Blast Cleaninng of Steel Ships Using Recycled Glass

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    Blast Cleaning of Ship Steelusing Re-cycled Glass

    Professor George Bruce

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    Content

    Background

    Blast Cleaning Media

    Legislation & Standards

    Project Blasting Trials

    Results

    Conclusions

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    Background

    The Importance of Blast Cleaning

    Control by Shipyard

    Shipowner Coating Company

    Critical in good Coating of Steel

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    Project Objectives

    Testing of Re-cycled Glass Materials (RGM)

    Blasting Capability Productivity

    Surface Condition Cost Comparison

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    Blasting Media

    Natural minerals - silica sand, garnet,olivine

    Manufactured media - steel shot, glass

    grit, alumina, plastic pellets or beads, solidcarbon dioxide, sodium bicarbonate

    Mineral slag - copper slag, nickel slag,

    iron slag and coal slag

    Organic media - corn cobs, nut shells,

    starch grains

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    Ship Blasting Media

    Sand Health and Safety Hazard

    Grit Copper Slag, Disposal Costs

    Steel Shot Expensive, Closed System

    Garnet High Quality but Expensive

    UHP Water Lower capability

    RGM To be tested

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    UK Legislation

    Landfill Tax will double disposal costs

    EU Packaging Directive Glass Recycling

    Kyoto Summit Emissions Reduction

    Statutory Re-cycling Targets

    Trying to anticipate future legislation

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    Working Standards

    Steel Surface Finish to SA 2.5 Standard

    Depends on initial sub-strate

    50-75 microns ideal for coating

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    Previous Results

    For Epoxy coating:

    Glass abrasive cleaned - 11.6 m2/hr

    Copper Slag cleaned 9.5 m2/hr

    Nickel Slag cleaned 8.0 m2/hr

    Glass abrasive consumed 40.9 kg/m2

    Copper Slag consumed 76.7 kg/m2

    Nickel Slag consumed 74.3 kg/m2

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    Potential Benefits of Glass

    Inert Material

    No Heavy Metals (unlike Copper Slag)

    No Salts Reduced Corrosion

    No Free Silica

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    Project Blasting Trials

    Initial Trials

    Small Samples in Controlled Conditions

    Establishing Baseline Comparisons

    Initial Shipyard Trials

    Small Samples in Shipyard Conditions

    Establishing Media Capability in Shipyards Full Scale Trials

    Blasting Marine Structures

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    Initial Controlled Trials

    Tests on Steel Plates

    Some Pipes

    Beams and other Structural Sections

    Established the capability of RGM

    Similar Performance to Grit

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    Initial Shipyard Trials

    Various Steel Plates from Ships

    RGM Compared to UHP

    RGM used wet as well as dry

    Compared in 2nd Shipyard to Copper Slag

    Samples blasted, inspected and coated

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    Plates prior to Blasting

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    RGM Closeup

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    RGM Blasting of Samples

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    Steel Samples after Blasting

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    Full Scale Shipyard Trials

    Mooring Barge

    Heavily Corroded Comparison between RGM and UHP

    Mooring Pontoon

    Heavily Coated

    Comparison between RGM and Copper Slag

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    Mooring Pontoon before Blasting

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    Mooring Barge before Blasting

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    Shipyard Trial Results (1)

    Abrasive Dry RGM Wet RGM Wet RGM UHPSize (mm) 0.75-1.5 0.75-1.5 0.75-1.5 N/A

    Surface

    cleanliness

    SA 2.5 SA 2.5 SA 2.5 SA 2.5

    Roughnessm

    2233 2207 2207 Could notbe measured

    Dust 2 1 1 1

    Productivity

    (m/h)

    4.19 1.62 4.63 5.15

    Specific GritConsumption

    (kg/m)

    19.33 115.74 42.74 186.48 lWater

    Table 1. Shipyard 1 Full Scale Trials with different media

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    Blasted Mooring Barge

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    Shipyard Trial Results (2)

    Abrasive Dry RGM Dry RGM Copper Slag Copper SlagSize (mm) 0.75 1.5 0.75 1.5 1.4 2.5 1.4 2.5

    Surface

    cleanliness

    SA 2.5 SA 2.5 SA 2.5 SA 2.5

    Roughness

    m

    95 2415 202 2396

    Dust 3 2 3 2

    Productivity(m/h)

    12.649 12.43 10.89 12.87

    Specific GritConsumption

    (kg/m)

    45.21 46.02 35.11 29.72

    Table 2. Shipyard 2 Full scale trials with different media

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    RGM Blasting of Pontoon

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    Pontoon after Blasting

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    Full Scale Shipyard Trials

    Comments

    RGM showed a steep learning curve

    Wet RGM was not very successful RGM gave improved appearance

    RGM is a Capable Process

    Further Monitoring is in Progress

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    Conclusions

    RGM Performance is Comparable to Other

    Media RGM is Equally Capable of Surface

    Preparation for Coating

    RGM has similar productivity to UHP

    Supplies of RGM at acceptable cost are

    essential

    Further work on disposal is required

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    Q & A

    George Bruce