Bhel Rsc Varanasi

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    HIGH CRONIC VIBRATION AT ANPARA

    U# 1

    Anpara Unit # 1 210 MW reported sever Axial andHigh Vertical vibration in Brg # 6 and Brg # 5 alsoshowed High Vertical Vibration

    High Vibrations were also noted in Stator Endshield and water header.

    The axial vibration and vertical vibration suddenlyincreased to the tune of above 50 microns ad

    machine had o be debarred

    Spectrum showed sever 2x components andother higher frequency components

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    USPV test

    Ultrasonic Pulse Velocity Test

    54KHZ , 24KHZ

    Velocity=Distance/time

    Homogeneity

    Presence of Cracks/voids, imperfections

    Change in structure which occurs with time

    PUNDIT :- Portable Ultrasonic Non-destructive Digital Indicative tester

    >4.5 Km/sec :- Excellent

    >4 km/sec :- Very good to Excellent

    3.5 to 4 Km/sec :-Good to very good

    3.0 to 4.0 km/sec :- Satisfactory but integrity suspected

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    PEAK TO PEAK

    NUMBER VIBRATION() NUMBER VIBRATION() pk-pk

    1 32.20 10 53.10

    2 30.00 11 45.80

    3 31.00 12 41.60

    4 34.70 13 32.40

    5 42.80 14 55.00

    6 41.80 15 32.10

    7 46.10 16 46.10

    8 47.10 17 65.4

    9 54.70 18 63.4

    15

    2

    1

    3

    456 7

    89

    10 11

    121314 16

    A CRACK IS BEING NOTICED(PIC S ATACCHED)17 18

    METAL BASE PLATE

    CIVIL FOUNDATION AREA

    BEARING NO .06 PADESTAL MAPPING(v)

    *READING OF THE COLUMN

    OF THE PEDESTAL WASTAKEN AT 6M AND 0M

    FRONT (BRG # 6)6 METER

    60.1

    0 METER 43.1

    REAR COLUMN BRG # 5 6

    METER 34.3

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    OBSERVATIONS

    THERE IS SEVERE VIBRATION IN THE STATOR WATER INLET ANDOUTLET LINE. DUMMY WOODEN SUPPORT AT BENDS WEREPROVIDED AND SOME REDUCTION IN VIBRATION WAS OBSERVEDBUT STILL NOTICABLE VIBRATION IS OBSERVED WHICH REDUCESGOING AWAY FROM THE GENERATOR

    THE ENDSHIELD OF TURBINE SIDE SHOWS NOTICABLE VIBRATION

    THERE IS VIBRATION IN FOUNDATION AREA OF BRG # 6 .

    THERE HAS BEEN DAMAGE OF COPPER TUBE OF THE BUSHING OF YPHASE IN APRIL 2013. THE TUBE WAS FOUND IN 2 PIECES (BROKEN)WE HAD INSISTED CUSTOMER FOR NFT BUT NFT HAD NOT BEENDONE

    SEAL OIL FLOW WAS AROUND 30L/MIN AT TE AND 35L/MIN IN EEWHICH HAS NOW INCREASED TO 45L/MIN IN TURBINE SIDE AND50L/MIN IN EXCITER END AFTER INCREASE IN VIBRATION IN BRG # 6

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    ACTION TAKEN1. INTEGRITY OF SECONDARY FOUNDATION GROUTING WAS SUSPCTED

    AND CHECKED BY NCCBM.

    2. INSPECTION OF FOUNDATION WAS ALSO DONE BY BHEL ENGINEERS3. UPV REVEALED HONEYCOMBING IN COLUMNS 11 & 12 AND ALSO

    CRACKS WAS FOUND IN SECONDARY GROUTING OF BRG # 6 PEDESTAL

    4. AS SUGGESTED BY NCCBM AND BHEL ENGINEERING ,THE HONEYCOMB

    IN THE FOUNDATION WAS REPAIRED BY PRESSURE EPOXY GROUTING

    AND SECONDARY GROUTNG WAS REDONE BY REMOVING BRG # 6 BASEPEDESTAL AND REGROUTING USING CONBETRAX GP2 .

    5. DESTRETCHING & STRETCHING OF FOUNDATION BOLTS WAS ALSO

    DONE.

    6. BRG. 4 WAS REPLACED

    7. GENERATOR ROTOR WAS REPLACED TO REMOVE GENERATOR INDUCED

    VIBRATION COMPONENTS.

    RESULTS : MACHINE SUCESSFULLY SYNCHRONISED WITH VIBRATIONS OF

    SHAFT BELOW 60 MICRONS PK-PK AND PEDESTAL BELOW 30 PK-PK IN

    ALL BRGS

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    MOULDS PREPARED FOR TEXT BEFORE SECONDARY GROUTING

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    MOULDS TEXTED FOR STRENGTH

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    Primary

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    BRG # 6 SPECTRUM AFTER RESTORATION WORK

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    NIT # 4 PANKI 105 MW HEAVY SPARKING AT EXCITER

    Heavy Sparking in exciter commutator of Unit # 4 Panki TPS was reported andsoon the problem rose to alarming level and machine had to be debarred onJune 21 2013.

