A Leading Pharmaceuticals Company - saspowertech

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Page 1 of 46 POWER QUALITY ANALYSIS REPORT FOR By SAS Powertech Pvt Ltd. 101, Gera's Regent Manor, Survey No. 33, Area No. 39/570, Behind Opulent Car Care Center Baner, Pune 411045 Tel: 020 25533015/16/17 email: [email protected] Audit Period : : 14 th Dec to 18 th Dec 2015. A Leading Pharmaceuticals Company

Transcript of A Leading Pharmaceuticals Company - saspowertech

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POWER QUALITY ANALYSIS REPORT

FOR

By

SAS Powertech Pvt Ltd.101, Gera's Regent Manor, Survey No. 33, Area No. 39/570,

Behind Opulent Car Care Center Baner, Pune 411045

Tel: 020 25533015/16/17email: [email protected]

Audit Period : : 14th Dec to 18th Dec 2015.

A Leading Pharmaceuticals Company

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INDEX

Sr.No Description Page No.

10 Major observations during audit 16 to 1811 Current and Voltage harmonics Compliance Limits 19

12 Analysis of historical data on Energy consumption andDivision of Electrical load between various sections 20 & 21

13 Power Quality parameters and comments at 33KV 22 to 2414 Power Quality parameters and comments at TR 1 secondary 25 & 2615 Power Quality parameters and comments at TR 2 secondary 27 to 2916 PQ parameters for feeder HVAC MCC2 GENE 237 30 To 3217 PQ parameters for feeder HVAC MCC 04 33 & 3418 PQ parameters for PMCC3 – GENE 244 35 to 3819 PQ Parameters for PMCC 39 to 4120 Voltage trends at 33KV, Tr1 Sec, Tr2 Sec 4221 Consolidated feeder wise PQ report for all feeders 43 & 44

22 UPS input & output side PQ parameters and Overallefficiency 45

23 Results of earthing check 46

1 Index 22 Site Details 33 Methodology of Audit 44 List of Abbreviation 55 Acknowledgement 66 A note on Power Quality 7 & 97 Executive Summary 10 to 128 HT infrastructure out of Plant and comments 139 Description Of electrical Infrastructure 14 & 15

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SITE DETAILS

Site Name

Analysis Period 14th Dec To 18th Dec 2015

Audit Conducted By Mr. Vijay Sonawne & Sandesh Biramane

Equipment UsedFor Analysis

KRYKARD ALM35 Power QualityAnalyzer

Chauvin Arnoux,France

Contact Person

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Methodology of Power quality audit conducted:

After visiting, surveying and understanding above infrastructure, we decided to follow followingmethodology for this audit.

Audit aim and Methodology: Record electrical parameter data at 33KV, 433V LT PCC at both transformers secondary for

around 24 hours. Record electrical parameter data at feeders identified by maintenance staff, where repeated

electronic failures are reported for around 24 hours. Record power quality parameter data at all sub distribution feeders and UPS outputs. Study above data and if required, recommend harmonic mitigation solutions at various levels in the

distribution to suppress the distortion and improve power quality. Study above data to know status of reactive power compensation provided at various locations and

their effects. Record electrical parameter data at all major UPS outputs to know current and voltage harmonic

levels of load – as supported by them. Conduct meeting with maintenance teams to understand nature of electrical failures / automation

failures and their frequency. Study relationship between failures and PQ parameters if any. Monitor sub cycle level disturbances at critical levels in the distribution and also at problem areas

located by maintenance team. Undertake infrared thermography to locate lose contacts, which can cause power quality issues

along with elevated temperatures. Undertake earthing audit to ensure quality of earthing using loop earthing test method. Analyse all above collected data and prepare report based on above to locate issues related power

quality and remedies to rectify the same if any.

Audit team:

SAS Powertech Pvt Ltd.

Mr. Narendra Duvedi. – Lead Auditor B.E. Electrical with specialization in power electronics 35 years experience. Bureau Of Energy Efficiency –certified ENERGY AUDITOR BVQI certified Lead Auditor for ISO 50001. Chartered Engineer.

Mr. Vijay Sonawne. – Diploma Electrical Engineering with more than 10 years field experience. Data collection engineer.

Mr. Sandesh Biramane Diploma Electronics Engineering Data collection engineer.

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LIST OF ABBREVIATION

MLTP

Main LT panelPQA Power quality analysisVrms

Phase to neutral voltageUrms

Phase to phase voltageArms

CurrentAvg.

AverageMin.

MinimumMax.

MaximumIthd

Total harmonics distortion in currentVthd

Total harmonics distortion in voltagePF Power factorPCC Power control circuit/point of common couplingTDD Total demand distortionTHD Total harmonics distortionDB Distribution boardDG Diesel generatorLT Low tensionIEEE

Institute of electrical and electronics engineersNEC National electric codeSLD Single line diagramUPS Uninterrupted power supply

COLOUR CODE

Red R-Phase / Line-1 / Phase-1 / R-YYellow

Y-Phase / Line-2 / Phase-2 / Y-BBlue B-Phase / Line-3 / Phase-3 / B-RBlack NeutralTotal GreenKWtotal

RedKVARtotal

Blue

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ACKNOWLEDGEMENT

We do hope you will find our recommendations useful in helping you to improve thepower quality of your electrical system

We wish the management success in their Endeavour to improve power quality.

