run
Time
Producti
on
Set Up
Time
Down
Time
Waiting
Time (ifany)
Number
ofChangeov
ers
Set Up
Time/Changeover
Produc
tion/hr
Hrs Hrs Numbers Hrs Hrs Hrs No's mins No's
JUL-11 600 524 32,55
8
429 25 26 97 62
Impact of theImpact of the
ActionsActions
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24/24THANKSTHANKS