    Vibrational analyses and electrical test were carried out by UPRVNL and basedon that following were suggested.

    1)Undercutting of mica on the commutator

    2)Carrying out the drop test on the commutator segments and on polepitchapart. This check will give you data about any dry soldering joints.

    3)Checking the commutator for any non uniform wear out

    4)Checking all the brush holders for their correct spring pressure andthe usage of correct grade of carbon brush.

    5)Check for the parallality of collecting mechanism arms.

    6)Check for the magnetic neutral axis of the collecting mechanism forany shifting during running of the Machine.

    7) Groove chamfering has to be carried out, using form tool

    Results : The sparking though reduced but still was totally resolved

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    ACTION TAKEN BY RSC VARANASI

    RSC ENGINEER VISITEDTHE SITE AND FOUNDTHAT THE UNDERCUTTING AND GOOVECHAMFERING WERE IMPROPER AND STILLDEMANDED MORE BUT THE COMMUTATORBEING OLD AND RESUED CONTINOUSLY RAISEDSUSPICIONS OVER POSSIBILITY OF FURTHERUNDERCUTTING

    THE EXCITER ARMATURE WAS SUGGESTED FORREPLACEMENT AND UNIT WAS BROUGHT BACKTO BAR WITHIN 7 DAYS.

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    Chronic axial Vibration Problem at Unit # 3 Unchahar TPS

    Unchahar Unit # 3 NTPC during overhauling inApril 2012 discussed with BHEL RSC Engineersregarding high axial vibration of LPT Rear

    Bearing Unit # 3. The axial vibrations were reportedly high to

    the tune of above 50 microns zero-pk andvelocity above 20 mm/sec

    The spectrum was analysed which revealedunloading of Brg # 4

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    U-3 LPT rear brg vibration

    0

    10

    20

    30

    40

    50

    60

    70

    11/20/00

    11/20/01

    11/20/02

    11/20/03

    11/20/04

    11/20/05

    11/20/06

    11/20/07

    11/20/08

    11/20/09

    Measurement Samples

    Velocity-mm/

    Axial

    Vertical

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    ACTION TAKEN

    1. CATENARY CORRECTION AND DECK CORRECTION

    2. PROPER BLUE MATCHING OF BRG WITH TORUS AS WELL AS TORUSWITH PEDESTAL

    3. DESTRETCHING & STRETCHING OF FOUNDATION BOLTS WERE

    CARRIED BUT THE REAR BRG WAS STRETCHED TO 2.43 AND THE

    FRONT BOLTS WERE STRETCHED TO 2.30 DEVIATING FROM THRNORMAL APPROACH OF STRETCHING THE FRONT TO A HIGHER

    VALUE AS COMPARED TO THE REAR .

    4. ALIGNMENT CORRECTION .

    RESULTS

    The axial vibration were brought to below 25 microns and

    velocity to less than 8 mm/sec.

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    U#3 PEDESTAL 4 BOLT STRETCHING

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    STRETCHING DETAILS U # 3 BRG NO

    4,O/H 12

    BOLT NO. DESIGN

    VALUE

    STRETCHI

    NG VALUE

    FRONT-L 1.83 2.30

    FRONT-R 1.83 2.30

    REAR-L 1.80 2.43

    REAR-R 1.80 2.43

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    SEVERE EARTH FAULT AT DEVIGHAT NEPAL(MACHINE BROUGHT TO GRID WITHIN 20 DAYS)

    NEA had reported about the earth fault of stator Unit # 2,Devighat. BHEL RSC engineer reported at site on 3/01/12for attending the earth fault. The fault after analyses wasfound to be severe in nature and had resulted in melting

    of overhang portion of two coils of B phase and burningdown of insulation of the nearby three other coils.

    Constraints : Space constraint on removal of poles & Timeon removal of rotor.

    Solution: Stator Removal Causing Both Time, Cost andWork easier

    Machine Relevelled aligned and Brought Back to Grid on23/1/12 with better running parameters compared to

    other running Units

    Aft l t f th i di id l il HV f th

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    IR AND PI AFTER PLACEMENT OF STATOR AND

    FINALISATION OF LEVELLING AND ALIGNMENTDATE 15/1/2012

    15 secs 60 secs 600 secs PIR-E 1000 3500 9000 2.57

    Y-E 1000 3500 9500 2.71B-E 1000 3250 8500 2.62RYB- E 200 1500R-Y 2500 8500B-Y 2500 8000

    Y-B 2500 8000

    After replacement of the individual coils HV of the new

    coils were carried out at 14.2 KV for 1 minute.

    After finalization of the stator the HV of all coils/phases

    was carried out at 9Kv in two parts.The stator was then re-position and final IR & PI was

    recorded.

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    U# 2 with better

    vibration

    parameters as

    compared to U #

    3