BNG Industrial experience on Superconducting Undulators

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BNG Industrial experience on Superconducting Undulators C. Boffo, T. Gehrard, B. Schraut, J. Steinmann, W. Walter, Babcock Noell GmbH T. Baumbach, S. Casalbuoni, S. Gerstl, A. Grau, M. Hagelstein, D. Saez de Jauregui, ISS Karlsruhe Institute of Technology Alfred Nobel Strasse 20 97080 Würzburg, Germany Phone: +49 931 9030 Fax: +49 931 9036000 [email protected] www.babcocknoell.de

description

BNG Industrial experience on Superconducting Undulators. Alfred Nobel Strasse 20 97080 Würzburg, Germany Phone: +49 931 9030  Fax:   +49 931 9036000 [email protected] www.babcocknoell.de. C. Boffo, T. Gehrard , B. Schraut , J. Steinmann, W . Walter, Babcock Noell GmbH - PowerPoint PPT Presentation

Transcript of BNG Industrial experience on Superconducting Undulators

Page 1: BNG Industrial  experience  on Superconducting Undulators

BNG Industrial experience on Superconducting UndulatorsC. Boffo, T. Gehrard, B. Schraut, J. Steinmann, W. Walter, Babcock Noell GmbHT. Baumbach, S. Casalbuoni, S. Gerstl, A. Grau, M. Hagelstein, D. Saez de

Jauregui,ISS Karlsruhe Institute of Technology

Alfred Nobel Strasse 20 97080 Würzburg, Germany Phone: +49 931 9030 Fax:   +49 931 9036000 [email protected] www.babcocknoell.de

Page 2: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Würzburg

HamburgBerlin

München

Babcock Noell GmbH

Babcock Noell GmbHAlfred-Nobel-Straße 20D-97080 Würzburg Phone: +49 (0)931 903-4101 Fax: +49 (0)931 903-4171

Page 3: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

2007 Nb3Sn short prototype built for KIT and tested at CERN

2007 Collaboration with KIT on SCUs and SCU15 contract

2008 SCU15 demonstrator

2009 SCUW prototype: design and fabrication based on KIT concept with test by KIT

2010 SCU15 1.5m long coils completed and tested by KIT at CERN

2010 First HTS SCU prototype: design and fabrication with test by KIT

SCU15: 15mm period undulatorSCUW : tripling period 15mm/45mm switchable device undulator/wiggler

Short history of BNG in SC undulators

Page 4: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

o Magnetic design: coil configuration, quench protection, correction coils.

o Mechanical design of the complete system from coils to cryostat.o Cryogenic design: cryogen free system.o Fabrication and high precision “alignment” of the yoke.o Winding process.o Vacuum-pressure impregnation.o Assembly of the complete system.

Most of our existing knowhow had to be further pushed in the past 3 years in order to design and fabricate SCU15

BNG knowhow on SCUs

Page 5: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Specifications

Design constrains:o Cryogen free magneto Variable gap (@ 4K)o End field correctiono Local shimming o Integral field compensation

Units ValuePeriod length mm 15Number of full periods - 100.5Max field on axis with 8 mm magnetic gap T 0.77Max field in the coils T 2.4Minimum magnetic gap mm 5.4Operating magnetic gap mm 8Gap at beam injection mm 16K value at 5 mm gap - >2Design beam heat load W 4Phase error r.m.s. ° 3.5

o High eng. Current density -> magnetic design

o Tolerate beam heat loads -> cryogenic design

o High mechanical accuracy -> fabrication technology

Page 6: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Design – Magnetic field calculation I

Design Parameters:o Yoke materialo Dimension of winding grooveo Eng. current density

Material.......................................................................... NbTiInsulation................................................................... varnishGeometry............................................................. rectangularHeight........................................................................... ..0.34Width (mm).....................................................................0,54Design critical current density* (A/mm2).......................1000Design operating temperature** (K).................................4,2Design magnetic field (T)***................................................4Cu/Sc ration................................................................1.2-1.5RRR.................................................................................>60Filament diameter (um)....................................................<40Twist pitch (mm)...............................................................<50

0 0.5 1 1.5 2 2.5 3 3.5 40

200

400

600

800

1000

1200

1400

1600

1800

2000Magnet Loadline

Magnetic Field [T]

Cur

rent

[A/m

m2]

T = 4.2 KT = 4.5 K

T = 4.80 K

T = 5.10 K

T = 5.35 K

Yoke – soft iron

Main coils

Electron beam

Correction coils

Period 15mm

+ -

Page 7: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Design – Magnetic field calculation II

0 0.5 1 1.5 2 2.5 3 3.5 40

200

400

600

800

1000

1200

1400

1600

1800

2000Magnet Loadline

Magnetic Field [T]

Cur

rent

[A/m

m2]

T = 4.2 KT = 4.5 K

T = 4.80 K

T = 5.10 K

T = 5.35 K

0 0.5 1 1.5 2 2.5 3 3.5 40

200

400

600

800

1000

1200

1400

1600

1800

2000Magnet Loadline

Magnetic Field [T]