For SAS Powertech, Pune Certification:Report Certified by:

Abhijiit Katre Narendra R. Duvedi.Authorized Signatory (B.E. Electrical and Certified Energy Auditor Reg. No: EA 10859)

We are thankful to the management of A Leading Pharmaceuticals Company . Forgiving usan opportunity to conduct power quality analysis at their premises.

We are also thankful to team of A Leading Pharmaceuticals Company for the helpandco-operation during Power Quality Analysis.

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A note on electrical Power quality, it’s importance, effects and remedies.

Commercially available AC – alternating electric power is usually available in “Sinusoidal”form. The main specifications of this are “Value of Voltage”, “Waveform” and “Frequency”.

In case of 50Hz frequency, each cycle takes 20msec to complete. Frequency variation cancause trouble to connected load and as such it should be as constant as possible. Iron losses inmotors, transformers etc change with frequency. The Grid power frequency is usuallymaintained within +/- 1Hz.

The electric distribution equivalent circuit is as follows

The waveform of voltage available across load may get affected and deviate from Sinewavedue to various reasons like drawing non sinusoidal currents containing harmonic components,defects in generators (Alternators or UPS systems), higher source impedance, overloading,etc. If (Source + Cable) impedance is negligible in comparison with Load impedance underall conditions, the source is termed as “Infinite bus” and then the problems are less.The distorted voltage waveform can affect equipment performance. Such distorted voltagesand currents can result into overheating of cables, transformers etc and can also causeexcessive voltage drops.

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Example of distorted current –.

Voltage disturbances could be “sub - cycle” as shown bellow or “Sustained”. Sub - cycledisturbances are known as transients and sustained disturbances are known as “Sags” or“Swells”. A sub classification is also known as “Voltage dip”

These power quality issues if present in available power supply can affect performance andreliability of critical loads like complex automation systems, communication devices anddigitally controlled power electronic circuits and reflect into unwanted resetting digitalcircuits like PLCs, VFD controllers etc.

In practise, the source, transmission level transformers, switchgear and part of cablingbelongs to utility company and once the feeder enters the premises of consumer, theinfrastructure belongs to consumer. If large amount of harmonic currents are demanded byload and are required to be supplied by utility company, the utility company equipment is alsosubjected to ill effects of these power quality disturbances. In view of limiting commercialimpact of this demand raised by consumer, normally utility companies bind consumer intolegal compliance requirements related to power quality. Such requirements usually are basedon some international standards. One such standard related to harmonic complianceapplicable at “Point of common coupling” or PCC is IEEE 519 1992.

Voltage regulation and dynamic response (Value of Dip or Rise and Time required forcorrection) are noticeable parameters of small capacity power supplies like DG sets, UPSsystems etc, which affect performance of critical loads if found beyond permissible limits.The applicable standard related to assess performance of UPS systems is IEC 62040 – 3

In view of avoiding effects of power quality on setup, it is required that available quality ofpower should be matched with specific requirement of critical equipment for smooth andreliable operation. If this is not possible then a suitable power conditioning equipment likeUPS / stabilizer / Series voltage correctors etc needs to be added in series after matching UPSoutput specifications with requirement of critical load.

Distorted Current.

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Visible effects of power quality issues.

Equipment malfunction. Equipment failure, especially related to controlled rectifiers and front end components. Control Power supply failures and associated damages to subsequent circuits. Abnormal heating of electrical conductors, nuisance tripping. Insulation failures. Loosing Load and Motor alignment frequently due to harmonic torques developed in the

motor.

Electrical compatibility and reliable equipment design.

Although providing good quality of power is important, “Electrical Compatibility” is more critical. Itis always advisable that the equipment manufacturer should decide detail power quality and workmanship compatibility requirements, exchange them among all stakeholders – namely

1) Critical equipment manufacturer,2) End user,3) UPS / SERVO STABILIZER / TRANSFORMER manufacturer4) Contractors involved in executing the project.

Depending upon project value and seriousness of known issues related to power quality, a third partycompliance / validation audit can be called for at the time of commissioning / execution and / or afterabout one month of operation. During such audits one can also decide periodicity of such inspectionalong with SOPs for predictive and preventive maintenance to get continual satisfactory performancefrom the equipment. During such audit, legal compliance as per requirements of utility company canalso be checked.

Lastly one should also note that there could be design related issues with the equipment, which canaffect reliable operation. Such issues may affect the performance despite of offering good qualitypower. It is very important to consider this while undertaking root cause analysis of failure of anequipment working on electrical power.

Acceptability of Power quality parameters have been decided in various international standardspublished by reputed world famous organizations like IEEE, IEC, NEMA etc. If equipmentmanufacturer commits that he can accept the power as per these standards, then the power quality canbe checked as per these standards during the audit, otherwise the compliance has to be ensured againstrequirements of equipment manufacturer.

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Executive Summary of findings and recommendations:

1) During this audit 33KV GEB incoming supply power quality was monitored for 24 hours. Largenumber of voltage alarms and voltage transients were recorded during this monitoring.

3) IGBT based series voltage correcting devices are now available in the market, which detect adisturbance in 2 msec and correct in 5 msec. They can support the load for few seconds even onphase loss. Such devices have unlimited over load capacity and 98% overall efficiency from 10%to 100% load. These devices can offer current balancing, waveform correction and correctionagainst up to 40% dips. These products are expensive and paybacks will be justified if they arerequired to cover production loss and associated time value of the same along with expensestowards breakdown maintenance.

