Aux power
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Transcript of Aux power
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IB THERMAL POWER STATION
CertifiedISO 14001 : 1996 standard
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The Company
Orissa Power Generation Corporation
conceived on 14th
November-1984,owns Ib Thermal Power Station witha capacity of 420 MW at Ib valleyarea of Jharsuguda district in theState of Orissa.
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The Company
OPGC is committed to provide clean,lowcost and reliable power to the state.
It has also highest commitmenttowards safety and clean environment.
It has obtained a number of awardsboth from state and center for itsremarkable achievement in different
fields.
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Award Winning Performance of
OPGC
Recipient of meritorious performance awardfrom MOP, GOI for the year 00-01,03-04.
Certificate of merit from MOP,GOI for low spoil consumption for the year 2001,2002 &2003.
Green tech environment Gold award for 03-04. Best environment management award from
Directorate of Factories for the year 2002-2003.
Green tech safety gold award for 2004-2005.
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Energy ConservationProgrammeat
Ib Thermal Power Station
Efficiency Department
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ACTION PLANS For Aux. PowerReduction.Operation & Maintenance
Duct Repair using castable ceramite coating
during annual outageInstallation of Soft touch seal in Air-Preheater
PA duct & Expansion Joint Repair
Condenser cleaning for improvement ofvacuum
Repair & Replacement of BFP R/C valves
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ACTION PLANS For Aux. PowerReduction.MODIFICATIONS
PRDS modification
HP bypass spray system modification
BFP re-circulation valve modification
Air pre-heater baskets replacement
Flue gas duct repairs / modification
Efficiency Department
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ACTION PLANS For Aux. PowerReduction.CAPITAL INVESTMENT
Using FRP blades for CT fans in Cooling Tower
100 % dry ash modification
Installation of VVF drive in selected auxiliarie
Installation of capacitor banks in HT motors
Efficiency Department
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Energy conservation by Heat RateImprovement.OPERATING PRACTICE
Continuous Blow down operation is beingregulated as per requirement
Intelligent Soot blowing operation
Startup & stabilization optimizationTrip analysis & recommendation forrectification
Efficiency Department
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Energy conservation by Heat RateImprovement.Combustion Optimization
Dirty Pitot tube test for setting fuel/Air Ratioand velocity deviation
Automatic Ash Sampling is to be installed forLOI optimization
Hot Foil LOI Analyser procurement for smartLOI analysis
FG gas analysis for Co trimming in Furnace
Efficiency Department
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Energy conservation by Heat RateImprovement.Performance Testing
Condenser Air-ingress test by Heliumdetection
Condenser performance testing
Heater performance testingBFP performance testing
Efficiency Department
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OUR ONGOING IMPORTANT PROJECTS
.
Duct Modification
PRDS modification
HP Bypass System Modification Smart Soot blowing
Condenser Cleaning
FRP blades in CT fans
Dry Ash Evacuation system
BFP Re-Circulation Valve Replacement
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DUCT MODIFICATION
Before unit 2 annual overhauling, the IDfans were drawing 155 amp (at full load).
In overhauling the ducts were opened &found there were holes in the bends andcorners of ducts. The holes were formed
due to flue gas erosion especially wherethe direction of velocity changes.
Efficiency Department
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In the overhauling, the castablerefractory was applied on the bends &
corners of duct.
After undertaking the modification workin ducts, the current drawn by the IDfans was reduced to 15 amp (at sameload)
So by applying castable refractory andwelding work in ducts, there is a saving of15 amp / ID fan.
Efficiency Department
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Ceramite coating
in the bend
Efficiency Department
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castable
refractory in the
corner
Efficiency Department
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Repair of Ducts
Recurring problem
Increases load on ID fan
Expected expenditure for repair Rs.10lacs
Payback period < 6 months
Long term Modify the ducts to reducefriction leading to saving in Aux Consumptionand life
Gas Distribution test
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PRDS system
Both pressure reducing and spray valvehave passing.
Old design- OEM, IEL not able to solvethe problem
Modifying to proven design of CCI
Expected cost Rs.50 lacs
Savings 8~10 Kcal
Pay back period
two years
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HP Bypass system
HP bypass control valve and spray valves arepassing
For HP bypass valve improved seat is sourcedfrom OEM CCI Sulzer
Spray valve is being replaced with new proven
design of CCIExpected cost Rs 60 lacs
Saving 14 kcal
Pa back three ears
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Smart Soot Blowing
System
Approx cost 1.2 Crores per unit
Pay back period ~3 yearsSoot blowing only when required, saving inheat rate and reduce chances tube failure,
increase overall heat transferFinal decision yet to taken
Feasible only in 2006 annual shutdownEfficiency Department
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CT FANSCT fans of both the units were installedby M/s Paharpur Cooling Towers Ltd. Withblades made of glass wool filled solid blades.
Power consumption per fan was 48 Kw withnormal flow rate of 929023 CFM.
It was proposed to replace the solid bladeswith hollow ones for economic power
consumption.
Efficiency Department
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Fan
Motor
CW IN Flow CV
Open Hot w ater Distribution basin
Louvers
Drft Eliminator
Splash fill
Or Splash Bar Air Flow
Basin CW OUT
CROSS FLOW INDUCED DRAFT COOLING TOWEREfficiency Department
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Accordingly FRP hollow blades from M/sEncon Ltd have been replaced in 12 no of CT
fans. By installing FRP blades the energy
consumption reduced to 30 Kw, withimprovement of flow rate to 1774899 CFM.
Energy saving over the old solid blades isaround 30 to 35%.
Efficiency Department
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Energy Saving
Around 18 KW is being saved per fan.
Assuming 335 days/year of operation of a
fan, the total energy saving will be 0.145MU.
The cost of energy saving will be Rs. 1.5lacs / year.
Cost of one FRP fan is Rs 2.6 lacs(approx).
Efficiency Department
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Dry Ash Collection System
Erection of Dry Ash Collection System bydense phase evacuation is started by M/s
Ultratech & M/s OPGC The Fly Ash from 2nd Field onwards will be
supplied to M/s Ultratech
Energy saving from wet Ash Handlingsystem
Efficiency Department
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Efficiency Department
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Energy Saving
One LP pump will run in stead of 2
One HP pump will run in stead of 2
One series of Ash slurry pump will run instead of 2 series
One of the Recycle pump can be stoppedout of 2 running pumps
Efficiency Department
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Energy Savings
Additional 2 nos compressors are required
Additional 2 nos of blowers
Additional 2 nos Silo fluidizing Blowers
Net saving in Energy 900 kw
Efficiency Department
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Arresting BFP Recirculation ValvePassing
By replacing the BPF Re-circulation valvefrom M/s IEL make to M/s MIL around 15
Amps saving is achieved per BFP This saving is achieved after arresting the
Recirculation valve passing
Around 145 Kw saving is achieved
Efficiency Department
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Efficiency Department