Aux power

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    IB THERMAL POWER STATION

    CertifiedISO 14001 : 1996 standard

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    The Company

    Orissa Power Generation Corporation

    conceived on 14th

    November-1984,owns Ib Thermal Power Station witha capacity of 420 MW at Ib valleyarea of Jharsuguda district in theState of Orissa.

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    The Company

    OPGC is committed to provide clean,lowcost and reliable power to the state.

    It has also highest commitmenttowards safety and clean environment.

    It has obtained a number of awardsboth from state and center for itsremarkable achievement in different

    fields.

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    Award Winning Performance of

    OPGC

    Recipient of meritorious performance awardfrom MOP, GOI for the year 00-01,03-04.

    Certificate of merit from MOP,GOI for low spoil consumption for the year 2001,2002 &2003.

    Green tech environment Gold award for 03-04. Best environment management award from

    Directorate of Factories for the year 2002-2003.

    Green tech safety gold award for 2004-2005.

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    Energy ConservationProgrammeat

    Ib Thermal Power Station

    Efficiency Department

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    ACTION PLANS For Aux. PowerReduction.Operation & Maintenance

    Duct Repair using castable ceramite coating

    during annual outageInstallation of Soft touch seal in Air-Preheater

    PA duct & Expansion Joint Repair

    Condenser cleaning for improvement ofvacuum

    Repair & Replacement of BFP R/C valves

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    ACTION PLANS For Aux. PowerReduction.MODIFICATIONS

    PRDS modification

    HP bypass spray system modification

    BFP re-circulation valve modification

    Air pre-heater baskets replacement

    Flue gas duct repairs / modification

    Efficiency Department

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    ACTION PLANS For Aux. PowerReduction.CAPITAL INVESTMENT

    Using FRP blades for CT fans in Cooling Tower

    100 % dry ash modification

    Installation of VVF drive in selected auxiliarie

    Installation of capacitor banks in HT motors

    Efficiency Department

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    Energy conservation by Heat RateImprovement.OPERATING PRACTICE

    Continuous Blow down operation is beingregulated as per requirement

    Intelligent Soot blowing operation

    Startup & stabilization optimizationTrip analysis & recommendation forrectification

    Efficiency Department

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    Energy conservation by Heat RateImprovement.Combustion Optimization

    Dirty Pitot tube test for setting fuel/Air Ratioand velocity deviation

    Automatic Ash Sampling is to be installed forLOI optimization

    Hot Foil LOI Analyser procurement for smartLOI analysis

    FG gas analysis for Co trimming in Furnace

    Efficiency Department

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    Energy conservation by Heat RateImprovement.Performance Testing

    Condenser Air-ingress test by Heliumdetection

    Condenser performance testing

    Heater performance testingBFP performance testing

    Efficiency Department

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    OUR ONGOING IMPORTANT PROJECTS

    .

    Duct Modification

    PRDS modification

    HP Bypass System Modification Smart Soot blowing

    Condenser Cleaning

    FRP blades in CT fans

    Dry Ash Evacuation system

    BFP Re-Circulation Valve Replacement

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    DUCT MODIFICATION

    Before unit 2 annual overhauling, the IDfans were drawing 155 amp (at full load).

    In overhauling the ducts were opened &found there were holes in the bends andcorners of ducts. The holes were formed

    due to flue gas erosion especially wherethe direction of velocity changes.

    Efficiency Department

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    In the overhauling, the castablerefractory was applied on the bends &

    corners of duct.

    After undertaking the modification workin ducts, the current drawn by the IDfans was reduced to 15 amp (at sameload)

    So by applying castable refractory andwelding work in ducts, there is a saving of15 amp / ID fan.

    Efficiency Department

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    Ceramite coating

    in the bend

    Efficiency Department

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    castable

    refractory in the

    corner

    Efficiency Department

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    Repair of Ducts

    Recurring problem

    Increases load on ID fan

    Expected expenditure for repair Rs.10lacs

    Payback period < 6 months

    Long term Modify the ducts to reducefriction leading to saving in Aux Consumptionand life

    Gas Distribution test

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    PRDS system

    Both pressure reducing and spray valvehave passing.

    Old design- OEM, IEL not able to solvethe problem

    Modifying to proven design of CCI

    Expected cost Rs.50 lacs

    Savings 8~10 Kcal

    Pay back period

    two years

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    HP Bypass system

    HP bypass control valve and spray valves arepassing

    For HP bypass valve improved seat is sourcedfrom OEM CCI Sulzer

    Spray valve is being replaced with new proven

    design of CCIExpected cost Rs 60 lacs

    Saving 14 kcal

    Pa back three ears

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    Smart Soot Blowing

    System

    Approx cost 1.2 Crores per unit

    Pay back period ~3 yearsSoot blowing only when required, saving inheat rate and reduce chances tube failure,

    increase overall heat transferFinal decision yet to taken

    Feasible only in 2006 annual shutdownEfficiency Department

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    CT FANSCT fans of both the units were installedby M/s Paharpur Cooling Towers Ltd. Withblades made of glass wool filled solid blades.

    Power consumption per fan was 48 Kw withnormal flow rate of 929023 CFM.

    It was proposed to replace the solid bladeswith hollow ones for economic power

    consumption.

    Efficiency Department

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    Fan

    Motor

    CW IN Flow CV

    Open Hot w ater Distribution basin

    Louvers

    Drft Eliminator

    Splash fill

    Or Splash Bar Air Flow

    Basin CW OUT

    CROSS FLOW INDUCED DRAFT COOLING TOWEREfficiency Department

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    Accordingly FRP hollow blades from M/sEncon Ltd have been replaced in 12 no of CT

    fans. By installing FRP blades the energy

    consumption reduced to 30 Kw, withimprovement of flow rate to 1774899 CFM.

    Energy saving over the old solid blades isaround 30 to 35%.

    Efficiency Department

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    Energy Saving

    Around 18 KW is being saved per fan.

    Assuming 335 days/year of operation of a

    fan, the total energy saving will be 0.145MU.

    The cost of energy saving will be Rs. 1.5lacs / year.

    Cost of one FRP fan is Rs 2.6 lacs(approx).

    Efficiency Department

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    Dry Ash Collection System

    Erection of Dry Ash Collection System bydense phase evacuation is started by M/s

    Ultratech & M/s OPGC The Fly Ash from 2nd Field onwards will be

    supplied to M/s Ultratech

    Energy saving from wet Ash Handlingsystem

    Efficiency Department

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    Efficiency Department

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    Energy Saving

    One LP pump will run in stead of 2

    One HP pump will run in stead of 2

    One series of Ash slurry pump will run instead of 2 series

    One of the Recycle pump can be stoppedout of 2 running pumps

    Efficiency Department

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    Energy Savings

    Additional 2 nos compressors are required

    Additional 2 nos of blowers

    Additional 2 nos Silo fluidizing Blowers

    Net saving in Energy 900 kw

    Efficiency Department

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    Arresting BFP Recirculation ValvePassing

    By replacing the BPF Re-circulation valvefrom M/s IEL make to M/s MIL around 15

    Amps saving is achieved per BFP This saving is achieved after arresting the

    Recirculation valve passing

    Around 145 Kw saving is achieved

    Efficiency Department

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    Efficiency Department