4) We have carried out Infrared thermography of entire electrical installation and have included thereport here with. We understand that plant maintenance team has IR imager and carry out imagingas predictive maintenance practice. It is recommended that the same should be carried out once insix months and a “pre imaging” – Shutdown and maintenance – “post imaging” format should befollowed to ensure effectiveness of maintenance.

5) We have carried out earthing audit using loop testing method and the report indicates that “TR2Neutral earthing resistance” is on higher side and needs attention.

6) We have recorded all input / output parameters of UPS systems. Total UPS load is around 6% ofrunning load. However almost all UPS systems have thyristor input rectifier stages and as suchdemand huge harmonic currents. Further the capacity utilization of these UPS systems as appearedduring audit was very poor. It is advised that whenever you replace these UPS systems you shouldopt for transformer less designs with input side power factor and current harmonics corrected as abuilt in facility.

7) Reactive power compensation at present is offered centrally using contactor switched detunedfilters. This is automatic and is taking care of maintaining power factor at close to unity and hasavoided current harmonic amplification to some extent. This has relived both the transformers andupstream HT distribution from handling large harmonic currents. However lot of loads are nonlinear and almost all power control / motor control centers in the plant deliver required harmoniccurrents to respective loads. The power quality at few loads is disturbed due to this. We haveenclosed detail analysis and remedies in for this in this report.

8) As per information received during audit, some equipment connected via MCCs and PCCs totransformer 2 have suffered from repeated failures.

2) A Leading Pharmaceuticals Company receives 33 KV GEB supply through RMU arrangement located outside the plant. Thisarrangement involves lot of cables and switches emerging from VERNA substation. This shouldbe thoroughly checked to rule out possibility of lose contacts, adequacy of cable / conductor sizeand inadequate source capacity.

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9) During specific investigation of point 8, following observations are recorded

a) TR 2 neutral earthing should be checked and redone, earthing resistance is 4.6ohms.b) TR 2 secondary recorded 63 voltage alarms during 24 hours recording; minimum voltage was

321volts while maximum was 439 volts.c) HVAC MCC 2 (GENE 237), HVAC MCC 04, Process MCC 3 (GENE 244), PMCC feeders

emerging from TR 2, were monitored for 24 hours. All these feeders recorded voltage alarmsand transients.

d) The loads connected to above feeders are non linear and harmonic currents result intoincreased voltage distortion, K factor etc. We have recommended active harmonic filters atthese feeders to reduce above ill effects. The cables used on incoming side of these feedersshould be validated for capacity (with specific reference to harmonic currents) as the voltagedistortion increases at downstream end.

e) Following active filters are recommended, however the implementation may be done fortransformer 2 initially.

Sr Feeder Suggested Active Filter1 TR 1 -

PADP 4 100AUtility MCC3 100A

2 TR 2 -HVAC MCC 60AAir Compressor 100APCC 3 100AHVAC MCC 2 GENE 237 60 AHVAC MCC 04 60AProcess MCC 3 GENE 244 60A

10) Following loads from the load list appear to be large loads. Few of them have VFDs / Softstarters connected where as few of them have DOL or star – delta starters.

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33KV side current pattern

TR 1 current pattern

TR2 current pattern

These current pattern show that there are large hiccups in load current, especially in case oftransformer 2, where most of the utility equipment are connected. This transformer is delivering about1000Amps RMS current as base load and on top of this if a large motor starts with Star delta starter,the staring inrush being 6 to 7 times full load current, can give rise to a voltage dip, which may createissues with other sensitive equipments. We recommend all such loads as listed above should have softstarters. Further wherever soft starters and VFDs are installed, inrush current ramp is alwayssettable. This facility should be used especially on all thermal systems like HVAC pumps and AHUs,where if these devices take few seconds to attain full speed, it does not affect the process, where asinrush currents get limited.

-------------------------------------------- END OF SUMMARY-----------------------------------------

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The 33 KV distribution arrangement with various cables and RMUs emerging from VERNA substation as“Circled” above needs to be checked for loose connection along with upstream source capacity.

This may throw light on frequent fluctuations observed on 33KV side. The source may occasionally be gettingoverloaded due to neighbouring Industries.

Another reason could be ill maintained upstream tap changers.

If you can expect co operation from GEB staff, this report may be shared with them and joint survey ofupstream electrical infrastructure coupled with maintenance should be planned.

If we know capacity and % impedance of upstream transformer along with it’s normal loading pattern, adequacyof source capacity can at least be ruled out.

HT infrastructure out of plant

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33KV1500 KW

TR-1 KVA 2000KVA

850KW

TR-2 2000KVA

810 KW

DG sets1250KVA x 3Synch

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33KV1500 KW

TR-1 KVA 2000KVA

850KW

TR-2 2000KVA

810 KW

DG sets1250KVA x 3Synch

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33KV1500 KW

TR-1 KVA 2000KVA

850KW

TR-2 2000KVA

810 KW

DG sets1250KVA x 3Synch

Description of electrical infrastructure

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Monthly KWh consumption chart prepared from electricity bills.

Peak loading on transformers during the audit matches maximum MD recorded so one can concludethat this the plant load was at it’s peak during the audit. The process being of batch processing type,the electrical load varies continuously and the peak demand may not prevail always.