Cur

rent

[A/m

m2]

T = 4.2 KT = 4.5 K

T = 4.80 K

T = 5.10 K

T = 5.35 K

Max field in main coils 2.4TMax Jeng 950 A/mm2 (175A)

Max field in correction coils 3.8TMax current 5AUse 0.15 mm diameter insul. wire

Max field in iron 4.5T

Page 8: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Design – Cryogenic circuit

100 150 200 250 300 3503.7

3.8

3.9

4.0

4.1

4.2

4.3

Magnet Heating during Ramp -hot spot- Input power 2.5 W for 100s Init. 0.5W Cu RRR 40/20

RRR 40RRR 20

Time [sec.]

Tem

pera

ture

[K]

Circuit B Circuit AShield

Main concepts:

o Two separate circuits for magnet and beam liner.

o Two base temperatures: 4K for the magnet and 10K for the beam liner.

o Minimization of gradients between cold head and most distant point in the magnet.

Liner Beam

Magnet

Magnet

Cool

ing

circ

uit

B

Cool

ing

circ

uit

A

Page 9: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Demonstrator – field performance

0 0.5 1 1.5 2 2.5 3 3.5 40

50

100

150

200

250

300

350Magnet Loadline

Magnetic Field [T]

Cur

rent

[A]

Magnet Operating Current

Tests by KIT - S. Casalbuoni et al., SRI09

o 16.5 periodso End field correction ¾ - ¼ o Quench protection with cold diodeso Local shimming

Single length wire winding Vacuum Pressure impregnation (VPI) Alignment of coils

Page 10: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Demonstrator – mechanical accuracies

1 3 5 7 9 11 13 15 17 19 21 23 25 27 29 31-250

-200

-150

-100

-50

0

50Yoke 1 after impregnation

Plate number

Flat

ness

mm

0 2 4 6 8 10 12 14 16 18 20 22 24 26 28 30 32-20

-15

-10

-5

0

5

10 Yoke 1 after winding

Plate number

Flat

ness

mm

o Yoke flatness measured after winding -> 20 mm.

o Yoke flatness measured after impregnation -> 250 mm.

The deformation is the result of the 180 C heating performed during impregnation.

Several mixtures have been tested to eliminate the “high temperature” step while keeping the correct physical properties.

C. Boffo et al., MT21

Page 11: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Prototypes

Best test results:

o Max current 240 Ao Max ramp rate 240 A/mino Max eng. current density above 1300 A/mm2

o Reached above 90% short sample limit

0 0.5 1 1.5 2 2.5 3 3.5 40

50

100

150

200

250

300

350Magnet Loadline

Magnetic Field [T]

Cur

rent

[A]

Magnet Operating Current

Tests by KIT - S. Casalbuoni et al., IPAC10

Page 12: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Fabrication

o Stapling and alignment of 205 plates for each yoke.

o Plates have been measured and positioned to minimize

period length variations.

o Winding with single wire.

o Single joint per magnet at end.

o Impregnation at room temperature.

o Measurement of yoke flatness between fabrication

steps.

o Support strongback in stainless steel.

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CLIC Damping Wigglers 03.12.2010 – C. Boffo

Achieved accuracies

Length difference between magnets: 20 mmYoke flatness along 1.5 m: 50 mmMaximum period length deviation: 30 mmMaximum deviation of relative position between the magnets: 50 mm

C. Boffo et al., ASC2010

Page 14: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Tests at CERN

• The magnet test was performed at CERN at BLOC4• Vertical configuration• Temperature between 4.5 and 2.2K• Tight quench detection system

Page 15: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Training and repairs

o The weakest point in the magnet system is in the thin wire.o Difficult to windo Easy to over bendo Sensible on yoke defectso BUT small filaments and high packing

factoro Three repairs have been

performed.o A special technique has been

developed to remove the impregnation and repair single coils.

o Uncertainty on the joints in conduction cooling.

S. Casalbuoni et al., ASC2010

Page 16: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Field performance -1

S. Casalbuoni et al., ASC2010

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CLIC Damping Wigglers 03.12.2010 – C. Boffo

Field performance -2

S. Casalbuoni et al., ASC2010

Phase error of 7.4 degrees over a length of 0.79 m obtained by application of mechanical shims in the support device

Good agreement between measurement and simulations performed at KIT taking into account the mechanical accuracies

Page 18: BNG Industrial  experience  on Superconducting Undulators

CLIC Damping Wigglers 03.12.2010 – C. Boffo

Conclusions

o After three years of close collaboration between KIT and BNG a new 1.5 m long undulator has been fabricated.

o The specifications of the system are such that the technology for the fabrication of SC magnets had to be pushed over the envelope to meet the requirements.

o The magnet performs very satisfactory, close to the envisages specs defined at the start of the R&D.

o The coils are being installed in the cryostat as we speak.

o BNG has a demonstrated knowhow in SCUs design and fabrication.