A Leading Pharmaceuticals Company receives 33KV from Goa state Electric Supply Authority at a VCB and pole structure insidethe compound. HT cable is laid from this point to HT distribution ( 1 x 2) inside the plant. This panelhas 3 VCBS – arranged as one incoming and two out going. The contract demand is 2500 KVA andthe load is further fed through 2 x 2 MVA 33KV/433V transformers. The feeder wise KW loadrecorded is as shown above. The individual UPS input KW are also mentioned in above diagram. Thefigures recorded are maximum figures and approximately match with the KWH chart shown bellowfor Months Jan 2015 to Nov 2015.

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Major observations during Power quality audit.

1) Above trend shows that the KW load varies between 1200KW to 1600KW depending upon processneeds.

2) Above trend shows that during recording period of 21 hours and 38 minutes the plant consumed30320Kwh. This makes it 33636 Kwh / day or approximately 874561 Kwh per month. Most of theutility feeders receive direct raw power, where as critical loads receive power through UPS. Theinstalled UPS capacity is 500 KVA and the peak loading observed during audit was 100KW. Fewmost critical loads are fed through “Parallel Redundant” UPS configurations.

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3) Current harmonic distortion varies from 7% to 13%. The compliance requirement as per IEEE519 1992 – may turn out to be 10 to 12%. (This is a guess as per our experience of capacity ofupstream infrastructure created by various electricity boards in other states)

4) The power factor as above is maintained close to unity. The plant has installed detuned filters,which are contactor switched. These filters work in automatic mode and maintain the powerfactor close to unity irrespective of load variation.

Above table shows major load centers which demand harmonic currents. Based on above data andplant areas where maintenance issues are located, some power quality mitigation solutions aresuggested in this report.

5) We have monitored ‘Alarms and Transients’ at critical locations while recording powerquality parameters for 24 hours. The Alarm was set at +/- 10% of nominal voltage whereas

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the transient threshold was set at 33% of respective Line to neutral voltage. Following issummary of recorded observations.

In 90% of the cases, HT 33KV side alarms are voltage dips as shown bellow. They are notalways associated with increase in plant loading due to inrush currents etc. Following tableshows a sample. 33KV input dropped for about 620msecs, i.e. 31 cycles to 16KV. Such dipscould be because of source capacity of input, loose contacts in HT service connection external tothe plant, or inrush loading of industries in neighbourhood.

Plant loads have few high inrush current motor loads, which become ON and OFF as per processrequirement. As per the list made available to us, Chillers and Heat pump do not have VFDs orSoft starters. They require high inrush currents. Air compressor has a soft starter. All soft starterramps should be adjusted as “Soft” as possible to avoid inrush currents. Most of other motorloads have VFDs connected to them. Acceleration time should be adjusted to suit load torquerequirement, but as “Soft” as possible to avoid inrush currents.

These frequent voltage dips can cause maintenance issues in automation systems employingelectronics, VFDs etc. One can also note that transients - “Sub cycle disturbances” are alsopresent on above feeders, which are remarkable in numbers.

6) Voltage harmonic distortion recorded at all feeders is below 4% on raw power and between 4 to5% on DG sets, which is within acceptable limits.

7) Both the transformers are loaded around 40% if average loading is concerned and around 60% ifpeak loading is considered. This is within acceptable limits, but considering that most of the load isnonlinear, you should increase the loading by maximum 10%. Further non linear loading mightresult into increase in voltage distortion.

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Current and voltage Harmonics compliance limits:

We tried to locate harmonic compliance requirements from JERC website, which is jointelectricity regulatory commission for Goa and other Union territories. We could not locate adocument giving exact requirements.

As per international standard practice and the practice followed by most of the states in India, aninternational standard - IEEE 519 1992 is referred for harmonic compliance between a utilitycompany and a consumer. The procedure given in this standard requires calculating a ratio Isc/ILwhere: Isc = short circuit current of upstream utility company EHT supply transformer from which

the consumer gets HT supply. IL = Average load current of load running at consumer premises.

Once this ratio is known, one can refer following table to know % total current harmonicscompliance limits.

Maximum harmonic current distortion in percentage of IL for voltages lessthan 22KV.

Individual harmonic order (odd harmonics)Isc/IL <11h 11≤h<17 17≤h<23 23≤h<35 35≤h<49 TDD<20 4.00 2.0 1.5 0.6 0.3 5.00

20<50 7.00 3.5 2.5 1.0 0.5 8.0050<100 10.00 4.5 4.0 1.5 0.7 12.00

100<1000 12.00 5.5 5.00 2.0 1.0 15.00>1000 15.00 7.00 6.00 3.5 1.4 20.00

Even harmonics are limited to 25% of odd harmonic limits above.

The code also says that the % total voltage harmonics should be less than 5% for voltages up to66KV.

Following table shows calculations for Isc/IL.

Parameter ValueGEB Transformer Capacity MVA 40

GEB Transformer % Impedance 8

GEB Transformer full load current @33 KV 699.84

GEB Transformer SC current @33 KV = Isc 8747.99

Wattson contract Demand KVA 2500

Max current as per contract demand on 33KV side 3436.71

Max measured current on 33KV side at normal load 2393.10

Isc / IL Ratio as per contract demand 194

Isc / IL Ratio as per Max Plant Current 278

As per Contract Demand and plant Max current the current harmonics compliance limit is 15%as the ratio is between 100<1000.

Client: A Leading Pharmaceuticals Company

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Analysis of historical data collected at Site.

Monthly KWh consumption Since Jan 2015

.This table shows that electrical consumption during Oct 2015 was maximum in the year. This is atypical pharmaceutical setup. Above figures indicate peak running KW load of around 1800KW. Theaudit was conducted with around same peak load working. The plant consumed around 33000Kwh in24 hours during audit, indicating average loading of about 1400KW.

This information confirms that the audit was conducted at loading which is almost same asaverage loading throughout the year.

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Division of loading

Above pie chart shows contribution of various sections into total electrical consumption.

Such pie charting helps in implementing recommendations if any, as sections whichcontribute significantly, can be taken up first to get more impact.

55% consumption is related to HVAC and compressors and appears to be significant area.

Critical load of 80KW is supported on various UPS with stand alone and parallel redundantconfigurations.

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Comments and Remarks

1) 33KV supply to plant is derived from a RMU fed from different lines originating fromVERNA substation. The information regarding origin of these lines is not clear and the loadingdetails with respect to time are also not available. This observation is noted here as we tried toco relate the fact shared indicating that the maintenance issues were negligible when the utilitycompany was a private player rather than GED. As lot of cables / cable terminations / jointsare involved in this distribution, there are chances of cable / transformer capacity issues andloose contacts, which need through checking of GED infrastructure. We are highlighting thisas number and level of voltage fluctuations observed on 33KV side within 24 hours areabnormal.

2) This is most upstream point in electrical distribution system in the plant. This point on thedistribution is also monitored by utility company supply code. Harmonics compliance limitshere are decided by applying provisions of IEEE 519 1992. If the harmonic levels areexcessive here, they can harm infrastructure installed by utility company prior to this PCC –Point of common coupling. (Theoretically PCC is defined as such nearest upstream point onutility distribution from which they can feed another consumer. It is not practical to get accessto such point so this point within plant premises is considered for monitoring.)

3) It can be seen that the reactive power requirement on continuous basis is negligible andaverage power factor is 0.99. Average current harmonic distortion is around 10%, which maybe border case.

5) Maintaining unity power factor by controlling reactive compensation and harmonic distortiongoes hand in hand and in turn can affect power quality, if executed using a wrong method.

6) Power factor control is achieved using contactor switched detuned filters. Due to this harmonicamplification is observed to be negligible.

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4) It appears from bills that utility company charges for 75% of contract demand, if actual MD isless than that. This has happened in all the months. There is 5% incentive on energy charges ifpower factor is maintained at 0.99 and above. A Leading Pharmaceuticals Company has claimed this incentive in all themonths.

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Sr Parameter ComplianceRequirement

Actual Valuerecorded

1 Total % current harmonic distortion 15% 13.2%2 % current harmonic distortion for

harmonic orders less than 1112% 8%

3 Total % voltage harmonic distortion < 5% 1.8% (6.8%)

7) List of alarms and transients is quite alarming. We have tried to match 33KV side alarms withLV side voltage disturbances recorded on one of the transformers. Even if we consider them asload generated and reflecting on primary side, the reason would be larger source impedance orinadequate source capacity.

8) During discussions with plant staff, we were given to understand that the utility power failscouple of times every day in abrupt manner. Abrupt power interruption is also a power qualityissue. It was also informed to us that most of the failures are observed in plant area, whereRaw power is supplied and the problems were minimum when the Raw power was availablefrom Reliance.

9) Considering point 6 and 7 above, we advise you to take “Power Quality Requirements” frommachine manufacturers in detail. A specific enquiry also should be made highlighting powerfailures. Once these details are received, we can check compliance against now availablepower quality data and then conclude about cause of failures. We are highlighting this becauseas per our experience, there is a possibility of fragile design which can cause such failures.Generally machine manufacturer should give following data.

Sr Parameter Value / Range1 Sine AC Voltage – Nominal + / - %2 Voltage Wave form distortion THDV allowed %3 Frequency – Nominal + / - %4 Source impedance ohms5 Nominal current / Max current6 Nominal KVA / Max KVA7 Specify allowable limits for sub cycle and RMS voltage dips and recovery

time for which machine performance will not be adversely affected.8 Do you specify any input breaker and cable capacity for the machine, if

yes, give ratings.9 Max current distortion caused due to nature of load THDI%10 Connection – 1ph/2,3 wire or 3 ph/ 3,4,5 wire11 Dedicated earthing required / not required12 Can abrupt power failure cause electrical / electronic part failure?13 Does machine always require un interrupted power and orderly shut down14 What is the temperature and humidity range for reliable operation of

machine electrical and electronic parts15 Do you recommend dust free air-conditioned atmosphere for reliable

machine performance

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Comments and Remarks

1) This is most upstream point in transformer 1 secondary circuit. The average loading here is700KW, while peak loading is 872KW.

2) It can be seen that the reactive power requirement on continuous basis is negligible andaverage power factor is 0.99. Average current harmonic distortion is below 10%.

3) Maintaining unity power factor by controlling reactive compensation and harmonicdistortion goes hand in hand and in turn can affect power quality, if executed using awrong method.

4) Power factor control is achieved using contactor switched detuned filters. Due to thisharmonic amplification is observed to be negligible.

5) List of alarms and transients is quite alarming. 99 alarms are recorded during which thevoltage has crossed +/- 5% of 420volts. Few of these alarms have lasted for less than acycle whereas few have lasted for several cycles.

6) K factor observed is less than 2 and transformer peak loading is 50%. This has resulted inon load voltage harmonic distortion to be less than 2.5%.

0.02.04.06.08.010

%

1 2 3Ah5

1 2 3Ah6

1 2 3Ah7

1 2 3Ah8

1 2 3Ah9

1 2 3Ah10

15-12-2015 - 23:08:45.000

0.0

1.0

2.0

3.0

%

1 2 3Ah11

1 2 3Ah12

1 2 3Ah13

1 2 3Ah14

1 2 3Ah15

1 2 3Ah16

15-12-2015 - 23:08:45.000

Page 27: A Leading Pharmaceuticals Company - saspowertech

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Page 28: A Leading Pharmaceuticals Company - saspowertech

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Comments and remarks:1) This is most upstream point in transformer 2 secondary circuit. The average loading here is

700KW, while peak loading is 818 KW.

2) It can be seen that the reactive power requirement on continuous basis is negligible andaverage power factor is 0.98. Average current harmonic distortion is up to 13% and thereis amplification of harmonics. Occasionally voltage distortion also touches 4%.

3) Maintaining unity power factor by controlling reactive compensation and harmonicdistortion goes hand in hand and in turn can affect power quality, if executed using awrong method.

0

5

10

15

%

1 2 3Ah5

1 2 3Ah6

1 2 3Ah7

1 2 3Ah8

1 2 3Ah9

1 2 3Ah10

14-12-2015 - 23:07:50.000

0.0

1.0

2.0

3.0

4.0

%

1 2 3Ah11

1 2 3Ah12

1 2 3Ah13

1 2 3Ah14

1 2 3Ah15

1 2 3Ah16

14-12-2015 - 23:07:50.000

8.500

9.000

9.500

10.00

10.50

11.00

11.50

12.00

12.50

13.00

13.50

14.00

%

12:52:55.55614-12-2015

13:20:53.73614-12-2015

5 min/Div27:58.180 (min:s)

2.600

2.800

3.000

3.200

3.400

3.600

3.800

4.000

4.200

%

12:50:30.00014-12-2015

13:18:49.49014-12-2015

5 min/Div28:19.490 (min:s)

Current, Voltage distortionreduces if capacitors aredisconnected

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4) Power factor control is achieved using contactor switched detuned filters. Due to thisharmonic amplification is observed to be less, but in case of Tr2, load fluctuations aremore and due to this contactor switched detuned filters do not provide continuous andexact correction (This is result of inherent delay in contactor switching).

5) Chiller forms almost 33% of total load on this transformer and has a separate detuned filterpanel connected to it for power factor improvement.

6) 99 alarms are recorded during which the voltage has crossed +/- 5% of 420volts. Few ofthese alarms have lasted for less than a cycle whereas few have lasted for several cycles.Actual alarms recorded were much more, we have neglected all those alarms which wererecorded at exactly 399 volts and have considered those alarms which were bellow 399V.

7) If transformers tap – changers and secondary side connections are not checked / servicedin recent past, we recommend this to be done to rule out possibility of any lose connection.

8) During audit – HT side alarms are also recorded in large numbers. Lowest alarmconditions observed on HT side are even 50% of nominal voltage of 33KV.

9) K factor observed is less than 2 and transformer peak loading is slightly more than 50%.

0.000

200.0

400.0

600.0

800.0

k Wk var

12:50:30.00014-12-2015

12:51:05.00015-12-2015

4 h/Div1:00:00:35 (d:h:min:s)

10) Most of the feeders on which electronic failures are observed are associated withtransformer 2. Hence we have also recorded power quality parameters on these feeders for24 hours. These feeders were suggested by A Leading Pharmaceuticals Company maintenance team.

Page 30: A Leading Pharmaceuticals Company - saspowertech

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Page 31: A Leading Pharmaceuticals Company - saspowertech

Page 31 of 46

Comments and remarks:

KW / KVAR load on the feeder

020406080

100

%

1 2 3Ah5

1 2 3Ah6

1 2 3Ah7

1 2 3Ah8

1 2 3Ah9

1 2 3Ah10

18-12-2015 - 00:42:55.000

0.0

50

100 %

1 2 3Ah11

1 2 3Ah12

1 2 3Ah13

1 2 3Ah14

1 2 3Ah15

1 2 3Ah16

18-12-2015 - 00:42:55.000

0.000

5.000

10.00

15.00

20.00

25.00

30.00

35.00

40.00

45.00

k Wk var

17:58:00.00017-12-2015

09:11:50.00018-12-2015

3 h/Div15:13:50 (h:min:s)

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Current and voltage harmonic distortion

Line to Line voltage

1) The load on this feeder is more or less constant as the same is mostly HVAC AHU / waterpump load.

2) The current harmonic distortion is too high pertaining to VFD load. The voltage distortion onDG is on higher side and touches 6.6% max. This can trouble VFDs and other sensitiveelectronic equipment.

3) The input voltage available from raw power is not stable, while the same appears to be stableon DG.

4) Abrupt power failure and change over to DG has generated large number of alarms andtransients. These disturbances can trouble critical loads.

5) K factor is also on higher side. It is recommended that incoming cable size for this MCCshould be checked for this type of load.

6) 60Amps active harmonic filter may be installed across the main incomer of this feeder. Thiswill help in reducing voltage distortion as well as K factor of this load and in turn powerquality available to this load will improve.

0.000

5.000

10.00

15.00

20.00

25.00

30.00

35.00

40.00

45.00

50.00

%

17:58:00.00017-12-2015

09:11:55.00018-12-2015

3 h/Div15:13:55 (h:min:s)

365.0370.0375.0380.0385.0390.0395.0400.0405.0410.0415.0420.0425.0430.0435.0440.0445.0450.0

V

17:58:00.00017-12-2015

01:02:36.43818-12-2015

1 h/Div7:04:36 (h:min:s)

On DG

Page 33: A Leading Pharmaceuticals Company - saspowertech

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Page 34: A Leading Pharmaceuticals Company - saspowertech

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Comments and remarks

1) The load on this feeder is more or less constant.

2) The current harmonic distortion is too high pertaining to VFD load. The voltage distortion onDG is on higher side and touches 5.5% max. This can trouble VFDs and other sensitiveelectronic equipment.

3) Abrupt power failure and change over to DG has generated large number of alarms andtransients. These disturbances can trouble critical loads.

4) K factor is also on higher side. It is recommended that cable size for incoming supply to thisMCC should be checked for this type of load.

5) 60Amps active harmonic filter may be installed across the main incomer of this feeder. Thiswill help in reducing voltage distortion as well as K factor of this load and in turn powerquality available to this load will improve.

0

5

10

15

20

A

1 2 3AhAbs5

1 2 3AhAbs6

1 2 3AhAbs7

1 2 3AhAbs8

1 2 3AhAbs9

1 2 3AhAbs10

17-12-2015 - 05:24:04.000

0.01.02.03.04.05.0

A

1 2 3AhAbs11

1 2 3AhAbs12

1 2 3AhAbs13

1 2 3AhAbs14

1 2 3AhAbs15

1 2 3AhAbs16

17-12-2015 - 05:24:04.000

0.000

5.000

10.00

15.00

20.00

25.00

30.00

35.00

40.00

45.00

50.00

55.00

k Wk var

03:00:00.00017-12-2015

09:51:30.00017-12-2015

1 h/Div6:51:30 (h:min:s)

Page 35: A Leading Pharmaceuticals Company - saspowertech

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Page 36: A Leading Pharmaceuticals Company - saspowertech

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Comments and Remarks

Line to Line voltage

There was a power failure during recoding time. The voltage is more stable during the periodwhen DG is ON.

KW Load

This is process MCC and the load is continuously variable.

0

10

20

30

40

A

1 2 3AhAbs5

1 2 3AhAbs6

1 2 3AhAbs7

1 2 3AhAbs8

1 2 3AhAbs9

1 2 3AhAbs10

17-12-2015 - 19:13:58.000

0.02.04.06.08.010

A

1 2 3AhAbs11

1 2 3AhAbs12

1 2 3AhAbs13

1 2 3AhAbs14

1 2 3AhAbs15

1 2 3AhAbs16

17-12-2015 - 19:13:58.000

0.000

50.00

100.0

150.0

200.0

250.0

300.0

350.0

400.0

450.0

V

17:54:08.00017-12-2015

04:59:59.00018-12-2015

2 h/Div11:05:51 (h:min:s)

0.000

5.000

10.00

15.00

20.00

25.00

30.00

35.00

40.00

45.00

50.00

55.00

60.00

65.00

k W

17:54:08.00017-12-2015

04:59:59.00018-12-2015

2 h/Div11:05:51 (h:min:s)

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K Factor

The load is variable and Non linear in nature. Load current in all three phases is not equal.Load exhibits large K factor ranging from 2.5% to 30%.Line current Amps

Line current is not balanced and also fluctuates continuouslyCurrent imbalance

There is substantial current imbalance as a result of nature of load.

0.000

5.000

10.00

15.00

20.00

25.00

30.00

35.00

40.00

17:54:08.00017-12-2015

04:59:59.00018-12-2015

2 h/Div11:05:51 (h:min:s)

0.000

20.00

40.00

60.00

80.00

100.0

120.0

A

17:54:08.00017-12-2015

04:59:59.00018-12-2015

2 h/Div11:05:51 (h:min:s)

0.000

5.000

10.00

15.00

20.00

25.00

30.00

35.00

40.00

45.00

50.00

%

17:54:08.00017-12-2015

04:59:59.00018-12-2015

2 h/Div11:05:51 (h:min:s)

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Current harmonic distortion

Current distortion ranges from 10% to 90%.Voltage harmonic distortion

Corresponding voltage harmonic distortion ranges from 3% to 6%.

1) The load on this feeder is continuously variable and also largely nonlinear. The load is notsame on all the phases – may be as requirement of process machines.

2) The current harmonic distortion is too high. The voltage distortion on DG is on higher sideand touches 5% max. This can trouble VFDs and other sensitive electronic equipment.

3) Abrupt power failure and change over to DG has generated large number of alarms andtransients. These disturbances can trouble critical loads.

4) K factor is also on higher side. It is recommended that incoming cable size for this MCCshould be checked for this type of load.

5) 60Amps active harmonic filter may be installed across the main incomer of this feeder. Thiswill help in reducing voltage distortion as well as K factor of this load and in turn powerquality available to this load will improve.

0.000

20.00

40.00

60.00

80.00

100.0

%

17:54:08.00017-12-2015

04:59:59.00018-12-2015

2 h/Div11:05:51 (h:min:s)

0.000

2.000

4.000

6.000

8.000

10.00

%

17:54:08.00017-12-2015

04:59:59.00018-12-2015

2 h/Div11:05:51 (h:min:s)

Page 39: A Leading Pharmaceuticals Company - saspowertech

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Page 40: A Leading Pharmaceuticals Company - saspowertech

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Comments and remarks

Line to Line voltage

Voltage varies continuously. One can see many operations of tap changer.Load current:

0

10

20

30

40

A

1 2 3AhAbs5

1 2 3AhAbs6

1 2 3AhAbs7

1 2 3AhAbs8

1 2 3AhAbs9

1 2 3AhAbs10

16-12-2015 - 17:31:57.000

0.0

2.0

4.0

6.0

A

1 2 3AhAbs11

1 2 3AhAbs12

1 2 3AhAbs13

1 2 3AhAbs14

1 2 3AhAbs15

1 2 3AhAbs16

16-12-2015 - 17:31:57.000

360.0

380.0

400.0

420.0

440.0

V

15:25:22.00016-12-2015

02:59:59.00017-12-2015

2 h/Div11:34:37 (h:min:s)

50.00

100.0

150.0

200.0

250.0

300.0

350.0

A

15:25:22.00016-12-2015

02:59:59.00017-12-2015

2 h/Div11:34:37 (h:min:s)

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Current harmonic distortion

Current harmonic distortion varies from 5% to 45%.

1) The load on this feeder is continuously variable and also largely nonlinear.

2) The current harmonic distortion is too high. The voltage distortion caused due to this is notvery alarming as the same is below 5%.

3) This recording is done purely on raw power and not on DG. As shown on next page Tr2secondary voltage (which is source for this feeder) follows 33KV input. Incoming 33KV iscorrected frequently by upstream utility side tap - changer and the associated voltagevariations are reflected on transformer secondary and further they reach this feeder.

4) Frequent peak inrush current requirements ranging from 150Amps to 380Amps are observedon this feeder, whereas average requirement is bellow 100Amps. If possible these loads maybe identified and provided with soft starters. (If they are motor loads)

5) The majority of the load catered by this feeder is non linear and current distortion ranges from15% to 45%. We recommend 60Amps active harmonic filter across the main incomer of thisfeeder. This will help reducing high frequency currents carried by long incoming cables.

5.000

10.00

15.00

20.00

25.00

30.00

35.00

40.00

45.00

50.00

%

15:25:22.00016-12-2015

02:59:59.00017-12-2015

2 h/Div11:34:37 (h:min:s)

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Voltage trends recorded at 33KV, Tr1 secondary and Tr2 secondary.

TR 1

TR 2

33KV

33KV and TR2 secondary trends are recorded on independent power analysers, simultaneously. Thetrend is presented above with same START TIME. One can see that source of most of the voltagevariations seen on TR2 secondary is variation on 33KV incoming line.

0.000

50.00

100.0

150.0

200.0

250.0

300.0

350.0

400.0

450.0

V

12:56:21.00015-12-2015

23:59:59.00015-12-2015

2 h/Div11:03:38 (h:min:s)

360.0

380.0

400.0

420.0

440.0

460.0

V

12:50:30.00014-12-2015

00:29:59.00015-12-2015

2 h/Div11:39:29 (h:min:s)

15.00

20.00

25.00

30.00

35.00

k

12:50:30.00014-12-2015

23:59:59.00014-12-2015

2 h/Div11:09:29 (h:min:s)

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Feeder wise Power Quality Report

This column clearly shows that majority ofthe load is non linear and demands harmoniccurrent,

Page 44: A Leading Pharmaceuticals Company - saspowertech

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These harmonic currents generate electrical noise which travels through the distribution in eitherconducted or radiated mode or both. At present the reactive power compensation at transformermain LT, being of detuned type, avoids resonance and harmonic amplification while correcting thepower factor, but these harmonic currents travel to their respective common bus bars, get addedvectorially and travel further upstream. Their presence is damped only due to phase cancellation ateach common point. In case the maintenance issues are at bothering level, these harmonic currentsneed to be constrained to flow upto possible downstream level. This can be achieved by connectingactive harmonic filters at respective PCCs which help in cancelling the harmonic currents by drawingantiphase currents from source. We have recommended active filters at various feeders in abovetable. TR 2 implementations may be done on priority and TR 1 may be compensated subsequentlyas per available budgets.

Page 45: A Leading Pharmaceuticals Company - saspowertech

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UPS Input side Power Quality Parameters and Overall efficiency.

UPS output side PQ parameters

Almost all UPS systems have Thyristor input stagesand hence draw harmonic currents from source.The UPS load is hardly 5% of total plant load, sothis is not major matter of concern.

Due to part load conditions, overall efficiency isabout 80% and plant spends 20Kwh / hour onconditioning the power and supplyinguninterrupted power to various critical loads.

UPS installed capacity is 480KVA, while their outputssupply 81KW to various loads which are nonlinear. TheUPS output voltage distortion is less than 2% whilesupplying load.

Page 46: A Leading Pharmaceuticals Company - saspowertech

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Earthing Resistance

Above table shows earthing resistance measured within loop. The Neutral Earthing Resistance fortransformer 2 is slightly on higher side and should be attended. Rest all earthings are in goodcondition.